Wilhelms, Frank; Miller, Heinz; Gerasimoff, Michael D; Drücker, Cord; Frenzel, Andreas; Fritzsche, Diedrich; Grobe, Hannes; Hansen, Steffen Bo; Hilmarsson, Sverrir Æ; Hoffmann, Georg; Hörnby, Kerstin; Jaeschke, Andrea; Jakobsdottir, Steinunn S; Juckschat, Paul; Karsten, Achim; Karsten, Lorenz; Kaufmann, Patrik R; Karlin, Torbjörn; Kohlberg, Eberhard; Kleffel, Guido; Lambrecht, Anja; Lambrecht, Astrid; Lawer, Gunther; Schärmeli, Ivan; Schmitt, Jochen; Sheldon, Simon G; Takata, Morimasa; Trenke, Marcus; Twarloh, Birthe; Valero Delgado, Fernando; Wilhelms-Dick, Dorothee (2014): EPICA Dronning Maud Land EDML ice core drilling protocol [dataset]. PANGAEA, https://doi.org/10.1594/PANGAEA.841035, Supplement to: Wilhelms, F et al. (2014): The EPICA Dronning Maud Land deep drilling operation. Annals of Glaciology, 55(68), 355-366, https://doi.org/10.3189/2014AoG68A189
Always quote citation above when using data! You can download the citation in several formats below.
Abstract:
We report on the EPICA Dronning Maud Land (East Antarctica) deep drilling operation. Starting with the scientific questions that led to the outline of the EPICA project, we introduce the setting of sister drillings at NorthGRIP and EPICA Dome C within the European ice-coring community. The progress of the drilling operation is described within the context of three parallel, deep-drilling operations, the problems that occurred and the solutions we developed. Modified procedures are described, such as the monitoring of penetration rate via cable weight rather than motor torque, and modifications to the system (e.g. closing the openings at the lower end of the outer barrel to reduce the risk of immersing the drill in highly concentrated chip suspension). Parameters of the drilling (e.g. core-break force, cutter pitch, chips balance, liquid level, core production rate and piece number) are discussed. We also review the operational mode, particularly in the context of achieved core length and piece length, which have to be optimized for drilling efficiency and core quality respectively. We conclude with recommendations addressing the design of the chip-collection openings and strictly limiting the cable-load drop with respect to the load at the start of the run.
Further details:
Talalay, Pavel G (2014): Drill heads of the deep ice electromechanical drills. Cold Regions Science and Technology, 97, 41-56, https://doi.org/10.1016/j.coldregions.2013.09.009
Project(s):
Funding:
Fifth Framework Programme (FP5), grant/award no. EVK2-CT-2000-00077: European Project for Ice Coring in Antarctica
Fourth Framework Programme (FP4), grant/award no. ENV4980702: European Project for Ice Coring in Antarctica
Coverage:
Latitude: -75.002500 * Longitude: 0.068400
Date/Time Start: 2001-01-10T00:00:00 * Date/Time End: 2006-01-17T00:00:00
Minimum DEPTH, ice/snow: 91.54 m * Maximum DEPTH, ice/snow: 2761.77 m
Event(s):
EDML (EPICA Dronning Maud Land, DML28C01_00) * Latitude: -75.002500 * Longitude: 0.068400 * Date/Time Start: 2001-01-10T00:00:00 * Date/Time End: 2006-01-17T00:00:00 * Elevation: 2891.7 m * Recovery: 2774.15 m * Campaign: EPICA-Campaigns * Basis: Kohnen Station * Method/Device: EPICA drill (EDRILL) * Comment: Elevation is given with reference to WGS84
Comment:
DEPTH, ice/snow [m] = Drilled depth, measured cable length. For offset to core depth refer to reference.
Parameter(s):
# | Name | Short Name | Unit | Principal Investigator | Method/Device | Comment |
---|---|---|---|---|---|---|
1 | Run | Run | Wilhelms, Frank | The run number, without prefix drilling run, "FR": filter run, "RR": reaming run, "START": start of season, "END": end of season | ||
2 | Run Date/Time | Run Date/Time | Wilhelms, Frank | Date/Time when run was started (GMT) | ||
3 | Core length | Core length | cm | Wilhelms, Frank | Total length of fitted core pieces immediately after core retrieval | |
4 | Number | n | # | Wilhelms, Frank | Number of core pieces counted immediately after core retrieval | |
5 | Break strength | Break str | daN | Wilhelms, Frank | Force needed to break the core as recorded with a load cell in the top tower wheel | |
6 | Mass | Mass | kg | Wilhelms, Frank | Weight of the spin extractor dried chips. See reference for the residual liquid content. | |
7 | DEPTH, ice/snow | Depth ice/snow | m | Geocode | ||
8 | Comment | Comment | Wilhelms, Frank | Special remarks on the run | ||
9 | Comment | Comment | Wilhelms, Frank | Special remarks related to the electronics | ||
10 | Comment | Comment | Wilhelms, Frank | Special remarks related to the pump | ||
11 | Pitch, lower limit | Pitch low | mm | Wilhelms, Frank | Minimal distance between 3 grooves on the core surface (P.G. Talalay, 2014) | |
12 | Pitch, upper limit | Pitch up | mm | Wilhelms, Frank | Maximal distance between 3 grooves on the core surface (P.G. Talalay, 2014) | |
13 | Level | Level | m | Wilhelms, Frank | Drilled depth when the top of the drilling liquid column is reached. See reference for details. | |
14 | Volume | Vol | m3 | Wilhelms, Frank | The volume of the drilling liquid pumped into the hole measured with a flow meter | |
15 | Density, mass density | Density | kg/m3 | Wilhelms, Frank | The density of the drilling liquid pumped to the hole simultaneosly measured with an aerometer and an alcohol thermometer | |
16 | Temperature, technical | T tech | °C | Wilhelms, Frank | The temperature of the drilling liquid pumped to the hole simultaneosly measured with an aerometer and an alcohol thermometer |
License:
Creative Commons Attribution-NonCommercial 3.0 Unported (CC-BY-NC-3.0)
Size:
14880 data points
Data
1 Run (The run number, without prefi...) | 2 Run Date/Time (Date/Time when run was starte...) | 3 Core length [cm] (Total length of fitted core p...) | 4 n [#] (Number of core pieces counted...) | 5 Break str [daN] (Force needed to break the cor...) | 6 Mass [kg] (Weight of the spin extractor ...) | 7 Depth ice/snow [m] | 8 Comment (Special remarks on the run) | 9 Comment (Special remarks related to th...) | 10 Comment (Special remarks related to th...) | 11 Pitch low [mm] (Minimal distance between 3 gr...) | 12 Pitch up [mm] (Maximal distance between 3 gr...) | 13 Level [m] (Drilled depth when the top of...) | 14 Vol [m3] (The volume of the drilling li...) | 15 Density [kg/m3] (The density of the drilling l...) | 16 T tech [°C] (The temperature of the drilli...) |
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
1 | 2002-01-25T10:02 | 91.54 | several bangs with 50 to 70 cm/s before drilling gets started | 0.224 | 918.0 | -26.5 | |||||||||
2 | 2002-01-25T11:55 | 94.33 | |||||||||||||
3 | 2002-01-25T12:36 | 96.06 | pump deformed, upper wave filed and brass glide bearings replaced | ||||||||||||
4 | 2002-01-25T16:20 | 96.86 | |||||||||||||
5 | 2002-01-25T18:13 | 97.23 | clogged chips in the pump's springs | ||||||||||||
6 | 2002-01-25T18:45 | 97.74 | |||||||||||||
7 | 2002-01-25T20:08 | 98.79 | slight damage on glide bearings | ||||||||||||
8 | 2002-01-25T20:55 | 99.41 | |||||||||||||
9 | 2002-01-25T21:27 | 100.34 | |||||||||||||
10 | 2002-01-25T22:05 | 100.95 | |||||||||||||
11 | 2002-01-25T22:27 | 21.7 | 2 | 101.03 | bang with 30 to 50 cm/s, antitorque rotation | ||||||||||
12 | 2002-01-26T10:05 | 81.0 | 3 | 137 | 13.00 | 101.83 | |||||||||
13 | 2002-01-26T10:40 | 97.0 | 2 | 202 | 102.78 | ||||||||||
14 | 2002-01-26T11:32 | 65.0 | 1 | 287 | 103.68 | ||||||||||
15 | 2002-01-26T12:20 | 83.0 | 1 | 271 | 26.50 | 104.47 | 0.000 | 3.500 | |||||||
16 | 2002-01-26T15:28 | 113.0 | 1 | 292 | 105.82 | 4.000 | 4.200 | 0.200 | 920.0 | -26.0 | |||||
17 | 2002-01-26T16:20 | 128.0 | 2 | 133 | 16.00 | 106.78 | change to long drill, offset in depth scale 4.26 m, corrected for previous runs | ||||||||
18 | 2002-01-26T17:28 | 265.0 | 1 | 197 | 18.00 | 109.84 | 4.700 | 4.700 | |||||||
19 | 2002-01-26T18:30 | 355.0 | 1 | 199 | 18.50 | 113.23 | |||||||||
20 | 2002-01-27T15:04 | 113.28 | drill blocked at 8.5A, still blocked on surface | 92.0 | |||||||||||
21 | 2002-01-27T15:40 | 321.0 | 1 | 248 | 20.50 | 116.52 | 4.000 | 4.000 | |||||||
22 | 2002-01-27T16:40 | 335.0 | 1 | 262 | 119.83 | 0.160 | 920.0 | -26.0 | |||||||
23 | 2002-01-27T17:39 | 291 | 119.83 | antitorque rotation | |||||||||||
23 | 2002-01-27T17:39 | 37.0 | 2 | 134 | 26.00 | 120.26 | antitorque rotation | ||||||||
24 | 2002-01-27T18:35 | 344.0 | 1 | 308 | 19.00 | 123.68 | mounted new AT blades, clearance 32 mm above hammer | ||||||||
25 | 2002-01-27T20:17 | 123.75 | no power to motor | ||||||||||||
26 | 2002-01-28T11:20 | 324.0 | 1 | 359 | 19.00 | 127.06 | electronics reassembled | ||||||||
27 | 2002-01-28T12:20 | 251 | 127.60 | antitorque rotation | |||||||||||
27 | 2002-01-28T12:20 | 60.0 | 2 | 201 | 127.60 | antitorque rotation | |||||||||
FR1 | 2002-01-28T13:57 | 5.50 | 127.60 | 107.0 | |||||||||||
28 | 2002-01-28T14:35 | 345.0 | 1 | 247 | 23.00 | 131.00 | replaced two weak sprongs of flap valve | ||||||||
29 | 2002-01-28T15:38 | 330.0 | 3 | 161 | 18.00 | 134.29 | liquid sample from hole: 920 kg/m**3 at -37.5°C, drill head with 3 closed windows and 3 core catchers | 3.100 | 3.100 | 0.250 | 920.0 | -30.0 | |||
30 | 2002-01-28T18:45 | 325.0 | 1 | 216 | 19.00 | 137.55 | shoes adjusted to 29/100 mm | 3.000 | 4.000 | ||||||
31 | 2002-01-28T21:32 | 349.0 | 1 | 216 | 17.50 | 141.08 | shims for 5/100 mm removed | 4.800 | 4.800 | ||||||
32 | 2002-01-28T22:25 | 352.0 | 1 | 164 | 19.00 | 144.65 | antitorque rotation, but restart possible, liquid sample from hole 920 kg/m**3 at -37.9°C | 4.800 | 4.800 | ||||||
33 | 2002-01-29T08:48 | 203 | 144.65 | antitorque rotation | 111.0 | ||||||||||
33 | 2002-01-29T08:48 | 267.0 | 2 | 182 | 19.00 | 147.07 | antitorque rotation | ||||||||
FR2 | 2002-01-29T09:50 | 6.00 | 147.07 | very fine slush | |||||||||||
34 | 2002-01-29T10:25 | 343.0 | 1 | 191 | 17.00 | 150.61 | 4.100 | 4.300 | |||||||
35 | 2002-01-29T11:35 | 109 | 151.04 | changed to core barrel with closed windows, 35/100 mm clearance under shoes | 3.450 | 3.450 | |||||||||
35 | 2002-01-29T11:35 | 109.0 | 2 | 345 | 8.00 | 151.76 | internal fracture in lower core, due to core catchers not disengaging with closed windows | 3.450 | 3.450 | ||||||
36 | 2002-01-29T12:45 | 349.0 | 1 | 201 | 18.00 | 155.21 | switched back to core barrel with open windows, 2.5/100 mm shims removed, AT sharpened and tuned to 34 mm | 4.200 | 4.600 | 121.0 | |||||
37 | 2002-01-29T13:45 | 336.0 | 1 | 217 | 18.00 | 157.96 | 4.800 | 4.800 | 106.0 | 0.335 | 924.0 | -33.5 | |||
38 | 2002-01-29T14:45 | 339.0 | 1 | 224 | 162.01 | some fine slush from wall on the screws from pump sleeve | 4.400 | 4.800 | 110.0 | ||||||
39 | 2002-01-29T15:45 | 187 | 162.71 | changed core barrel to one with windows open, shims for 7/100 mm removed | 4.200 | 4.200 | 114.0 | ||||||||
39 | 2002-01-29T15:45 | 116.0 | 2 | 186 | 9.00 | 163.18 | liquid sample from hole 922 kg/m**3 at -38.8°C | 4.200 | 4.200 | 117.0 | |||||
40 | 2002-01-29T16:35 | 161.0 | 1 | 184 | 12.00 | 164.79 | terminated due to motor no power, working after heating to +30°C | 4.600 | 4.600 | ||||||
41 | 2002-01-29T18:45 | 347.0 | 1 | 245 | 17.00 | 168.36 | 4.400 | 4.500 | 118.0 | ||||||
42 | 2002-01-29T19:54 | 351.0 | 1 | 175 | 18.50 | 171.84 | 4.400 | 4.400 | 126.0 | ||||||
43 | 2002-01-29T20:50 | 326.0 | 1 | 304 | 18.50 | 175.14 | 4.400 | 4.800 | 126.0 | ||||||
44 | 2002-01-29T21:50 | 334.0 | 1 | 235 | 19.50 | 178.92 | 4.400 | 4.500 | 135.0 | ||||||
FR3 | 2002-01-29T23:02 | 7.00 | 178.92 | a lot of fine slush, most likely from the column | 135.0 | ||||||||||
45 | 2002-01-30T08:56 | 329.0 | 1 | 215 | 16.00 | 182.02 | 4.400 | 5.000 | |||||||
46 | 2002-01-30T09:47 | 165 | 182.10 | antitorque rotation | 4.800 | 4.800 | 106.0 | 0.550 | 922.0 | -31.6 | |||||
46 | 2002-01-30T09:47 | 302.0 | 2 | 350 | 19.50 | 184.00 | pump disengaged | 4.800 | 4.800 | ||||||
47 | 2002-01-30T11:35 | 329.0 | 1 | 336 | 18.00 | 188.12 | 4.600 | 4.700 | 108.0 | ||||||
48 | 2002-01-30T12:40 | 346.0 | 1 | 282 | 18.00 | 191.51 | 4.500 | 4.700 | 108.0 | ||||||
49 | 2002-01-30T13:45 | 279 | 192.11 | antitorque rotation | 4.200 | 4.200 | 116.0 | ||||||||
49 | 2002-01-30T13:45 | 99.0 | 3 | 279 | 8.00 | 192.36 | antitorque rotation | computer went crazy | 4.200 | 4.200 | |||||
50 | 2002-01-30T14:26 | 337.0 | 1 | 222 | 9.00 | 195.84 | 4.600 | 4.800 | 119.0 | ||||||
FR4 | 2002-01-30T15:17 | 9.80 | 195.84 | ||||||||||||
FR5 | 2002-01-30T15:45 | 3.50 | 195.84 | 119.0 | |||||||||||
51 | 2002-01-30T16:10 | 231.0 | 1 | 287 | 5.50 | 198.18 | antitorque rotation | 4.700 | 4.800 | 120.0 | |||||
52 | 2002-01-30T17:10 | 142.0 | 1 | 280 | 8.50 | 199.62 | clearance of shoes measured to 36/100 mm, put 1 shim 2.5/100 mm under shoes | changed to 19'' 486 rack computer | 3.500 | 4.800 | 128.0 | ||||
53 | 2002-01-30T21:00 | 123.0 | 1 | 220 | 11.00 | 200.87 | antitorque rotation | speed counter is disturbed, plug all electronics to one phase | switch to shaft with pump without lubrication holes | 4.200 | 4.200 | 125.0 | |||
FR6 | 2002-01-30T21:45 | 6.00 | 200.87 | removed one shim, should be approx. 36/100 mm | 128.0 | ||||||||||
54 | 2002-01-30T22:25 | 59.0 | 1 | 165 | 201.54 | Terminated due to upper pressure 1.15 ERR ON | 4.400 | 4.400 | |||||||
55 | 2002-01-31T15:21 | 67.0 | 1 | 285 | 6.00 | 202.06 | disassembled electronics, much liquid in upper space, inner tube dry | 4.700 | 4.700 | 0.450 | 921.0 | -29.7 | |||
56 | 2002-02-01T11:59 | 163.0 | 1 | 510 | 9.00 | 203.56 | redone solderings on 300 V modules, motor turns when powered on without bits set | 4.400 | 4.400 | 105.0 | |||||
57 | 2002-02-01T13:02 | 261.0 | 1 | 340 | 12.00 | 205.90 | 4.300 | 4.400 | 108.0 | ||||||
58 | 2002-02-01T14:30 | 306.0 | 1 | 397 | 17.00 | 209.39 | replaced spacer in lower spring, liquid sample from hole 925 kg/m**3 at -40°C | electric depth counter disturbed | 4.200 | 4.700 | 108.0 | ||||
59 | 2002-02-01T15:37 | 351.0 | 1 | 381 | 16.50 | 212.83 | 4.300 | 4.400 | 115.0 | ||||||
60 | 2002-02-01T16:32 | 331.0 | 1 | 315 | 20.50 | 216.17 | 4.200 | 4.300 | 118.0 | ||||||
61 | 2002-02-01T17:48 | 324.0 | 1 | 569 | 21.00 | 219.41 | 4.000 | 4.000 | 125.0 | ||||||
62 | 2002-02-01T19:40 | 328.0 | 1 | 306 | 222.70 | 3.200 | 3.400 | 131.0 | |||||||
63 | 2002-02-01T20:50 | 304.0 | 1 | 394 | 18.00 | 225.79 | removed one shim 2.5/100 mm | 4.500 | 4.600 | 132.0 | |||||
FR7 | 2002-02-01T22:00 | 4.00 | 225.79 | drill head tuned to 38-39/100 mm | 110.0 | 0.330 | 924.7 | -33.5 | |||||||
64 | 2002-02-02T10:36 | 326.0 | 1 | 435 | 16.50 | 228.97 | 4.900 | 5.200 | 116.0 | ||||||
65 | 2002-02-02T11:47 | 317.0 | 1 | 364 | 18.50 | 232.24 | 4.900 | 5.300 | 117.0 | ||||||
66 | 2002-02-02T13:02 | 290 | 232.65 | no rotation at 9 A, still blocked after core break | pump very difficult to turn | 5.000 | 5.000 | 121.0 | |||||||
66 | 2002-02-02T13:02 | 125.0 | 2 | 391 | 8.50 | 233.49 | |||||||||
67 | 2002-02-02T13:59 | 219.0 | 3 | 346 | 11.00 | 235.69 | bad penetration | icing in pump | 3.500 | 3.900 | 130.0 | ||||
68 | 2002-02-02T15:01 | 327.0 | 1 | 412 | 238.98 | turned AT blades to new sharp side, removed one core catcher | 4.600 | 4.800 | 134.0 | ||||||
69 | 2002-02-02T16:30 | 15.0 | 1 | 360 | 17.00 | 239.05 | several antitorque rotations | 5.200 | 5.200 | 138.0 | |||||
70 | 2002-02-02T17:12 | 322.0 | 1 | 304 | 16.50 | 242.26 | put in one shim 2.5/100 mm | 4.600 | 4.600 | 135.0 | |||||
71 | 2002-02-02T18:23 | 331.0 | 1 | 434 | 15.00 | 245.60 | 4.800 | 4.900 | 127.0 | 0.375 | 924.0 | -34.5 | |||
FR8 | 2002-02-03T14:03 | 8.50 | 245.60 | 120.0 | |||||||||||
72 | 2002-02-03T14:37 | 302.0 | 1 | 569 | 17.00 | 248.51 | antitorque rotations | 4.300 | 4.400 | 120.0 | |||||
73 | 2002-02-03T15:47 | 61.0 | 1 | 594 | 5.00 | 249.23 | adjusted AT springs to 31.5 mm above hammer | 4.200 | 4.200 | 122.0 | |||||
74 | 2002-02-03T16:37 | 114.0 | 1 | 420 | 7.00 | 250.31 | antitorque rotation | 4.200 | 4.300 | 126.0 | |||||
75 | 2002-02-03T17:27 | 336.0 | 1 | 543 | 17.00 | 253.71 | 4.200 | 4.200 | 134.0 | ||||||
76 | 2002-02-03T18:36 | 75.0 | 1 | 654 | 3.00 | 254.48 | 4.300 | 4.300 | 138.0 | ||||||
77 | 2002-02-03T19:46 | 335.0 | 1 | 582 | 15.00 | 257.82 | one shim removed 2.5-3/100 mm | 3.700 | 3.800 | 141.0 | |||||
78 | 2002-02-03T20:58 | 10.0 | 1 | 448 | 257.87 | 109.0 | 0.450 | 922.0 | -30.5 | ||||||
79 | 2002-02-03T21:35 | 314.0 | 1 | 382 | 16.50 | 261.05 | several antitorque rotations | flap valves partly open due to hard chips in them | 3.300 | 3.300 | 117.0 | ||||
80 | 2002-02-03T22:55 | 12.0 | 1 | 627 | 3.00 | 261.16 | 103.0 | 0.310 | 925.0 | -34.0 | |||||
FR9 | 2002-02-03T23:50 | 261.16 | |||||||||||||
FR10 | 2002-02-03T23:50 | 10.50 | 261.16 | ||||||||||||
FR11 | 2002-02-03T23:50 | 2.50 | 261.16 | ||||||||||||
81 | 2002-02-04T08:10 | 337.0 | 1 | 532 | 18.00 | 264.24 | 4.000 | 4.300 | 112.0 | ||||||
82 | 2002-02-04T09:25 | 565 | 264.92 | antitorque rotation | 106.0 | ||||||||||
82 | 2002-02-04T09:25 | 154.0 | 4 | 727 | 10.00 | 266.11 | 3.400 | 3.700 | |||||||
83 | 2002-02-04T10:46 | 227.0 | 1 | 590 | 11.00 | 268.36 | 3.700 | 3.900 | 107.0 | ||||||
84 | 2002-02-04T11:47 | 64.0 | 1 | 636 | 269.01 | no chips in chip chamber | 4.200 | 4.200 | 114.0 | ||||||
FR12 | 2002-02-04T12:47 | 5.00 | 269.01 | ||||||||||||
85 | 2002-02-04T13:25 | 343.0 | 2 | 475 | 16.00 | 272.38 | 3.600 | 3.700 | 118.0 | ||||||
86 | 2002-02-04T15:00 | 253.0 | 1 | 568 | 14.00 | 275.01 | antitorque rotation | 3.600 | 3.800 | 124.0 | |||||
87 | 2002-02-04T17:40 | 18.0 | 1 | 649 | 275.04 | changed to 300 V modules with replaced BC107 | 125.0 | ||||||||
88 | 2002-02-04T20:05 | 322.0 | 1 | 617 | 16.00 | 278.54 | 3.600 | 3.700 | 130.0 | ||||||
89 | 2002-02-04T21:20 | 264.0 | 1 | 773 | 12.00 | 281.19 | 4.700 | 4.900 | |||||||
FR13 | 2002-02-04T22:27 | 10.00 | 281.19 | 136.0 | |||||||||||
90 | 2002-02-04T23:25 | 320.5 | 1 | 520 | 14.00 | 284.36 | antitorque rotation | 4.800 | 5.000 | 113.0 | 0.360 | 926.0 | -35.5 | ||
91 | 2002-02-05T08:21 | 12.0 | 1 | 381 | 5.00 | 284.50 | 114.0 | ||||||||
92 | 2002-02-05T09:18 | 323.0 | 1 | 678 | 13.00 | 287.66 | 4.300 | 4.700 | 118.0 | ||||||
93 | 2002-02-05T10:19 | 330.0 | 1 | 692 | 15.00 | 290.90 | 4.900 | 5.000 | 123.0 | ||||||
94 | 2002-02-05T11:24 | 320.0 | 1 | 1001 | 19.00 | 294.23 | 4.700 | 5.200 | 130.0 | ||||||
95 | 2002-02-05T12:34 | 39.0 | 1 | 307 | 4.00 | 294.54 | 134.0 | ||||||||
96 | 2002-02-05T13:32 | 314.0 | 1 | 571 | 14.50 | 297.64 | reduced clearance under shoes by 2.5-3/100 mm, should now be 33-34/100 mm | 4.700 | 4.800 | 136.0 | |||||
FR14 | 2002-02-05T14:46 | 9.50 | 297.64 | 142.0 | |||||||||||
FR15 | 2002-02-05T15:34 | 5.00 | 297.64 | ||||||||||||
97 | 2002-02-05T16:22 | 327.0 | 1 | 382 | 16.00 | 301.03 | 5.200 | 5.200 | 0.500 | 924.0 | -32.5 | ||||
98 | 2002-02-05T19:08 | 82.0 | 1 | 458 | 4.00 | 301.74 | changed rotation speed in 375 electronics module | 4.800 | 5.200 | 110.0 | |||||
99 | 2002-02-05T20:10 | 266.0 | 1 | 665 | 17.00 | 304.43 | introduced 2.5/100 mm shims under shoes, should now be 31-30/100 mm | 4.200 | 4.500 | 113.0 | |||||
100 | 2002-02-05T21:35 | 250.0 | 1 | 557 | 14.50 | 306.91 | introduced 2.5/100 mm shims under shoes, should now be 27-28/100 mm | 3.700 | 3.900 | 118.0 | |||||
101 | 2002-02-05T23:00 | 398 | 307.08 | removed one shim 2.5/100 mm, should now be 30-34/100 mm clearance | 122.0 | ||||||||||
101 | 2002-02-05T23:00 | 138.0 | 2 | 661 | 9.50 | 308.23 | |||||||||
FR16 | 2002-02-06T00:19 | 3.50 | 308.23 | 123.0 | |||||||||||
102 | 2002-02-06T08:23 | 343.0 | 1 | 711 | 20.00 | 311.67 | drill head tuned to 27-28/100 mm clearance | 3.900 | 4.200 | 102.0 | 0.360 | 925.0 | -33.6 | ||
103 | 2002-02-06T09:49 | 341.0 | 1 | 501 | 20.00 | 315.14 | 4.000 | 4.200 | 105.0 | ||||||
104 | 2002-02-06T11:22 | 345.0 | 1 | 555 | 19.50 | 318.49 | 3.300 | 3.400 | 108.0 | ||||||
105 | 2002-02-06T12:59 | 318.0 | 1 | 563 | 19.00 | 321.69 | 3.700 | 3.800 | 113.0 | ||||||
106 | 2002-02-06T14:35 | 575 | 322.46 | 122.0 | |||||||||||
106 | 2002-02-06T14:35 | 349.0 | 2 | 546 | 20.00 | 325.18 | 3.600 | 3.800 | |||||||
107 | 2002-02-06T16:03 | 342.0 | 1 | 546 | 19.00 | 328.57 | 3.800 | 4.000 | 126.0 | ||||||
108 | 2002-02-06T17:37 | 343.0 | 1 | 573 | 18.00 | 331.99 | 3.800 | 4.000 | 127.0 | ||||||
109 | 2002-02-06T18:57 | 338.0 | 1 | 433 | 20.00 | 335.49 | 3.800 | 4.100 | 133.0 | ||||||
110 | 2002-02-06T20:49 | 345.0 | 1 | 465 | 20.00 | 338.98 | 3.900 | 4.100 | 138.0 | ||||||
111 | 2002-02-06T22:45 | 346.0 | 1 | 433 | 20.00 | 342.36 | 4.000 | 4.100 | 141.0 | ||||||
112 | 2002-02-07T08:20 | 330.0 | 1 | 607 | 20.50 | 345.69 | 4.000 | 4.200 | 118.0 | 0.390 | 924.0 | -33.5 | |||
113 | 2002-02-07T09:53 | 343.0 | 1 | 349 | 21.00 | 349.07 | 3.900 | 4.600 | 125.0 | ||||||
114 | 2002-02-07T11:44 | 324.0 | 1 | 764 | 20.00 | 352.36 | 4.000 | 4.200 | 126.0 | ||||||
115 | 2002-02-07T13:26 | 329.0 | 1 | 539 | 19.00 | 355.70 | antitorque rotation | 3.800 | 4.000 | 131.0 | |||||
116 | 2002-02-07T15:12 | 330.0 | 1 | 426 | 19.50 | 358.94 | antitorque rotation | 4.100 | 4.300 | 137.0 | |||||
117 | 2002-02-07T17:14 | 325.0 | 1 | 661 | 20.00 | 362.21 | 4.300 | 4.400 | 140.0 | ||||||
118 | 2002-02-07T18:43 | 331.0 | 1 | 669 | 18.50 | 365.48 | 4.000 | 4.100 | 105.0 | 0.450 | 925.0 | -34.0 | |||
119 | 2002-02-07T20:04 | 317 | 366.31 | antitorque rotation | 4.000 | 4.200 | 111.0 | ||||||||
119 | 2002-02-07T20:04 | 339.0 | 3 | 341 | 19.00 | 368.86 | 111.0 | ||||||||
120 | 2002-02-07T21:26 | 330.0 | 3 | 448 | 19.50 | 372.14 | 3.900 | 4.100 | 120.0 | ||||||
121 | 2002-02-07T23:36 | 317.0 | 2 | 558 | 19.50 | 375.30 | 126.0 | ||||||||
122 | 2002-02-08T08:28 | 331.0 | 1 | 571 | 20.00 | 378.50 | 3.500 | 3.700 | 130.0 | ||||||
123 | 2002-02-08T09:48 | 333.0 | 2 | 575 | 19.50 | 381.87 | 3.700 | 3.900 | 135.0 | ||||||
124 | 2002-02-08T11:42 | 206.0 | 1 | 1249 | 11.50 | 384.01 | 3.500 | 3.900 | 99.0 | 0.500 | 924.0 | -32.5 | |||
FR17 | 2002-02-08T13:10 | 384.01 | 101.0 | ||||||||||||
FR18 | 2002-02-08T13:54 | 5.50 | 384.01 | 102.0 | |||||||||||
125 | 2002-02-08T14:55 | 250 | 384.01 | penetration problems | electronics works after power down and surface program restart | 105.0 | |||||||||
125 | 2002-02-08T14:55 | 244.0 | 2 | 499 | 15.50 | 386.36 | 105.0 | ||||||||
126 | 2002-02-08T16:30 | 323.0 | 1 | 347 | 17.50 | 389.62 | 3.700 | 3.800 | 108.0 | ||||||
127 | 2002-02-08T18:13 | 332.0 | 1 | 672 | 19.50 | 392.89 | 3.800 | 4.000 | 113.0 | ||||||
128 | 2002-02-08T19:40 | 832 | 393.09 | removed one shim under shoes, should be 30-32/100 mm | 118.0 | ||||||||||
128 | 2002-02-08T19:40 | 78.0 | 1 | 362 | 8.00 | 393.58 | 118.0 | ||||||||
129 | 2002-02-08T20:50 | 258.0 | 1 | 478 | 15.00 | 396.19 | 3.800 | 4.600 | 121.0 | ||||||
130 | 2002-02-08T22:10 | 320.0 | 6 | 483 | 16.50 | 399.52 | 4.200 | 4.200 | 124.0 | ||||||
131 | 2002-02-08T23:30 | 226.0 | 2 | 553 | 13.50 | 401.72 | 3.900 | 4.200 | 101.0 | 0.450 | 920.0 | -28.5 | |||
FR19 | 2002-02-09T08:15 | 401.72 | 100.0 | ||||||||||||
132 | 2002-02-09T09:21 | 278.0 | 1 | 425 | 17.50 | 404.51 | 4.300 | 4.400 | 104.0 | ||||||
133 | 2002-02-09T10:35 | 144.0 | 2 | 416 | 4.50 | 405.80 | 4.200 | 4.200 | 108.0 | ||||||
134 | 2002-02-09T11:46 | 94.0 | 1 | 418 | 406.85 | 4.100 | 4.100 | 112.0 | |||||||
135 | 2002-02-09T12:45 | 328.0 | 1 | 258 | 24.00 | 410.17 | pump blocked by piece of ice | 4.000 | 4.200 | 115.0 | |||||
136 | 2002-02-09T13:52 | 327.0 | 3 | 399 | 21.00 | 413.38 | 4.100 | 4.400 | 119.0 | ||||||
137 | 2002-02-09T15:10 | 327.0 | 2 | 283 | 21.00 | 416.69 | 3.700 | 4.200 | 124.0 | ||||||
138 | 2002-02-09T16:37 | 900 | 418.86 | drill not free when pulled up 3 m | 4.100 | 4.100 | 128.0 | ||||||||
138 | 2002-02-09T16:37 | 900 | 418.86 | second pull about 3 m up, came free at 8 A rotation | |||||||||||
138 | 2002-02-09T16:37 | 215.0 | 1 | 479 | 15.00 | 418.86 | |||||||||
139 | 2002-02-09T17:46 | 5.00 | 418.92 | reaming run to clean wall | 134.0 | ||||||||||
FR20 | 2002-02-10T10:15 | 418.92 | 135.0 | ||||||||||||
140 | 2002-02-10T11:25 | 225.0 | 1 | 447 | 8.50 | 421.06 | drill head measured to 29-32/100 mm, tuned to 30/100 mm clearance | pump didn't work properly | 3.900 | 4.100 | 135.0 | ||||
141 | 2002-02-10T12:35 | 421.06 | changed to drillhead with closed windows, Rufli cutters with 30/100 mm clearance under shoes, no way to penetrate, several reaming attempts. core barrel gone! | 117.0 | 0.250 | 925.0 | -34.0 | ||||||||
142 | 2002-02-10T14:55 | 421.06 | unsuccessful fishing run with full drill | ||||||||||||
143 | 2002-02-10T15:45 | 182 | 421.06 | core barrel recovered in fishing run with HT shaft and without outer core barrel. spirals badly damaged, pcs left down hole | |||||||||||
FR21 | 2002-02-10T18:35 | 3.00 | 421.06 | 119.0 | |||||||||||
144 | 2002-02-10T20:18 | 4.0 | 4 | 421.05 | 11cm long spiral piece brought up | 120.0 | |||||||||
145 | 2002-02-10T21:30 | 221 | 421.05 | 121.0 | |||||||||||
145 | 2002-02-10T21:30 | 265 | 421.05 | fished another half of aluminum spiral | |||||||||||
146 | 2002-02-10T22:30 | 332 | 421.05 | several hard bangs, no way to start run | 122.0 | ||||||||||
147 | 2002-02-10T23:32 | 52.0 | 1 | 435 | 422.06 | changed to Viking knives, 32/100 mm clearance | 120.0 | ||||||||
FR22 | 2002-02-11T08:30 | 422.06 | 122.0 | ||||||||||||
148 | 2002-02-11T10:06 | 326.0 | 1 | 554 | 24.00 | 424.86 | 4.100 | 4.300 | 124.0 | ||||||
149 | 2002-02-11T11:45 | 274.0 | 1 | 550 | 12.50 | 427.72 | 128.0 | ||||||||
150 | 2002-02-11T13:28 | 310.0 | 3 | 294 | 18.00 | 430.81 | 4.000 | 4.200 | 134.0 | ||||||
151 | 2002-02-11T15:19 | 74.0 | 1 | 458 | 431.52 | 4.000 | 4.200 | 140.0 | |||||||
152 | 2002-02-11T17:05 | 97.0 | 1 | 754 | 8.00 | 432.68 | 3.300 | 3.300 | 140.0 | ||||||
153 | 2002-02-11T19:18 | 78.0 | 1 | 535 | 8.50 | 433.23 | 120.0 | 0.200 | 922.0 | -31.0 | |||||
154 | 2002-02-11T20:50 | 119.0 | 1 | 448 | 7.00 | 434.42 | several antitorque rotations | ||||||||
155 | 2002-02-11T22:00 | 69.0 | 1 | 587 | 435.20 | 3.900 | 4.000 | 117.0 | 0.120 | 920.0 | -27.7 | ||||
FR23 | 2002-02-11T23:06 | 2.50 | 435.20 | 120.0 | |||||||||||
156 | 2002-02-12T09:09 | 33.0 | 1 | 242 | 435.48 | 1 screw head brought up with chips | 118.0 | ||||||||
157 | 2002-02-12T10:45 | 333.0 | 1 | 502 | 24.00 | 438.80 | cutters sharpened | 4.600 | 4.600 | 121.0 | |||||
END | 2002-02-12T16:00 | 438.80 | 55.0 | 1.500 | 920.0 | -29.0 | |||||||||
START | 2002-12-21T15:46 | 438.27 | use long drill with windows on lower end closed by welding | put on 50 V motor with 80:1 gear | 81.5 | ||||||||||
FR24 | 2002-12-21T21:19 | 438.27 | created little kinck in cable about 6 m on top of drill, new termination with pull test to 17430 N | 82.0 | |||||||||||
158 | 2002-12-21T20:38 | 5.00 | 438.27 | disturbed pressure sensors | 90.0 | ||||||||||
159 | 2002-12-25T16:37 | 47.0 | 2 | 612 | 438.60 | put on head new Rufli No. 4 head with 0.26 mm clearance to front and 0.7 mm to tail of shoe, stopped due to persistent antitorque rotation, use cutters with outer side cutting edge all to the top | put on 60 V motor with 80:1 gear | 3.800 | 4.000 | ||||||
160 | 2002-12-26T09:20 | 36.0 | 1 | 138 | 6.00 | 439.30 | stopped due to persistent antitorque rotation even at slow rotation speed, picked up two pieces from brass screw, cutter damaged | 4.200 | 4.200 | ||||||
161 | 2002-12-26T11:05 | 45.0 | 2 | 247 | 2.50 | 439.63 | tuned antitorque from 33 mm to 34 mm above hammer, still persistent antitorque rotation | 4.300 | 4.300 | ||||||
162 | 2002-12-26T16:00 | 49.0 | 1 | 311 | 2.00 | 440.30 | changed to HT drill with same head and plastic flights, stopped due to antitorque rotation | 4.600 | 4.600 | ||||||
163 | 2002-12-26T17:00 | 122 | 440.42 | adjusted antitorque to 31 mm above hammer, no way to penetrate | |||||||||||
164 | 2002-12-26T18:10 | 440.42 | adjusted antitorque to 36 mm above hammer | high pressure seal stat leakage | |||||||||||
165 | 2002-12-26T20:30 | 55.0 | 1 | 260 | 440.87 | stopped due to antitorque rotation | 4.400 | 4.400 | |||||||
166 | 2002-12-26T21:37 | 440.87 | termination of run because of pressure in stat seal fast rising | ||||||||||||
167 | 2002-12-27T09:40 | 38.5 | 1 | 396 | 3.50 | 441.11 | stopped due to antitorque rotation problems | had pressure section drying over night and mounted it warm in the morning | 4.200 | 4.200 | |||||
168 | 2002-12-27T10:35 | 441.11 | termination of run because of pressure in stat seal fast rising | ||||||||||||
169 | 2002-12-27T11:52 | 441.11 | heated lower end of pressure tube till it was hand warm, termination of run due to non tight seal | ||||||||||||
170 | 2002-12-27T17:03 | 441.19 | mounted section with 60 V motor and 50:1 gear, not enough torque to drill | ||||||||||||
171 | 2002-12-27T22:18 | 83.0 | 1 | 206 | 442.00 | mounted section with 60 V motor and 80:1 gear | ice pieces in pump | 92.0 | |||||||
172 | 2002-12-28T09:03 | 110.0 | 1 | 450 | 10.00 | 443.00 | 4.400 | 4.500 | 92.0 | ||||||
173 | 2002-12-28T10:36 | 67.0 | 1 | 316 | 443.80 | drill blocked for unidentified reason, 8 cm of chips on top of core | 4.200 | 4.200 | 93.0 | ||||||
174 | 2002-12-28T12:03 | 102.0 | 1 | 330 | 444.92 | 16 cm of chips on top of core | 4.400 | 4.400 | 93.0 | ||||||
175 | 2002-12-28T13:45 | 60.0 | 1 | 397 | 6.00 | 445.49 | stopped dur to persistent antitorque rotation | 4.100 | 4.300 | 94.0 | |||||
176 | 2002-12-28T14:50 | 88.0 | 1 | 354 | 446.39 | antitorque rotation at 9 A | 4.500 | 4.500 | 96.0 | ||||||
177 | 2002-12-28T16:22 | 11.0 | 1 | 340 | 11.00 | 446.20 | switched to long drill with same drill head, persistent antitorque rotation | 97.0 | |||||||
178 | 2002-12-29T13:38 | 8.5 | 1 | 160 | 446.40 | sharpened antitorque and adjusted to 33 mm above hammer, changed to Rufli head 0 with 0.22 mm clearance to front and 0.62 mm clearance to tail of shoe | 98.0 | ||||||||
179 | 2002-12-29T15:00 | 10.5 | 1 | 198 | 446.45 | tuned antitorque to 37 mm above hammer, stop due to blocked drill at 8 A | 99.0 | ||||||||
180 | 2002-12-29T16:20 | 22.0 | 1 | 174 | 446.68 | put on Rufli head 4 with nominal pitch of 4.5 mm, stop due to antitorque rotation | 99.5 | ||||||||
181 | 2002-12-29T17:50 | 195 | 446.70 | too high idle current, pull up slowly to preserve packing on drill head, on surface two channels blocked | 101.0 | ||||||||||
182 | 2002-12-29T19:43 | 55.0 | 1 | 325 | 447.35 | changed to HT drill with pump and Al-flights with same drillhead | chip chamber full | 4.500 | 4.600 | 97.0 | |||||
183 | 2002-12-29T22:08 | 122.0 | 1 | 442 | 15.00 | 448.63 | 94.0 | ||||||||
184 | 2002-12-30T09:00 | 90.0 | 1 | 250 | 449.45 | blocked at 8 A, antitorque rotation at 9 A | 94.0 | ||||||||
185 | 2002-12-30T10:25 | 86.5 | 1 | 487 | 450.35 | valve open, chip chamber only 2/10 filled | 94.0 | ||||||||
186 | 2002-12-30T11:53 | 46.0 | 1 | 678 | 450.87 | changed screws of valve, stopped due to no rotation at 10.2 A | 4.800 | 4.800 | 94.0 | ||||||
187 | 2002-12-30T13:22 | 125.0 | 1 | 377 | 17.00 | 452.09 | put on Rufli head from last year with 0.21 mm clearance to front and 0.62 mm clearance to tail of shoe | 3.800 | 3.900 | ||||||
188 | 2002-12-30T14:35 | 127.0 | 1 | 343 | 453.35 | 3.800 | 3.800 | 94.0 | |||||||
189 | 2002-12-30T16:18 | 37.0 | 1 | 250 | 11.00 | 453.50 | changed to long drill with same drill head, pulled up for security because of fast dropping load | 3.800 | 3.800 | 98.0 | |||||
190 | 2002-12-30T17:46 | 35.0 | 1 | 202 | 453.99 | not cutting at too much load drop | 3.300 | 3.300 | 98.0 | ||||||
191 | 2002-12-30T20:05 | 78.0 | 1 | 256 | 6.00 | 454.85 | put in three spacer rings between pump and superbanger, drill head has now about 18 mm clearance to lower end of outer barrel | 3.300 | 3.300 | 0.402 | 916.0 | -24.0 | |||
192 | 2002-12-31T09:00 | 2 | 350 | 454.85 | |||||||||||
192 | 2002-12-31T09:00 | 74.0 | 2 | 324 | 455.33 | stopped due to high idle current | 2.600 | 2.800 | |||||||
193 | 2002-12-31T12:38 | 90.0 | 1 | 548 | 456.51 | 3.000 | 3.100 | 112.0 | |||||||
194 | 2002-12-31T14:23 | 443 | 457.56 | ||||||||||||
194 | 2002-12-31T14:23 | 207.0 | 3 | 491 | 19.50 | 458.55 | stopped for security after 2 m | 3.000 | 3.000 | 106.0 | |||||
195 | 2002-12-31T16:15 | 496 | 459.62 | break core for security | |||||||||||
195 | 2002-12-31T16:15 | 183.0 | 2 | 529 | 10.00 | 460.38 | run stopped due to rising current | 2.900 | 2.950 | 105.0 | |||||
196 | 2003-01-01T12:30 | 53.0 | 1 | 359 | 7.00 | 460.89 | antitorque adjusted to 34 mm, stopped due to antitorque rotation | 2.950 | 2.950 | ||||||
197 | 2003-01-01T14:05 | 36.0 | 1 | 303 | 461.22 | changed to groove bended Gerasimoff antitorque blades, clearance about 25 mm over hammer, stopped due to antitorque rotation at 6 A | 2.950 | 2.950 | 126.0 | ||||||
198 | 2003-01-01T15:10 | 103.0 | 1 | 331 | 8.00 | 462.21 | termination to check drill head | 2.700 | 2.940 | ||||||
199 | 2003-01-01T16:56 | 210.0 | 1 | 228 | 12.00 | 464.39 | 3.600 | 3.600 | 125.0 | ||||||
200 | 2003-01-01T18:14 | 202.0 | 1 | 446 | 11.00 | 466.47 | 2.600 | 3.500 | 128.0 | ||||||
201 | 2003-01-01T20:20 | 220.0 | 1 | 376 | 13.00 | 468.72 | 3.450 | 3.650 | |||||||
202 | 2003-01-02T09:40 | 46.0 | 1 | 322 | 2.50 | 469.08 | cutters sharpened, clearance 0.22 mm for all cutters to front end of shoe, terminated due to antitorque rotation at 8.8 A | 3.450 | 3.450 | ||||||
203 | 2003-01-02T10:55 | 28.0 | 1 | 272 | 468.73 | antitorque adjusted to 31 mm clearance, replaced 5 mm by 3 mm spacer to have lock screw clamping on thread all it's way, head-outer barrel clearance now 16 mm, terminated due to antitorque rotation | 3.700 | 3.700 | |||||||
204 | 2003-01-02T11:51 | 74.0 | 1 | 312 | 470.17 | antitorque adjusted to 32 mm now | 144.0 | ||||||||
205 | 2003-01-02T13:04 | 23.0 | 1 | 243 | 470.29 | stopped due to blocked drilled at 10.5 A | 3.440 | 3.440 | 0.402 | 917.0 | -25.0 | ||||
206 | 2003-01-02T14:33 | 333 | 470.78 | antitorque rotation | 120.0 | ||||||||||
206 | 2003-01-02T14:33 | 219.0 | 2 | 565 | 13.00 | 472.55 | 3.650 | 3.650 | |||||||
207 | 2003-01-02T15:44 | 57.0 | 1 | 286 | 2.00 | 473.20 | fake reading of upper pressure | 3.500 | 3.500 | 125.0 | |||||
208 | 2003-01-02T16:51 | 261 | 473.94 | blocked at 10 A, antitorque rotation at 12 A | |||||||||||
208 | 2003-01-02T16:51 | 261.0 | 1 | 375 | 16.00 | 475.71 | blocked at 12.4 A, no antitorque rotation | 3.400 | 3.600 | 127.0 | |||||
209 | 2003-01-02T18:33 | 433 | 476.56 | antitorque rotation at 8.8 A | |||||||||||
209 | 2003-01-02T18:33 | 320.0 | 2 | 480 | 18.50 | 478.87 | fake readings of electronics | 3.600 | 3.600 | 128.0 | |||||
210 | 2003-01-02T20:24 | 361 | 480.05 | antitorque rotation at 10.5 A | |||||||||||
210 | 2003-01-02T20:24 | 290.0 | 2 | 578 | 17.50 | 481.31 | more than 25 fake readings | 3.500 | 3.640 | 135.0 | |||||
211 | 2003-01-03T08:58 | 154.0 | 1 | 503 | 10.00 | 483.40 | power failure in trench | more than 20 fake readings | 3.500 | 3.700 | 140.0 | ||||
212 | 2003-01-03T11:00 | 320.0 | 1 | 227 | 18.00 | 485.52 | more than 39 fake readings | 3.600 | 3.600 | 145.0 | |||||
213 | 2003-01-03T16:36 | 61.0 | 1 | 461 | 7.00 | 487.23 | stopped due to high idle current | more than 15 fake readings | replaced hose clamps by wire | 3.460 | 3.460 | 150.0 | |||
214 | 2003-01-03T18:22 | 172.0 | 1 | 317 | 9.00 | 488.82 | stopped due to antitorque rotation | more than 21 fake readings | 3.500 | 3.500 | 155.0 | 0.432 | 917.0 | -24.5 | |
215 | 2003-01-04T02:48 | 418 | 489.70 | flame straightened outer tube | electronics totally cleaned and copper chip removed from circuit board in 375 V section | 126.0 | |||||||||
215 | 2003-01-04T02:48 | 250.0 | 2 | 601 | 18.00 | 491.40 | 3.400 | 3.400 | |||||||
216 | 2003-01-04T08:51 | 149.0 | 1 | 428 | 8.50 | 492.98 | drill blocked at 9 A | 3.400 | 3.400 | 128.0 | |||||
217 | 2003-01-04T10:48 | 204.0 | 1 | 301 | 11.00 | 494.96 | 3.400 | 3.400 | 133.0 | ||||||
218 | 2003-01-04T14:21 | 239 | 496.10 | sharpened cutters, clearance to front of shoe 0.2 mm | 139.0 | ||||||||||
218 | 2003-01-04T14:21 | 108.0 | 2 | 228 | 8.00 | 496.21 | 2.900 | 3.050 | |||||||
219 | 2003-01-04T15:36 | 186.0 | 6 | 200 | 11.00 | 498.02 | loosened antitorque by 1 mm, stopped due to bad penetration | 2.800 | 2.900 | 142.0 | |||||
220 | 2003-01-04T17:22 | 162 | 498.62 | antitorque rotations, break and tra again | 146.0 | 0.350 | 917.0 | -26.0 | |||||||
220 | 2003-01-04T17:22 | 338.0 | 2 | 692 | 18.50 | 501.31 | 3.000 | 3.500 | 0.500 | 911.0 | -18.0 | ||||
221 | 2003-01-05T11:45 | 514 | 6.50 | 502.38 | antitorque rotation | 91.0 | |||||||||
221 | 2003-01-05T11:45 | 304.0 | 2 | 158 | 21.50 | 504.20 | 3.250 | 3.450 | |||||||
222 | 2003-01-05T13:55 | 279.0 | 1 | 317 | 17.00 | 507.16 | 3.200 | 3.400 | 95.0 | ||||||
223 | 2003-01-05T15:25 | 244.0 | 1 | 164 | 15.00 | 509.45 | antitorque rotations | 3.050 | 3.500 | 97.0 | |||||
224 | 2003-01-05T17:14 | 189.0 | 1 | 118 | 17.00 | 512.59 | pulled up rotating | 3.300 | 3.300 | 99.0 | |||||
225 | 2003-01-05T18:53 | 645 | 513.82 | antitorque rotation | 3.250 | 3.300 | 104.0 | ||||||||
225 | 2003-01-05T18:53 | 351.0 | 3 | 260 | 14.00 | 514.83 | 3.250 | 3.300 | |||||||
226 | 2003-01-05T20:25 | 484 | 515.70 | antitorque rotation | 109.0 | ||||||||||
226 | 2003-01-05T20:25 | 312.0 | 4 | 559 | 18.00 | 518.03 | 3.160 | 3.220 | |||||||
227 | 2003-01-05T21:40 | 216 | 518.05 | antitorque rotation | 113.0 | ||||||||||
227 | 2003-01-05T21:40 | 290.0 | 4 | 376 | 16.50 | 520.91 | 3.110 | 3.180 | |||||||
228 | 2003-01-05T22:55 | 210 | 522.16 | tuned antitorque harder to 31 mm above hammer, bad penetration | 119.0 | ||||||||||
228 | 2003-01-05T22:55 | 215.0 | 2 | 471 | 12.00 | 523.04 | 3.180 | 3.380 | |||||||
229 | 2003-01-06T08:21 | 471 | 524.46 | tuned antitorque 0.5 to 1 mm softer / 29.5 mm now, bad penetration | 121.0 | ||||||||||
229 | 2003-01-06T08:21 | 317.0 | 2 | 202 | 19.00 | 526.18 | 3.250 | 3.450 | |||||||
230 | 2003-01-06T10:04 | 194 | 527.32 | bad penetration | 126.0 | ||||||||||
230 | 2003-01-06T10:04 | 309.0 | 2 | 467 | 18.00 | 529.39 | 3.050 | 3.450 | |||||||
231 | 2003-01-06T11:46 | 595 | 530.71 | bad pentration | 132.0 | ||||||||||
231 | 2003-01-06T11:46 | 195.0 | 2 | 481 | 13.00 | 531.17 | bad pentration | 3.450 | 3.450 | ||||||
232 | 2003-01-06T13:25 | 288.0 | 2 | 471 | 17.00 | 534.11 | 3.240 | 3.410 | 136.0 | ||||||
233 | 2003-01-06T15:08 | 311.0 | 1 | 288 | 21.00 | 537.25 | tuned antitorque 0.5 mm harder | 2.810 | 3.030 | 140.0 | |||||
234 | 2003-01-06T16:43 | 284.0 | 2 | 523 | 18.00 | 540.07 | 2.900 | 2.900 | 145.0 | 0.442 | 916.0 | -24.5 | |||
235 | 2003-01-06T18:15 | 273.0 | 1 | 118 | 17.00 | 542.80 | 2.950 | 3.000 | 118.0 | ||||||
236 | 2003-01-06T19:43 | 215 | 544.93 | 125.0 | |||||||||||
236 | 2003-01-06T19:43 | 285.0 | 2 | 347 | 20.00 | 545.62 | 2.970 | 3.110 | |||||||
237 | 2003-01-06T21:00 | 475 | 547.23 | 132.0 | |||||||||||
237 | 2003-01-06T21:00 | 283.0 | 2 | 324 | 17.00 | 548.42 | 2.970 | 3.230 | |||||||
238 | 2003-01-06T22:09 | 249.0 | 6 | 459 | 13.50 | 550.99 | few electronics fake readings | 2.980 | 3.010 | 137.0 | |||||
239 | 2003-01-06T23:26 | 217.0 | 1 | 560 | 12.00 | 553.18 | few electronics fake readings | 2.910 | 3.110 | 138.0 | 0.437 | 917.0 | -25.5 | ||
240 | 2003-01-07T08:25 | 188.0 | 1 | 309 | 10.00 | 555.14 | more than 15 fake readings | 2.950 | 2.950 | ||||||
241 | 2003-01-07T10:05 | 233.0 | 1 | 650 | 16.00 | 557.47 | more than 15 fake readings | 3.600 | 3.600 | 112.0 | |||||
242 | 2003-01-07T11:58 | 299 | 558.51 | more than 9 fake readings | 117.0 | ||||||||||
242 | 2003-01-07T11:58 | 309.0 | 2 | 425 | 18.00 | 560.43 | 3.600 | 3.600 | |||||||
243 | 2003-01-07T14:10 | 233.0 | 3 | 668 | 16.00 | 562.72 | changed to Danish drill head with 0.21 mm clearance to front of shoe, new Rufli cutters | more than 8 fake readings | 3.800 | 3.800 | 121.0 | ||||
244 | 2003-01-07T15:55 | 275.0 | 1 | 317 | 15.00 | 565.55 | reduced pitch by one shim under shoes | more than 33 fake readings, disassembled electronics one inclinometer was wet from silicon oil | 2.250 | 2.500 | 127.0 | ||||
245 | 2003-01-08T01:30 | 265.0 | 1 | 260 | 18.50 | 568.20 | more than 4 fake readings | 2.600 | 2.600 | ||||||
246 | 2003-01-08T08:15 | 284.0 | 3 | 437 | 18.50 | 571.02 | more than 1 fake reading | 2.400 | 2.800 | 136.0 | |||||
247 | 2003-01-08T10:00 | 239.0 | 2 | 371 | 14.00 | 573.42 | changed drill head to Rufli head from last year | 3.200 | 3.300 | 141.0 | |||||
248 | 2003-01-08T11:35 | 213.0 | 1 | 339 | 14.00 | 575.54 | changed drill head to Danish head and removed one shim | 3.300 | 3.400 | 146.0 | 0.470 | 917.0 | -26.0 | ||
249 | 2003-01-08T13:10 | 216.0 | 1 | 501 | 12.50 | 577.66 | put in one shim | 2.780 | 3.000 | 115.0 | |||||
250 | 2003-01-08T14:20 | 283.0 | 1 | 326 | 18.50 | 580.53 | 2.790 | 2.960 | 123.0 | ||||||
251 | 2003-01-08T15:45 | 323 | 582.02 | persistent antitorque rotation | 125.0 | ||||||||||
251 | 2003-01-08T15:45 | 305.0 | 3 | 492 | 18.00 | 583.55 | 2.780 | 2.780 | |||||||
252 | 2003-01-08T17:00 | 230.0 | 1 | 389 | 13.50 | 585.87 | 3.100 | 3.100 | 128.0 | ||||||
253 | 2003-01-08T18:36 | 433 | 587.03 | 132.0 | |||||||||||
253 | 2003-01-08T18:36 | 326.0 | 5 | 582 | 19.00 | 589.00 | 2.820 | 2.980 | |||||||
254 | 2003-01-08T20:10 | 290.0 | 4 | 555 | 18.00 | 591.97 | 2.830 | 2.840 | 137.0 | ||||||
255 | 2003-01-08T21:31 | 374 | 593.43 | 141.0 | |||||||||||
255 | 2003-01-08T21:31 | 308.0 | 4 | 679 | 18.00 | 595.12 | 2.840 | 2.860 | |||||||
256 | 2003-01-08T22:55 | 361 | 596.39 | 147.0 | |||||||||||
256 | 2003-01-08T22:55 | 312.0 | 2 | 803 | 19.00 | 598.20 | 2.810 | 2.810 | 0.589 | 915.0 | -21.0 | ||||
FR25 | 2003-01-09T00:30 | 4.50 | 598.20 | 115.0 | |||||||||||
FR26 | 2003-01-09T01:05 | 598.20 | 118.0 | ||||||||||||
257 | 2003-01-09T08:23 | 459 | 599.09 | 117.0 | |||||||||||
257 | 2003-01-09T08:23 | 318.0 | 4 | 329 | 20.00 | 601.20 | 2.800 | 3.200 | |||||||
258 | 2003-01-09T10:23 | 591 | 602.94 | 121.0 | |||||||||||
258 | 2003-01-09T10:23 | 310.0 | 2 | 587 | 19.00 | 604.42 | 2.850 | 2.900 | |||||||
259 | 2003-01-09T12:02 | 264.0 | 1 | 503 | 17.50 | 607.05 | 2.800 | 2.900 | 127.0 | ||||||
260 | 2003-01-09T13:40 | 292.0 | 3 | 409 | 19.00 | 610.01 | 2.680 | 2.760 | 132.0 | ||||||
261 | 2003-01-09T15:06 | 386 | 611.75 | 136.0 | |||||||||||
261 | 2003-01-09T15:06 | 484 | 612.50 | ||||||||||||
261 | 2003-01-09T15:06 | 305.0 | 6 | 548 | 17.50 | 613.01 | 2.700 | 2.770 | |||||||
262 | 2003-01-09T16:40 | 415 | 614.20 | 141.0 | |||||||||||
262 | 2003-01-09T16:40 | 315.0 | 4 | 403 | 18.50 | 616.18 | 2.800 | 2.900 | |||||||
263 | 2003-01-09T18:27 | 463 | 617.17 | 150.0 | |||||||||||
263 | 2003-01-09T18:27 | 303.0 | 5 | 586 | 19.50 | 619.16 | 2.770 | 2.820 | 0.443 | 916.0 | -25.0 | ||||
264 | 2003-01-09T20:05 | 320 | 619.60 | ||||||||||||
264 | 2003-01-09T20:05 | 307.0 | 5 | 555 | 18.50 | 622.18 | 2.770 | 2.920 | |||||||
265 | 2003-01-09T21:35 | 176.0 | 1 | 659 | 11.00 | 624.07 | stopped due to persistent ant-torque rotation | 2.700 | 2.830 | ||||||
266 | 2003-01-09T23:15 | 559 | 625.10 | tight antitorque by 1 mm to 31.5 mm, switched to Rufli drill head from last year with 0.22 mm clearance to front of shoe | 130.0 | ||||||||||
266 | 2003-01-09T23:15 | 313.0 | 6 | 324 | 20.00 | 627.16 | 3.060 | 3.330 | |||||||
267 | 2003-01-10T08:22 | 246.0 | 1 | 533 | 17.00 | 629.60 | loosened antitorque by 0.5 mm, 31 mm now | 2.800 | 3.350 | 136.0 | |||||
268 | 2003-01-10T10:00 | 671 | 631.48 | 139.0 | |||||||||||
268 | 2003-01-10T10:00 | 291.0 | 4 | 186 | 19.00 | 632.59 | 3.100 | 3.200 | |||||||
269 | 2003-01-10T11:48 | 245.0 | 1 | 507 | 15.00 | 634.94 | 3.100 | 3.100 | 142.0 | 0.420 | 916.0 | -25.0 | |||
270 | 2003-01-10T13:17 | 275.0 | 2 | 389 | 17.50 | 637.72 | 3.030 | 3.300 | 119.0 | ||||||
271 | 2003-01-10T14:55 | 250.0 | 1 | 321 | 16.00 | 640.35 | 3.330 | 3.540 | |||||||
272 | 2003-01-10T16:30 | 285.0 | 2 | 311 | 16.50 | 643.08 | 3.400 | 3.400 | 128.0 | ||||||
273 | 2003-01-10T18:30 | 500 | 644.93 | antitorque blades sharpened | 130.0 | ||||||||||
273 | 2003-01-10T18:30 | 322.0 | 2 | 539 | 18.00 | 646.19 | 3.000 | 3.200 | |||||||
274 | 2003-01-10T20:12 | 405 | 648.69 | ||||||||||||
274 | 2003-01-10T20:12 | 338.0 | 4 | 379 | 18.00 | 649.72 | 3.280 | 3.350 | |||||||
275 | 2003-01-10T21:50 | 492 | 652.20 | changed to Rufli head from last year with freshly sharpened cutters 0.2 mm to 0.22 mm clearance to front edge | |||||||||||
275 | 2003-01-10T21:50 | 268.0 | 2 | 464 | 15.50 | 652.43 | 3.250 | 3.500 | |||||||
276 | 2003-01-11T00:00 | 361 | 653.17 | 146.0 | |||||||||||
276 | 2003-01-11T00:00 | 188.0 | 2 | 289 | 13.50 | 654.15 | 3.560 | 3.370 | 0.443 | 915.0 | -25.3 | ||||
277 | 2003-01-11T08:20 | 237 | 654.73 | 120.0 | |||||||||||
277 | 2003-01-11T08:20 | 238.0 | 2 | 331 | 17.50 | 656.60 | 3.400 | 3.400 | |||||||
278 | 2003-01-11T10:21 | 607 | 656.64 | reduced clearance by 1 shim | 125.0 | ||||||||||
278 | 2003-01-11T10:21 | 279.0 | 2 | 253 | 18.00 | 659.40 | 2.860 | 2.860 | |||||||
279 | 2003-01-11T12:00 | 372 | 660.06 | 129.0 | |||||||||||
279 | 2003-01-11T12:00 | 459 | 661.74 | 2.700 | 2.800 | ||||||||||
279 | 2003-01-11T12:00 | 300.0 | 5 | 485 | 18.00 | 662.43 | |||||||||
280 | 2003-01-11T13:55 | 518 | 664.22 | 134.0 | |||||||||||
280 | 2003-01-11T13:55 | 287.0 | 2 | 457 | 21.00 | 665.26 | 2.800 | 2.830 | |||||||
281 | 2003-01-11T15:36 | 413 | 665.61 | 139.0 | |||||||||||
281 | 2003-01-11T15:36 | 214.0 | 3 | 694 | 13.00 | 667.38 | 2.650 | 2.680 | |||||||
282 | 2003-01-11T17:22 | 299.0 | 2 | 375 | 19.00 | 670.42 | 3.660 | 3.780 | 145.0 | ||||||
283 | 2003-01-12T11:55 | 294.0 | 1 | 625 | 18.50 | 673.28 | put on new electronics with TERN controller, 300 V modules, 50 V motor, 80:1 gear | 3.450 | 3.450 | 155.0 | 0.522 | 918.0 | -26.5 | ||
284 | 2003-01-12T13:55 | 240 | 675.46 | 116.0 | |||||||||||
284 | 2003-01-12T13:55 | 312.0 | 4 | 355 | 19.85 | 676.40 | put on old electronics, 375 V modules, 60 V motor, 80:1 gear to speed up communications and implement further heating for inclinometers | 3.550 | 3.760 | ||||||
285 | 2003-01-12T15:55 | 441 | 678.34 | 129.0 | |||||||||||
285 | 2003-01-12T15:55 | 306.0 | 6 | 180 | 18.00 | 679.40 | 3.570 | 3.780 | |||||||
286 | 2003-01-12T17:30 | 309.0 | 1 | 374 | 18.50 | 682.55 | 3.860 | 4.080 | 131.0 | ||||||
287 | 2003-01-12T19:10 | 412 | 685.01 | 132.0 | |||||||||||
287 | 2003-01-12T19:10 | 318.0 | 3 | 534 | 19.00 | 685.74 | 3.750 | 3.750 | |||||||
288 | 2003-01-12T21:02 | 437 | 687.62 | 135.0 | |||||||||||
288 | 2003-01-12T21:02 | 322.0 | 3 | 494 | 20.00 | 688.93 | 3.700 | 3.800 | |||||||
289 | 2003-01-12T22:51 | 451 | 690.87 | 139.0 | |||||||||||
289 | 2003-01-12T22:51 | 336.0 | 2 | 518 | 692.25 | 3.900 | 3.900 | 0.565 | 917.0 | -26.1 | |||||
290 | 2003-01-13T08:20 | 599 | 694.71 | 108.0 | |||||||||||
290 | 2003-01-13T08:20 | 300.0 | 3 | 473 | 19.00 | 695.35 | 3.770 | 3.820 | |||||||
291 | 2003-01-13T10:12 | 479 | 696.46 | 113.0 | |||||||||||
291 | 2003-01-13T10:12 | 306.0 | 3 | 247 | 18.70 | 698.33 | 3.750 | 3.840 | |||||||
292 | 2003-01-13T11:48 | 295.0 | 3 | 507 | 18.00 | 701.36 | 3.710 | 3.880 | 117.0 | ||||||
293 | 2003-01-13T13:37 | 577 | 703.34 | 123.0 | |||||||||||
293 | 2003-01-13T13:37 | 299.0 | 3 | 362 | 18.00 | 704.35 | 3.500 | 3.700 | |||||||
294 | 2003-01-13T15:16 | 379 | 705.38 | 128.0 | |||||||||||
294 | 2003-01-13T15:16 | 321.0 | 3 | 501 | 17.50 | 707.53 | 3.700 | 3.700 | |||||||
295 | 2003-01-13T16:58 | 279.0 | 3 | 482 | 18.00 | 710.25 | 3.420 | 3.800 | 133.0 | ||||||
296 | 2003-01-13T18:45 | 299.0 | 1 | 554 | 18.00 | 713.33 | 3.800 | 3.800 | 138.0 | ||||||
297 | 2003-01-13T20:32 | 273.0 | 2 | 390 | 17.00 | 716.12 | 3.700 | 3.700 | 142.0 | 0.522 | 917.0 | -26.2 | |||
298 | 2003-01-13T22:06 | 605 | 717.19 | 111.0 | |||||||||||
298 | 2003-01-13T22:06 | 314.0 | 3 | 446 | 20.20 | 719.30 | 3.500 | 3.800 | |||||||
299 | 2003-01-14T08:17 | 275.0 | 4 | 632 | 17.00 | 722.04 | 3.500 | 3.760 | 116.0 | ||||||
300 | 2003-01-14T10:12 | 522 | 724.46 | 121.0 | |||||||||||
300 | 2003-01-14T10:12 | 336.0 | 2 | 449 | 18.50 | 725.38 | 3.400 | 3.570 | |||||||
301 | 2003-01-14T12:24 | 489 | 727.47 | 126.0 | |||||||||||
301 | 2003-01-14T12:24 | 337.0 | 4 | 578 | 18.00 | 728.54 | 3.600 | 3.600 | |||||||
302 | 2003-01-14T14:28 | 676 | 730.74 | 130.0 | |||||||||||
302 | 2003-01-14T14:28 | 231.0 | 2 | 386 | 19.00 | 731.75 | 3.800 | 3.800 | |||||||
303 | 2003-01-14T16:28 | 279.0 | 1 | 515 | 13.00 | 733.82 | 3.660 | 3.960 | 136.0 | ||||||
304 | 2003-01-14T18:15 | 692 | 735.50 | more than 9 fake readings | 142.0 | ||||||||||
304 | 2003-01-14T18:15 | 330.0 | 1 | 447 | 18.00 | 737.04 | 3.550 | 3.550 | |||||||
305 | 2003-01-14T20:29 | 485 | 739.55 | 144.0 | |||||||||||
305 | 2003-01-14T20:29 | 294.0 | 2 | 594 | 18.00 | 740.03 | 3.300 | 3.500 | 0.562 | 918.0 | -26.0 | ||||
306 | 2003-01-14T22:22 | 489 | 742.60 | 109.0 | |||||||||||
306 | 2003-01-14T22:22 | 338.0 | 2 | 221 | 19.00 | 743.33 | 3.400 | 3.400 | |||||||
307 | 2003-01-15T09:10 | 251.0 | 1 | 652 | 17.40 | 745.81 | put on new electronics with TERN controller, 300 V modules, 50 V motor, 80:1 gear | 2.070 | 2.160 | ||||||
308 | 2003-01-15T10:41 | 253.0 | 3 | 534 | 14.80 | 748.41 | 3.020 | 3.340 | 119.0 | ||||||
309 | 2003-01-15T11:59 | 303.0 | 1 | 515 | 18.50 | 751.51 | put on old electronics, 375 V modules, 60 V motor, 80:1 gear to speed up communications and implement further heating for inclinometers | 3.000 | 3.040 | 124.0 | |||||
310 | 2003-01-15T13:24 | 306.0 | 3 | 505 | 17.50 | 754.48 | 3.150 | 3.150 | 128.0 | ||||||
311 | 2003-01-15T15:14 | 754.48 | could not start motor, changed to 375 V modules, old computer and 80:1 gear | 131.0 | |||||||||||
312 | 2003-01-15T16:32 | 576 | 756.03 | 133.0 | |||||||||||
312 | 2003-01-15T16:32 | 317.0 | 3 | 637 | 18.00 | 757.49 | 3.220 | 3.440 | |||||||
313 | 2003-01-15T18:30 | 790 | 759.95 | 137.0 | |||||||||||
313 | 2003-01-15T18:30 | 280.0 | 2 | 568 | 18.00 | 760.50 | 3.300 | 3.300 | |||||||
314 | 2003-01-15T20:12 | 270.0 | 3 | 659 | 16.50 | 763.09 | 3.000 | 3.200 | 144.0 | ||||||
315 | 2003-01-15T21:53 | 257.0 | 1 | 542 | 16.00 | 765.78 | 3.300 | 3.500 | 149.0 | 0.645 | 916.5 | -24.7 | |||
316 | 2003-01-15T23:34 | 288.0 | 1 | 615 | 19.50 | 768.65 | changed to new computer, 300 V modules have been modified to 375 V, changed operational amplifier, rectifier diode checked | 3.300 | 3.400 | 110.0 | |||||
317 | 2003-01-16T08:15 | 253.0 | 2 | 541 | 16.00 | 771.17 | changed to Rufli head from 2001 season, 0.19 mm - 0.2 mm clearance to front edge of shoe | 3.340 | 3.390 | 115.0 | |||||
318 | 2003-01-16T09:44 | 443 | 772.87 | 120.0 | |||||||||||
318 | 2003-01-16T09:44 | 281.0 | 4 | 663 | 17.00 | 773.98 | 3.280 | 3.380 | |||||||
319 | 2003-01-16T11:28 | 406 | 774.98 | 126.0 | |||||||||||
319 | 2003-01-16T11:28 | 320.0 | 2 | 640 | 20.50 | 777.13 | 3.120 | 3.180 | |||||||
320 | 2003-01-16T12:59 | 366 | 779.43 | tower motor gone, operating with chain hoist | 131.0 | ||||||||||
320 | 2003-01-16T12:59 | 297.0 | 5 | 347 | 19.00 | 780.19 | 2.900 | 3.100 | |||||||
321 | 2003-01-16T16:10 | 787 | 781.84 | first core not broken, release tension again | |||||||||||
321 | 2003-01-16T16:10 | 175.0 | 1 | 610 | 11.50 | 781.84 | 2.600 | 3.140 | 134.0 | ||||||
322 | 2003-01-16T18:05 | 307.0 | 5 | 351 | 18.00 | 784.96 | 2.900 | 3.200 | 140.0 | ||||||
323 | 2003-01-16T19:56 | 594 | 785.90 | ||||||||||||
323 | 2003-01-16T19:56 | 286.0 | 2 | 356 | 7.50 | 787.71 | 2.700 | 2.850 | |||||||
324 | 2003-01-16T22:09 | 295.0 | 4 | 647 | 18.10 | 790.85 | changed to Danish drill head with sharpened cutters, sharpened skates | 3.100 | 3.100 | 150.0 | 0.530 | 918.0 | -26.2 | ||
FR27 | 2003-01-17T00:55 | 1.60 | 790.85 | 121.0 | |||||||||||
325 | 2003-01-17T08:22 | 756 | 793.02 | 119.0 | |||||||||||
325 | 2003-01-17T08:22 | 331.0 | 5 | 379 | 18.00 | 793.86 | 3.060 | 3.300 | |||||||
326 | 2003-01-17T09:59 | 306.0 | 1 | 515 | 18.00 | 797.22 | 2.740 | 2.880 | 125.0 | ||||||
327 | 2003-01-17T11:40 | 493 | 798.29 | 132.0 | |||||||||||
327 | 2003-01-17T11:40 | 345.0 | 3 | 364 | 19.00 | 800.59 | 2.960 | 3.120 | |||||||
328 | 2003-01-17T13:28 | 299.0 | 1 | 774 | 19.50 | 803.63 | 2.800 | 2.800 | 135.0 | ||||||
329 | 2003-01-17T15:08 | 305.0 | 2 | 584 | 19.00 | 806.66 | 3.100 | 3.100 | 139.0 | ||||||
330 | 2003-01-17T16:39 | 270.0 | 4 | 726 | 17.50 | 809.34 | 2.920 | 3.140 | 144.0 | ||||||
331 | 2003-01-17T18:09 | 311.0 | 4 | 398 | 18.00 | 812.47 | 2.560 | 2.980 | 149.0 | ||||||
332 | 2003-01-17T19:35 | 316.0 | 3 | 782 | 19.00 | 815.64 | 2.800 | 3.100 | 154.0 | 0.502 | 917.0 | -25.8 | |||
333 | 2003-01-17T21:04 | 311.0 | 1 | 387 | 19.00 | 818.74 | 2.900 | 3.100 | 123.0 | ||||||
334 | 2003-01-17T22:34 | 303.0 | 3 | 573 | 19.80 | 821.86 | 3.300 | 3.300 | 127.0 | ||||||
335 | 2003-01-18T08:20 | 305.0 | 3 | 493 | 18.00 | 824.84 | 2.630 | 2.880 | 132.0 | ||||||
336 | 2003-01-18T09:43 | 297.0 | 2 | 409 | 17.60 | 827.82 | 2.830 | 2.980 | 137.0 | ||||||
337 | 2003-01-18T11:01 | 308.0 | 1 | 465 | 18.00 | 830.88 | 2.570 | 3.020 | 142.0 | ||||||
338 | 2003-01-18T12:20 | 311.0 | 2 | 568 | 18.00 | 834.00 | 3.000 | 3.000 | 148.0 | 0.500 | 918.0 | -24.7 | |||
339 | 2003-01-18T13:49 | 287.0 | 1 | 350 | 17.00 | 836.84 | 2.900 | 3.100 | 117.0 | ||||||
340 | 2003-01-18T15:19 | 312.0 | 3 | 573 | 19.00 | 839.95 | 2.800 | 2.800 | 122.0 | ||||||
341 | 2003-01-18T16:49 | 299.0 | 2 | 536 | 17.00 | 842.97 | 2.700 | 2.800 | 127.0 | 0.300 | 912.0 | -20.0 | |||
342 | 2003-01-19T11:14 | 309.0 | 2 | 573 | 19.00 | 845.99 | broken spring in pump changed | 3.200 | 3.500 | 111.0 | |||||
343 | 2003-01-19T12:54 | 311.0 | 1 | 420 | 18.20 | 849.12 | 2.570 | 2.880 | 116.0 | ||||||
344 | 2003-01-19T14:14 | 302.0 | 2 | 710 | 20.00 | 852.21 | 2.500 | 2.800 | 121.0 | ||||||
345 | 2003-01-19T15:47 | 308.0 | 1 | 493 | 19.00 | 855.20 | 2.800 | 3.200 | 126.0 | ||||||
346 | 2003-01-19T17:27 | 311.0 | 1 | 355 | 18.50 | 858.36 | 130.0 | ||||||||
347 | 2003-01-19T19:03 | 297.0 | 2 | 549 | 18.70 | 861.43 | 2.880 | 3.060 | 136.0 | ||||||
348 | 2003-01-19T20:33 | 317.0 | 1 | 648 | 19.00 | 864.56 | 2.880 | 2.960 | 141.0 | 0.476 | 917.0 | -25.4 | |||
349 | 2003-01-19T22:01 | 310.0 | 2 | 640 | 18.50 | 867.57 | 2.670 | 2.820 | 118.0 | ||||||
350 | 2003-01-19T23:25 | 317.0 | 1 | 570 | 18.00 | 870.78 | 2.810 | 3.100 | 122.0 | ||||||
351 | 2003-01-20T01:21 | 266.0 | 1 | 568 | 16.00 | 873.37 | 3.860 | 3.860 | 126.5 | ||||||
352 | 2003-01-20T03:04 | 474 | 875.12 | 132.0 | |||||||||||
352 | 2003-01-20T03:04 | 283.0 | 2 | 398 | 17.50 | 876.31 | 3.200 | 3.200 | |||||||
353 | 2003-01-20T04:46 | 559 | 877.71 | 136.0 | |||||||||||
353 | 2003-01-20T04:46 | 311.0 | 2 | 719 | 17.50 | 879.43 | 3.400 | 3.400 | |||||||
354 | 2003-01-20T06:30 | 295.0 | 100 | 488 | 18.00 | 882.46 | 140.0 | ||||||||
355 | 2003-01-20T08:20 | 312.0 | 1 | 325 | 19.00 | 885.60 | 3.000 | 3.200 | 140.0 | 0.565 | 918.0 | -27.0 | |||
356 | 2003-01-20T10:14 | 310.0 | 1 | 515 | 18.00 | 888.56 | 3.100 | 3.100 | 112.0 | ||||||
357 | 2003-01-20T11:45 | 309.0 | 3 | 528 | 18.50 | 891.73 | 2.900 | 3.200 | 117.0 | ||||||
358 | 2003-01-20T13:16 | 316.0 | 2 | 677 | 19.50 | 894.81 | 2.560 | 2.890 | 121.0 | ||||||
359 | 2003-01-20T14:50 | 294.0 | 3 | 602 | 18.20 | 897.82 | 2.480 | 2.750 | 127.0 | ||||||
360 | 2003-01-20T16:14 | 320.0 | 2 | 438 | 18.00 | 900.85 | 3.200 | 3.200 | 132.0 | ||||||
361 | 2003-01-20T17:42 | 296.0 | 1 | 525 | 18.00 | 904.00 | 2.850 | 2.850 | 137.0 | ||||||
362 | 2003-01-20T19:12 | 303.0 | 1 | 369 | 18.50 | 907.00 | 2.700 | 2.980 | 142.0 | ||||||
363 | 2003-01-20T20:43 | 311.0 | 2 | 360 | 18.50 | 910.08 | 2.840 | 2.960 | 147.0 | 0.538 | 917.0 | -25.5 | |||
364 | 2003-01-20T22:04 | 300.0 | 2 | 517 | 18.00 | 913.07 | 2.600 | 3.080 | 115.0 | ||||||
365 | 2003-01-20T23:29 | 298.0 | 3 | 559 | 18.00 | 916.13 | 2.540 | 2.740 | 120.0 | ||||||
366 | 2003-01-21T00:55 | 313.0 | 1 | 412 | 18.50 | 919.20 | 123.0 | ||||||||
367 | 2003-01-21T02:35 | 296.0 | 1 | 492 | 18.00 | 922.21 | 125.0 | ||||||||
368 | 2003-01-21T04:10 | 297.0 | 100 | 370 | 18.00 | 925.19 | 132.0 | ||||||||
369 | 2003-01-21T06:03 | 800 | 926.44 | 138.0 | |||||||||||
369 | 2003-01-21T06:03 | 328.0 | 2 | 652 | 18.00 | 928.22 | |||||||||
370 | 2003-01-21T08:18 | 309.0 | 1 | 469 | 19.00 | 931.54 | 3.100 | 3.300 | 143.0 | ||||||
371 | 2003-01-21T09:54 | 289.0 | 1 | 563 | 17.00 | 934.38 | 3.300 | 3.300 | 149.0 | 0.521 | 920.0 | -28.5 | |||
372 | 2003-01-21T11:22 | 306.0 | 1 | 669 | 20.00 | 937.53 | 2.800 | 3.100 | 119.0 | ||||||
373 | 2003-01-21T12:55 | 316.0 | 2 | 506 | 19.00 | 940.45 | 2.600 | 3.000 | 121.0 | ||||||
374 | 2003-01-21T14:28 | 305.0 | 1 | 695 | 21.50 | 943.54 | 2.680 | 2.800 | 127.0 | ||||||
375 | 2003-01-21T15:59 | 280.0 | 3 | 712 | 18.00 | 946.45 | changed to Rufli head from last year | 2.800 | 3.100 | 133.0 | |||||
376 | 2003-01-21T17:55 | 435 | 948.53 | 139.0 | |||||||||||
376 | 2003-01-21T17:55 | 310.0 | 2 | 440 | 18.70 | 949.39 | 3.000 | 3.100 | |||||||
377 | 2003-01-21T20:07 | 243 | 951.63 | 145.0 | |||||||||||
377 | 2003-01-21T20:07 | 289.0 | 2 | 379 | 17.50 | 952.14 | 3.080 | 3.660 | 0.571 | 915.0 | -23.5 | ||||
378 | 2003-01-21T22:13 | 286.0 | 2 | 451 | 17.00 | 955.13 | changed to freshly sharpened Danish head | 2.720 | 3.160 | 112.0 | |||||
379 | 2003-01-21T23:38 | 296.0 | 3 | 753 | 18.00 | 958.19 | 2.800 | 3.470 | 117.0 | ||||||
380 | 2003-01-22T01:10 | 279.0 | 1 | 399 | 16.50 | 960.77 | 121.0 | ||||||||
381 | 2003-01-22T02:44 | 469 | 963.02 | 127.0 | |||||||||||
381 | 2003-01-22T02:44 | 311.0 | 3 | 446 | 18.50 | 963.99 | |||||||||
382 | 2003-01-22T04:18 | 469 | 966.28 | 130.0 | |||||||||||
382 | 2003-01-22T04:18 | 333.0 | 3 | 415 | 18.50 | 967.24 | |||||||||
383 | 2003-01-22T06:00 | 243.0 | 1 | 611 | 10.00 | 969.81 | 135.0 | ||||||||
384 | 2003-01-22T07:55 | 203.0 | 1 | 391 | 19.50 | 971.85 | 2.500 | 2.500 | 139.0 | ||||||
385 | 2003-01-22T09:24 | 302.0 | 1 | 540 | 18.50 | 974.77 | 2.600 | 2.800 | 144.0 | 0.500 | 920.0 | -28.0 | |||
386 | 2003-01-22T10:51 | 305.0 | 1 | 384 | 19.00 | 977.85 | 2.500 | 2.600 | 126.0 | ||||||
387 | 2003-01-22T12:16 | 315.0 | 2 | 386 | 19.00 | 981.00 | 3.000 | 3.100 | 119.0 | ||||||
388 | 2003-01-22T13:47 | 278.0 | 2 | 619 | 19.00 | 983.76 | 2.780 | 2.800 | 123.0 | ||||||
389 | 2003-01-22T15:06 | 299.0 | 100 | 485 | 18.00 | 986.67 | 3.050 | 3.050 | 127.0 | ||||||
390 | 2003-01-22T16:47 | 314.0 | 1 | 732 | 18.50 | 989.89 | 2.700 | 2.800 | 132.0 | ||||||
391 | 2003-01-22T18:27 | 503 | 992.40 | 136.0 | |||||||||||
391 | 2003-01-22T18:27 | 328.0 | 2 | 426 | 18.50 | 992.98 | 2.760 | 2.940 | |||||||
392 | 2003-01-22T20:07 | 285.0 | 1 | 541 | 18.00 | 996.02 | 2.370 | 2.860 | 141.0 | 0.477 | 918.0 | -27.1 | |||
393 | 2003-01-22T21:29 | 308.0 | 1 | 395 | 18.00 | 998.89 | 2.260 | 2.760 | 113.0 | ||||||
394 | 2003-01-22T22:50 | 298.0 | 1 | 406 | 17.00 | 1001.95 | 2.540 | 2.740 | 118.0 | ||||||
FR28 | 2003-01-23T01:20 | 4.00 | 1001.95 | ||||||||||||
395 | 2003-01-23T02:48 | 471 | 1003.42 | 124.0 | |||||||||||
395 | 2003-01-23T02:48 | 319.0 | 2 | 368 | 18.00 | 1005.07 | |||||||||
396 | 2003-01-23T04:45 | 487 | 1006.87 | 128.0 | |||||||||||
396 | 2003-01-23T04:45 | 330.0 | 2 | 467 | 18.50 | 1008.39 | |||||||||
397 | 2003-01-23T06:21 | 318.0 | 1 | 570 | 18.50 | 1011.73 | 132.0 | ||||||||
398 | 2003-01-23T07:57 | 310.0 | 1 | 408 | 18.50 | 1014.91 | 2.600 | 3.000 | 138.0 | ||||||
399 | 2003-01-23T09:27 | 311.0 | 1 | 552 | 19.00 | 1017.88 | 2.500 | 2.800 | 144.0 | 0.549 | 917.0 | -25.5 | |||
400 | 2003-01-23T11:12 | 307.0 | 1 | 269 | 19.00 | 1020.96 | replaced worn out seal, new springs in pump | 2.500 | 2.600 | 110.0 | |||||
401 | 2003-01-23T12:45 | 279.0 | 2 | 700 | 17.00 | 1023.72 | 2.820 | 2.880 | 114.0 | ||||||
402 | 2003-01-23T14:16 | 303.0 | 1 | 422 | 20.00 | 1026.80 | 2.300 | 2.570 | 120.0 | ||||||
403 | 2003-01-23T15:46 | 284.0 | 1 | 453 | 16.00 | 1029.37 | 2.680 | 2.710 | 125.0 | ||||||
404 | 2003-01-23T17:28 | 306.0 | 1 | 412 | 18.50 | 1032.69 | 2.600 | 2.600 | 130.0 | ||||||
405 | 2003-01-23T19:14 | 285.0 | 1 | 742 | 18.00 | 1035.55 | 2.410 | 2.920 | 135.0 | ||||||
406 | 2003-01-23T20:47 | 289.0 | 1 | 433 | 19.00 | 1038.20 | changed to freshly tuned Rufli head | 3.000 | 3.900 | 141.0 | 0.655 | 914.0 | -22.5 | ||
407 | 2003-01-23T22:46 | 306.0 | 1 | 411 | 17.50 | 1041.22 | 2.740 | 2.880 | 100.0 | ||||||
408 | 2003-01-24T00:10 | 275.0 | 1 | 398 | 17.50 | 1044.21 | 108.0 | ||||||||
409 | 2003-01-24T01:46 | 618 | 1046.11 | 114.0 | |||||||||||
409 | 2003-01-24T01:46 | 311.0 | 2 | 494 | 18.00 | 1047.25 | |||||||||
410 | 2003-01-24T03:29 | 575 | 1049.02 | 118.0 | |||||||||||
410 | 2003-01-24T03:29 | 293.0 | 3 | 366 | 18.00 | 1050.30 | |||||||||
411 | 2003-01-24T05:32 | 285.0 | 1 | 524 | 17.50 | 1053.26 | winch inverter failure, dripped 2 m of cable suddenly down. Fixed after power off and power on | 124.0 | |||||||
412 | 2003-01-24T07:08 | 299.0 | 1 | 855 | 18.50 | 1056.24 | 2.600 | 2.600 | 128.0 | ||||||
413 | 2003-01-24T08:55 | 547 | 1057.67 | 132.0 | |||||||||||
413 | 2003-01-24T08:55 | 325.0 | 2 | 708 | 18.00 | 1059.34 | 2.900 | 3.100 | |||||||
414 | 2003-01-24T10:32 | 626 | 1060.95 | 139.0 | |||||||||||
414 | 2003-01-24T10:32 | 296.0 | 2 | 483 | 18.50 | 1062.26 | 2.900 | 2.900 | |||||||
415 | 2003-01-24T12:28 | 232.0 | 1 | 408 | 16.00 | 1064.54 | readjusted clearance of linings, because winch brake did not open anymore | 2.610 | 2.660 | 107.0 | 0.517 | 919.0 | -27.0 | ||
416 | 2003-01-24T15:40 | 318.0 | 1 | 576 | 18.00 | 1067.98 | 2.500 | 2.600 | 112.0 | ||||||
417 | 2003-01-24T17:27 | 312.0 | 1 | 554 | 18.00 | 1071.08 | 2.500 | 3.000 | 116.0 | ||||||
418 | 2003-01-24T19:06 | 312.0 | 1 | 658 | 18.50 | 1074.02 | 2.440 | 2.530 | |||||||
419 | 2003-01-24T20:46 | 313.0 | 1 | 684 | 28.00 | 1077.18 | replaced missing screw on upper valve | 2.460 | 2.720 | 125.0 | |||||
420 | 2003-01-24T22:22 | 306.0 | 1 | 481 | 18.50 | 1080.25 | 2.780 | 2.900 | 130.0 | ||||||
421 | 2003-01-25T00:05 | 321.0 | 1 | 612 | 19.00 | 1083.51 | 135.0 | ||||||||
422 | 2003-01-25T02:14 | 697 | 1085.73 | put on Danish drill head with freshly sharpened cutters, clearance 0.19 mm - 0.2 mm to front edge of shoe | 131.0 | ||||||||||
422 | 2003-01-25T02:14 | 301.0 | 2 | 422 | 18.00 | 1086.46 | 3.400 | 3.400 | |||||||
423 | 2003-01-25T03:58 | 783 | 1088.24 | 136.0 | |||||||||||
423 | 2003-01-25T03:58 | 207.0 | 2 | 698 | 14.00 | 1088.57 | |||||||||
424 | 2003-01-25T06:12 | 287.0 | 1 | 497 | 18.00 | 1091.61 | changed to other core barrel with Danish drill head, clearance 0.2 mm - 0.21 mm | 144.0 | 0.491 | 919.0 | -27.8 | ||||
425 | 2003-01-25T08:17 | 339.0 | 1 | 399 | 18.00 | 1094.84 | 2.400 | 2.500 | 122.0 | ||||||
426 | 2003-01-25T09:54 | 319.0 | 1 | 686 | 18.50 | 1097.97 | 2.500 | 2.500 | 128.0 | ||||||
427 | 2003-01-25T11:22 | 317.0 | 1 | 697 | 18.50 | 1101.13 | 2.600 | 2.600 | 133.0 | ||||||
428 | 2003-01-25T12:52 | 307.0 | 1 | 708 | 18.50 | 1104.06 | 2.180 | 2.290 | 137.0 | ||||||
429 | 2003-01-25T14:22 | 315.0 | 2 | 21.50 | 1107.34 | 2.320 | 2.400 | 142.0 | 0.600 | 920.0 | -28.5 | ||||
430 | 2003-01-25T15:50 | 316.0 | 1 | 377 | 18.50 | 1110.39 | 2.460 | 3.060 | 107.0 | ||||||
431 | 2003-01-25T17:17 | 314.0 | 1 | 456 | 18.00 | 1113.52 | changed to old computer with 50 V motor | 2.290 | 2.640 | 112.0 | |||||
432 | 2003-01-26T10:57 | 277.0 | 1 | 664 | 19.00 | 1116.52 | total power shortage for whole trench | 3.200 | 3.200 | 117.0 | |||||
433 | 2003-01-26T13:29 | 275.0 | 1 | 665 | 18.00 | 1119.15 | 2.940 | 3.130 | 122.0 | ||||||
434 | 2003-01-26T16:30 | 297.0 | 1 | 671 | 18.00 | 1122.09 | switched power supply for modem from net to UPS (uninterruptable power supply) | 2.860 | 3.020 | 127.0 | |||||
435 | 2003-01-26T18:50 | 291.0 | 1 | 464 | 18.00 | 1125.04 | switched power supply for modem back, because of faulty readings from the depth meter | 3.000 | 3.000 | 133.0 | |||||
436 | 2003-01-26T20:36 | 307.0 | 1 | 507 | 17.50 | 1128.41 | 2.700 | 2.700 | 137.0 | ||||||
437 | 2003-01-26T22:11 | 440 | 1130.22 | 142.0 | |||||||||||
437 | 2003-01-26T22:11 | 324.0 | 2 | 451 | 18.00 | 1131.23 | 2.500 | 2.500 | 0.547 | 917.0 | -25.5 | ||||
438 | 2003-01-27T00:00 | 260.0 | 1 | 397 | 17.00 | 1134.03 | 120.0 | ||||||||
439 | 2003-01-27T01:50 | 306.0 | 1 | 486 | 18.00 | 1136.96 | 112.0 | ||||||||
440 | 2003-01-27T03:30 | 275.0 | 1 | 703 | 17.00 | 1139.81 | 2.800 | 2.800 | 116.0 | ||||||
441 | 2003-01-27T05:10 | 513 | 1141.22 | 125.0 | |||||||||||
441 | 2003-01-27T05:10 | 304.0 | 2 | 737 | 17.50 | 1142.61 | |||||||||
442 | 2003-01-27T07:12 | 490 | 1143.80 | 130.0 | |||||||||||
442 | 2003-01-27T07:12 | 279.0 | 2 | 549 | 17.00 | 1145.37 | 2.550 | 2.780 | |||||||
443 | 2003-01-27T09:04 | 190.0 | 2 | 508 | 15.00 | 1147.43 | changed to the other core barrel with freshly sharpened head | 2.960 | 2.960 | 134.0 | |||||
444 | 2003-01-27T10:59 | 247.0 | 1 | 476 | 14.00 | 1150.13 | one screw of spiral lost | 3.460 | 3.540 | 137.0 | |||||
445 | 2003-01-27T12:51 | 269.0 | 1 | 700 | 15.50 | 1152.68 | 2.500 | 2.500 | 140.0 | 0.525 | 919.0 | -27.6 | |||
446 | 2003-01-27T14:34 | 448 | 1153.40 | bronze on damaged knife, changed to other Danish head | changed to new electronics, because of slightly higher current limit settings | 109.0 | |||||||||
446 | 2003-01-27T14:34 | 324.0 | 2 | 735 | 18.00 | 1155.78 | 2.700 | 3.100 | |||||||
447 | 2003-01-27T17:24 | 46.0 | 1 | 375 | 5.20 | 1156.33 | cutting current going straight up to the limit | 114.0 | |||||||
448 | 2003-01-27T18:58 | 40.0 | 1 | 406 | 3.00 | 1156.62 | marks of spiral on inner barrel | 115.0 | |||||||
449 | 2003-01-27T20:23 | 269.0 | 1 | 570 | 16.00 | 1159.52 | 117.0 | ||||||||
450 | 2003-01-27T23:02 | 129.0 | 1 | 463 | 8.00 | 1161.14 | changed to HT drill with plastic spirals, picked up one screw head sitting in the spirals | 118.0 | |||||||
451 | 2003-01-28T01:00 | 123.0 | 1 | 733 | 10.00 | 1162.44 | 2.600 | 2.600 | 121.0 | ||||||
452 | 2003-01-28T02:40 | 506 | 1163.03 | changed back to long drill | 126.0 | ||||||||||
452 | 2003-01-28T02:40 | 112.0 | 2 | 544 | 8.50 | 1163.16 | no rotation at 12 A | ||||||||
453 | 2003-01-28T04:35 | 849 | 1164.48 | switched to Danish head with ARN 42.5° cutters, clearance 0.19 mm - 0.2 mm to front edge of shoe | 129.0 | ||||||||||
453 | 2003-01-28T04:35 | 312.0 | 2 | 450 | 18.00 | 1166.16 | 3.500 | 3.500 | |||||||
454 | 2003-01-28T06:30 | 459 | 1168.39 | 134.0 | |||||||||||
454 | 2003-01-28T06:30 | 274.0 | 2 | 612 | 15.00 | 1168.98 | switched to Rufli head from last year | ||||||||
455 | 2003-01-28T08:29 | 283.0 | 1 | 611 | 16.50 | 1171.91 | 3.040 | 3.100 | 138.0 | ||||||
456 | 2003-01-28T10:08 | 438 | 1173.97 | 141.0 | |||||||||||
456 | 2003-01-28T10:08 | 333.0 | 2 | 829 | 19.00 | 1174.99 | 2.900 | 3.070 | 0.538 | 922.0 | -30.6 | ||||
457 | 2003-01-28T13:44 | 117.0 | 1 | 506 | 8.00 | 1176.33 | changed to Danish head, clearance 0.22 mm to front edge of shoe, no rotation possible | 106.0 | |||||||
458 | 2003-01-28T15:37 | 260.0 | 1 | 446 | 15.00 | 1179.00 | changed to Rufli head from last year | 2.960 | 3.160 | 110.0 | |||||
459 | 2003-01-28T17:35 | 87.0 | 2 | 898 | 2.00 | 1179.79 | pump badly blocked with chips | 115.0 | |||||||
460 | 2003-01-28T19:00 | 898 | 1180.28 | no core break, pull down, rotate | 117.0 | ||||||||||
460 | 2003-01-28T19:00 | 56.0 | 1 | 504 | 3.50 | 1180.28 | 3.400 | 3.600 | |||||||
461 | 2003-01-28T20:43 | 904 | 1181.30 | changed springs in both core catchers, put in one shim respectively, no core break, went down to 90 kg | 120.0 | ||||||||||
461 | 2003-01-28T20:43 | 96.0 | 1 | 706 | 6.00 | 1181.30 | no rotation possible | 3.600 | 3.600 | ||||||
462 | 2003-01-28T22:15 | 206.0 | 1 | 544 | 13.00 | 1183.39 | 3.400 | 3.400 | 124.0 | ||||||
FR29 | 2003-01-29T01:26 | 1.00 | 1183.39 | calibration of load cell with dynamometer: 700 N too high reading at 20500 N | |||||||||||
463 | 2003-01-29T08:05 | 304.0 | 1 | 663 | 18.00 | 1186.38 | 3.360 | 3.440 | 128.0 | ||||||
464 | 2003-01-29T10:09 | 302.0 | 1 | 445 | 17.00 | 1189.50 | 3.600 | 4.100 | 135.0 | ||||||
465 | 2003-01-29T12:19 | 293.0 | 1 | 582 | 17.00 | 1192.46 | 3.200 | 3.400 | 140.0 | ||||||
466 | 2003-01-29T14:15 | 305.0 | 1 | 478 | 17.50 | 1195.43 | put one shim under the shoes respectively | 2.600 | 2.800 | 143.0 | 0.522 | 920.0 | -28.5 | ||
467 | 2003-01-29T16:13 | 705 | 1195.38 | 109.0 | |||||||||||
467 | 2003-01-29T16:13 | 319.0 | 2 | 525 | 18.50 | 1198.37 | changed to Danish head with 0.18 mm - 0.19 mm clearance to front of shoe | 3.000 | 3.160 | ||||||
468 | 2003-01-29T18:27 | 556 | 1200.50 | 114.0 | |||||||||||
468 | 2003-01-29T18:27 | 322.0 | 2 | 866 | 18.50 | 1201.64 | 3.200 | 3.300 | |||||||
469 | 2003-01-29T20:13 | 461 | 1202.87 | 119.0 | |||||||||||
469 | 2003-01-29T20:13 | 338.0 | 2 | 425 | 18.50 | 1205.01 | 3.200 | 3.200 | |||||||
470 | 2003-01-29T22:10 | 720 | 1206.45 | ||||||||||||
470 | 2003-01-29T22:10 | 208.0 | 2 | 603 | 6.00 | 1207.25 | |||||||||
471 | 2003-01-30T01:33 | 531 | 1208.77 | changed to new electronics: put more inclinometer heating, fixed 3 loose screws, where one had shorted, ground connector of 2 V source had gone off | 129.0 | ||||||||||
471 | 2003-01-30T01:33 | 237.0 | 2 | 672 | 17.00 | 1209.47 | |||||||||
472 | 2003-01-30T02:25 | 659 | 1210.73 | 136.0 | |||||||||||
472 | 2003-01-30T02:25 | 299.0 | 2 | 831 | 9.00 | 1212.63 | screw on side loose | ||||||||
473 | 2003-01-30T04:27 | 586 | 1212.89 | 140.0 | |||||||||||
473 | 2003-01-30T04:27 | 96.0 | 2 | 473 | 17.00 | 1213.47 | |||||||||
474 | 2003-01-30T05:55 | 259.0 | 1 | 587 | 15.00 | 1216.20 | 145.0 | ||||||||
475 | 2003-01-30T07:57 | 282.0 | 1 | 740 | 16.70 | 1219.20 | 3.150 | 3.160 | 150.0 | 0.572 | 918.0 | -26.3 | |||
476 | 2003-01-30T09:48 | 490 | 1220.40 | 112.0 | |||||||||||
476 | 2003-01-30T09:48 | 212.0 | 2 | 498 | 8.00 | 1221.02 | pump badly blocked with chips | 3.070 | 3.220 | ||||||
477 | 2003-01-30T11:39 | 892 | 1221.73 | 116.0 | |||||||||||
477 | 2003-01-30T11:39 | 208.0 | 2 | 463 | 16.00 | 1223.06 | 3.020 | 3.210 | |||||||
478 | 2003-01-30T13:14 | 731 | 1225.18 | 121.0 | |||||||||||
478 | 2003-01-30T13:14 | 320.0 | 2 | 490 | 17.50 | 1226.26 | 2.700 | 3.000 | |||||||
479 | 2003-01-30T15:20 | 458 | 1228.69 | cleaned and adjusted top valve | 126.0 | ||||||||||
479 | 2003-01-30T15:20 | 326.0 | 2 | 751 | 18.00 | 1229.52 | 3.000 | 3.000 | |||||||
480 | 2003-01-30T17:13 | 272.0 | 1 | 585 | 16.50 | 1232.98 | 2.950 | 3.180 | 131.0 | ||||||
481 | 2003-01-30T18:48 | 303.0 | 1 | 459 | 17.00 | 1235.33 | 2.850 | 2.850 | 135.0 | ||||||
482 | 2003-01-30T21:00 | 292.0 | 1 | 832 | 17.00 | 1238.40 | 3.000 | 3.200 | 140.0 | ||||||
483 | 2003-01-30T22:57 | 309.0 | 1 | 544 | 18.00 | 1241.49 | 145.0 | 0.501 | 917.0 | -26.0 | |||||
484 | 2003-01-31T00:37 | 301.0 | 1 | 613 | 17.00 | 1244.46 | 115.0 | ||||||||
485 | 2003-01-31T02:10 | 289.0 | 1 | 506 | 16.00 | 1247.41 | 121.0 | ||||||||
486 | 2003-01-31T03:39 | 285.0 | 1 | 474 | 16.00 | 1250.27 | 126.0 | ||||||||
487 | 2003-01-31T05:12 | 277.0 | 1 | 474 | 15.00 | 1253.02 | 130.0 | ||||||||
488 | 2003-01-31T06:40 | 292.0 | 1 | 506 | 17.00 | 1255.94 | 135.0 | ||||||||
489 | 2003-01-31T08:13 | 311.0 | 1 | 598 | 17.50 | 1258.93 | 2.980 | 3.140 | 139.0 | ||||||
490 | 2003-01-31T09:50 | 310.0 | 1 | 576 | 17.30 | 1261.99 | 3.180 | 3.180 | 143.0 | 0.552 | 918.0 | -26.4 | |||
491 | 2003-01-31T11:22 | 311.0 | 1 | 618 | 17.50 | 1265.04 | 2.980 | 3.160 | 109.0 | ||||||
492 | 2003-01-31T13:02 | 308.0 | 1 | 592 | 17.00 | 1268.17 | 2.500 | 2.700 | 114.0 | ||||||
493 | 2003-01-31T14:41 | 262.0 | 1 | 494 | 16.00 | 1270.97 | 3.000 | 3.000 | 118.0 | ||||||
494 | 2003-01-31T16:15 | 695 | 1273.18 | 123.0 | |||||||||||
494 | 2003-01-31T16:15 | 321.0 | 2 | 434 | 17.50 | 1273.89 | 3.140 | 3.480 | |||||||
495 | 2003-01-31T18:03 | 306.0 | 1 | 660 | 18.00 | 1277.05 | 3.080 | 3.150 | 128.0 | ||||||
496 | 2003-01-31T20:00 | 311.0 | 1 | 460 | 18.00 | 1280.24 | 2.750 | 2.750 | 133.0 | ||||||
497 | 2003-01-31T21:46 | 320.0 | 1 | 656 | 18.00 | 1283.45 | changed to shaft with narrow holes | 2.900 | 2.900 | 137.0 | |||||
498 | 2003-01-31T23:33 | 292.0 | 1 | 695 | 17.00 | 1286.49 | 143.0 | ||||||||
499 | 2003-02-01T01:12 | 290.0 | 1 | 412 | 17.00 | 1289.36 | 147.0 | 0.572 | 918.0 | -26.3 | |||||
500 | 2003-02-01T02:45 | 287.0 | 1 | 424 | 16.00 | 1292.16 | 115.0 | ||||||||
501 | 2003-02-01T04:12 | 297.0 | 1 | 732 | 17.00 | 1295.19 | 123.0 | ||||||||
502 | 2003-02-01T05:42 | 284.0 | 1 | 618 | 17.00 | 1298.03 | 128.0 | ||||||||
503 | 2003-02-01T07:08 | 264.0 | 1 | 567 | 16.50 | 1300.67 | 3.010 | 3.100 | 133.0 | ||||||
504 | 2003-02-01T09:04 | 308.0 | 1 | 551 | 16.50 | 1303.54 | 3.080 | 3.820 | 134.0 | ||||||
505 | 2003-02-01T10:29 | 308.0 | 1 | 677 | 17.00 | 1306.71 | 2.600 | 2.870 | 140.0 | ||||||
506 | 2003-02-01T11:59 | 313.0 | 1 | 408 | 17.00 | 1309.77 | 2.860 | 2.870 | 115.0 | 0.622 | 914.0 | -22.8 | |||
507 | 2003-02-01T13:27 | 312.0 | 1 | 521 | 18.00 | 1313.00 | 2.800 | 2.800 | 108.0 | ||||||
508 | 2003-02-01T15:00 | 288.0 | 1 | 555 | 17.50 | 1316.06 | 2.900 | 2.900 | 112.0 | ||||||
509 | 2003-02-01T16:29 | 286.0 | 1 | 572 | 17.50 | 1318.72 | 2.900 | 2.900 | 117.0 | ||||||
510 | 2003-02-01T17:59 | 307.0 | 1 | 649 | 17.50 | 1321.81 | 2.900 | 2.900 | 122.0 | ||||||
511 | 2003-02-02T11:23 | 305.0 | 1 | 594 | 18.00 | 1324.83 | 2.900 | 2.900 | 126.0 | ||||||
512 | 2003-02-02T13:06 | 302.0 | 1 | 378 | 17.50 | 1327.92 | 2.690 | 2.740 | 132.0 | ||||||
513 | 2003-02-02T14:44 | 303.0 | 1 | 672 | 17.00 | 1331.01 | 2.700 | 2.700 | 140.0 | ||||||
514 | 2003-02-02T16:18 | 308.0 | 1 | 638 | 17.00 | 1333.40 | two power failures on the way down | both bronce slide bearings broken | 2.600 | 2.600 | 142.0 | ||||
515 | 2003-02-02T18:40 | 320.0 | 1 | 510 | 17.80 | 1337.25 | 2.620 | 2.730 | 145.0 | ||||||
516 | 2003-02-02T20:30 | 268.0 | 1 | 532 | 16.50 | 1340.02 | 155.0 | ||||||||
517 | 2003-02-02T22:04 | 297.0 | 1 | 633 | 17.00 | 1343.03 | 158.0 | 0.620 | 919.0 | -28.1 | |||||
518 | 2003-02-02T23:40 | 310.0 | 1 | 391 | 16.50 | 1346.04 | 2.550 | 2.600 | 121.0 | ||||||
519 | 2003-02-03T01:49 | 304.0 | 1 | 574 | 17.00 | 1349.12 | 2.400 | 2.500 | 125.0 | ||||||
520 | 2003-02-03T03:57 | 316.0 | 1 | 558 | 18.00 | 1352.20 | 2.600 | 2.650 | 129.0 | ||||||
521 | 2003-02-03T06:03 | 319.0 | 1 | 563 | 18.00 | 1355.43 | 2.800 | 2.800 | 133.0 | ||||||
522 | 2003-02-03T08:35 | 313.0 | 1 | 586 | 18.00 | 1358.29 | 2.800 | 2.800 | 137.0 | ||||||
523 | 2003-02-03T10:23 | 301.0 | 1 | 471 | 18.00 | 1361.61 | 2.700 | 2.900 | 142.0 | ||||||
524 | 2003-02-03T13:11 | 285.0 | 1 | 865 | 17.50 | 1364.41 | changed all four slide bearings | 147.0 | |||||||
525 | 2003-02-03T14:51 | 304.0 | 1 | 712 | 17.00 | 1367.52 | 155.0 | ||||||||
526 | 2003-02-03T17:00 | 292.0 | 1 | 508 | 17.00 | 1370.37 | 2.500 | 2.500 | 157.0 | 0.485 | 921.0 | -29.5 | |||
527 | 2003-02-03T18:57 | 283.0 | 1 | 729 | 16.50 | 1373.11 | changed to Danish drill head with new cutters and sharpened core catchers, clearance to front of shoe 0.18 mm | 2.700 | 2.900 | 124.0 | |||||
528 | 2003-02-03T20:52 | 230.0 | 1 | 481 | 13.50 | 1375.58 | 3.100 | 3.100 | 133.0 | ||||||
529 | 2003-02-03T22:20 | 271.0 | 1 | 657 | 15.00 | 1378.27 | modified rpm limit and torque limit settings of winch controller to pull faster and more secure | 3.200 | 3.200 | 138.0 | |||||
530 | 2003-02-03T23:55 | 301.0 | 1 | 489 | 17.00 | 1381.27 | 3.000 | 3.100 | 143.0 | ||||||
531 | 2003-02-04T01:37 | 295.0 | 1 | 826 | 16.50 | 1384.23 | 3.200 | 3.200 | 145.0 | ||||||
532 | 2003-02-04T03:49 | 779 | 1386.10 | 151.0 | |||||||||||
532 | 2003-02-04T03:49 | 321.0 | 2 | 867 | 18.00 | 1387.21 | 3.100 | 3.150 | |||||||
533 | 2003-02-04T05:49 | 264.0 | 1 | 588 | 16.00 | 1390.47 | 3.100 | 3.100 | 157.0 | ||||||
534 | 2003-02-04T07:53 | 470 | 1392.32 | 163.0 | |||||||||||
534 | 2003-02-04T07:53 | 342.0 | 2 | 495 | 18.00 | 1393.35 | 3.100 | 3.300 | 0.434 | 922.0 | -31.4 | ||||
535 | 2003-02-04T09:49 | 912 | 1395.44 | no core break, lower to 140 kg | 132.0 | ||||||||||
535 | 2003-02-04T09:49 | 204.0 | 1 | 500 | 13.00 | 1395.44 | 3.200 | 3.200 | |||||||
536 | 2003-02-04T11:27 | 285.0 | 1 | 591 | 17.50 | 1398.33 | 3.200 | 3.200 | 135.0 | ||||||
537 | 2003-02-04T13:09 | 237.0 | 1 | 490 | 14.00 | 1400.71 | winch has really bad spooling errors | 140.0 | |||||||
538 | 2003-02-04T14:50 | 237.0 | 1 | 824 | 13.00 | 1403.06 | spooling down to arrange cable | 147.0 | |||||||
539 | 2003-02-04T16:50 | 254.0 | 1 | 907 | 14.80 | 1405.66 | 3.200 | 3.200 | 152.0 | ||||||
540 | 2003-02-04T20:20 | 98.0 | 1 | 904 | 5.00 | 1406.68 | changed to Danish drill head No.1, clearance 0.16 mm - 0.17 mm | 2.750 | 2.750 | 157.0 | |||||
541 | 2003-02-04T21:45 | 217.0 | 1 | 446 | 14.00 | 1408.90 | changed to Danish drill head No. 0, clearance 0.18 mm | 3.100 | 3.100 | 150.0 | 0.572 | 921.0 | -30.0 | ||
542 | 2003-02-04T23:32 | 311.0 | 1 | 707 | 17.50 | 1411.86 | 3.000 | 3.000 | 127.0 | ||||||
543 | 2003-02-05T01:33 | 258.0 | 1 | 492 | 16.00 | 1414.58 | 3.050 | 3.300 | 132.0 | ||||||
544 | 2003-02-05T03:28 | 276.0 | 1 | 504 | 17.50 | 1417.39 | 3.000 | 3.050 | 136.0 | ||||||
545 | 2003-02-05T05:30 | 256.0 | 1 | 743 | 14.50 | 1420.10 | 3.050 | 3.100 | 141.0 | ||||||
546 | 2003-02-05T07:13 | 479 | 1421.20 | 146.0 | |||||||||||
546 | 2003-02-05T07:13 | 305.0 | 2 | 494 | 17.00 | 1422.93 | changed to Danish drill head No.1, clearance 0.18 mm - 0.19 mm | 3.400 | 3.400 | ||||||
547 | 801 | 1424.37 | 149.0 | ||||||||||||
547 | 2003-02-05T09:30 | 266.0 | 2 | 502 | 16.00 | 1425.44 | 3.400 | 3.400 | |||||||
548 | 2003-02-05T11:25 | 519 | 1426.72 | removed on shim from each cutter respectively | 154.0 | ||||||||||
548 | 2003-02-05T11:25 | 192.0 | 2 | 708 | 11.50 | 1427.40 | 3.900 | 3.900 | |||||||
549 | 2003-02-05T13:17 | 233.0 | 1 | 484 | 14.00 | 1429.81 | 2.800 | 2.800 | 158.0 | 0.556 | 923.0 | -31.8 | |||
550 | 2003-02-05T14:46 | 298.0 | 1 | 526 | 16.50 | 1432.76 | 141.0 | ||||||||
551 | 2003-02-05T16:28 | 245.0 | 1 | 544 | 14.50 | 1435.24 | 2.900 | 2.900 | 133.0 | ||||||
552 | 2003-02-05T18:03 | 298.0 | 1 | 721 | 17.00 | 1438.21 | 134.0 | ||||||||
553 | 2003-02-05T19:49 | 238.0 | 1 | 745 | 14.00 | 1440.61 | 142.0 | ||||||||
554 | 2003-02-05T21:26 | 272.0 | 1 | 828 | 15.50 | 1443.34 | 145.0 | ||||||||
FR30 | 2003-02-05T23:12 | 2.00 | 1443.34 | very clean hole with tiny amount of grey slush | 147.0 | ||||||||||
555 | 2003-02-06T00:50 | 220.0 | 1 | 490 | 13.00 | 1445.57 | soldered broken plug in winchs remote control | 2.950 | 2.950 | 152.0 | 0.497 | 923.0 | -32.8 | ||
556 | 2003-02-06T03:09 | 309.0 | 1 | 581 | 19.00 | 1448.70 | 3.000 | 3.100 | 125.0 | ||||||
557 | 2003-02-06T05:10 | 311.0 | 1 | 699 | 19.00 | 1451.86 | 2.950 | 2.950 | 127.0 | ||||||
558 | 2003-02-06T07:09 | 259.0 | 1 | 504 | 15.00 | 1454.46 | 3.200 | 3.200 | 130.0 | ||||||
559 | 2003-02-06T09:13 | 306.0 | 1 | 435 | 17.50 | 1457.46 | changed to Danish head No.1, clearance 0.18 mm - 0.19 mm | 2.900 | 2.900 | 132.0 | |||||
560 | 2003-02-06T11:03 | 286.0 | 1 | 667 | 17.00 | 1460.40 | 2.900 | 2.900 | 137.0 | ||||||
561 | 2003-02-06T12:54 | 271.0 | 1 | 606 | 16.00 | 1462.91 | 141.0 | ||||||||
562 | 2003-02-06T14:25 | 286.0 | 2 | 653 | 16.00 | 1465.71 | 149.0 | ||||||||
563 | 2003-02-06T15:56 | 280.0 | 1 | 595 | 16.00 | 1468.57 | 3.000 | 3.000 | 153.0 | ||||||
564 | 2003-02-06T17:37 | 275.0 | 1 | 540 | 16.50 | 1471.40 | 3.000 | 3.100 | 157.0 | ||||||
565 | 2003-02-06T19:33 | 301.0 | 1 | 505 | 17.00 | 1474.42 | 161.0 | 0.521 | 922.5 | -31.6 | |||||
566 | 2003-02-06T21:10 | 32.0 | 1 | 472 | 4.50 | 1474.68 | changed to Rufli head No. 4 with core barrel attachments for testing purpose, clearance 0.165 mm - 0.18 mm to front edge of shoe | 143.0 | |||||||
567 | 2003-02-06T22:20 | 279.0 | 1 | 863 | 15.50 | 1477.53 | changed back to Danish head No.1, clearance 0.18 mm - 0.19 mm | 135.0 | |||||||
568 | 2003-02-06T23:54 | 263.0 | 1 | 735 | 14.50 | 1480.26 | 2.950 | 2.950 | 140.0 | ||||||
569 | 2003-02-07T01:34 | 282.0 | 1 | 646 | 16.50 | 1483.07 | winch cable cutting into the lower layer below even at 2750 N load | 2.950 | 2.950 | 144.0 | |||||
570 | 2003-02-07T04:38 | 533 | 1484.70 | 149.0 | |||||||||||
570 | 2003-02-07T04:38 | 331.0 | 2 | 579 | 18.00 | 1486.18 | 2.900 | 3.000 | |||||||
571 | 2003-02-07T06:41 | 828 | 1487.72 | 154.0 | |||||||||||
571 | 2003-02-07T06:41 | 314.0 | 2 | 843 | 18.00 | 1489.26 | 2.900 | 2.900 | |||||||
572 | 2003-02-07T09:48 | 223.0 | 1 | 781 | 15.00 | 1491.75 | changed to Danish head No. 0, clearance 0.17 mm - 0.18 mm | 157.0 | |||||||
573 | 2003-02-07T12:30 | 240.0 | 1 | 795 | 14.00 | 1494.12 | 160.0 | 0.504 | 922.0 | -31.0 | |||||
574 | 2003-02-07T14:33 | 192.0 | 1 | 528 | 11.50 | 1496.00 | 130.0 | ||||||||
575 | 2003-02-07T16:15 | 174.0 | 1 | 521 | 10.00 | 1497.59 | changed to Danish head No. 1, clearance 0.17 mm - 0.18 mm, antitorque loosened by 0.5 mm | loose screw in pump fastened | 3.400 | 3.400 | |||||
576 | 2003-02-07T18:05 | 313.0 | 1 | 555 | 18.00 | 1500.76 | 2.750 | 2.750 | 138.0 | ||||||
577 | 2003-02-07T20:01 | 284.0 | 1 | 533 | 16.00 | 1503.67 | 145.0 | ||||||||
578 | 2003-02-07T21:33 | 297.0 | 1 | 692 | 17.00 | 1506.74 | 150.0 | ||||||||
579 | 2003-02-07T23:12 | 293.0 | 1 | 766 | 17.50 | 1509.72 | 2.500 | 2.600 | 154.0 | ||||||
580 | 2003-02-08T01:20 | 901 | 1511.54 | 2.600 | 2.600 | 159.0 | |||||||||
580 | 2003-02-08T01:20 | 173.0 | 1 | 312 | 17.50 | 1512.61 | about 1.3 m core left in hole due to blocked core catcher | 0.538 | 920.0 | -28.7 | |||||
581 | 2003-02-08T03:50 | 309.0 | 1 | 465 | 11.50 | 1514.41 | 2.350 | 2.450 | 125.0 | ||||||
582 | 2003-02-08T05:39 | 308.0 | 1 | 500 | 18.00 | 1517.62 | 2.350 | 2.600 | 129.0 | ||||||
583 | 2003-02-08T07:26 | 304.0 | 1 | 561 | 18.00 | 1520.76 | 2.400 | 2.400 | 134.0 | ||||||
584 | 2003-02-08T09:16 | 286.0 | 1 | 781 | 17.50 | 1523.50 | 2.500 | 2.500 | 135.0 | ||||||
585 | 2003-02-08T10:57 | 592 | 1525.76 | 139.0 | |||||||||||
585 | 2003-02-08T10:57 | 335.0 | 2 | 645 | 18.00 | 1526.63 | 2.400 | 2.400 | |||||||
586 | 2003-02-08T12:51 | 275.0 | 1 | 515 | 17.00 | 1529.46 | 145.0 | ||||||||
587 | 2003-02-08T14:35 | 306.0 | 1 | 757 | 16.50 | 1532.56 | 152.0 | ||||||||
588 | 2003-02-08T16:17 | 298.0 | 1 | 514 | 18.00 | 1535.61 | 2.400 | 2.400 | 157.0 | ||||||
589 | 2003-02-08T18:04 | 313.0 | 1 | 477 | 18.00 | 1538.63 | 160.0 | 0.518 | 923.0 | -31.5 | |||||
590 | 2003-02-08T19:56 | 304.0 | 1 | 456 | 17.50 | 1541.70 | 126.0 | ||||||||
591 | 2003-02-08T21:52 | 295.0 | 1 | 736 | 17.00 | 1544.66 | 130.0 | ||||||||
592 | 2003-02-08T23:42 | 312.0 | 1 | 519 | 17.50 | 1547.82 | 2.200 | 2.400 | 135.0 | ||||||
593 | 2003-02-09T01:35 | 295.0 | 1 | 512 | 17.50 | 1550.77 | 140.0 | ||||||||
FR31 | 2003-02-09T03:28 | 1550.77 | 143.0 | ||||||||||||
594 | 2003-02-09T05:22 | 60.0 | 1 | 751 | 5.00 | 1551.55 | changed to HT drill with plastic flights for cleaning | 144.8 | |||||||
2003-02-09T15:00 | 1551.55 | 0.566 | 924.0 | -33.1 | |||||||||||
2003-02-09T16:00 | 1551.55 | 0.607 | 923.0 | -32.1 | |||||||||||
2003-02-09T17:00 | 1551.55 | indicated liquid level about 75 m | 0.206 | 921.0 | -28.5 | ||||||||||
END | 2003-02-10T12:00 | 1551.55 | plumbing with antitorque zeroed on lid | 76.2 | |||||||||||
START | 2003-12-08T09:00 | 1551.55 | logging the hole, indicated liquid level about 81m | ||||||||||||
595 | 2003-12-09T09:25 | 204.0 | 1 | 837 | 17.00 | 1553.05 | drill head H1 with 18/100 mm shoe clearance of 4.0 mm shoes; distance pins on upper coupling 14.3-4 mm | 3.240 | 3.240 | 81.0 | |||||
596 | 2003-12-09T12:07 | 192.0 | 1 | 455 | 12.00 | 1555.03 | 88.0 | ||||||||
597 | 2003-12-09T13:54 | 205.0 | 1 | 682 | 12.50 | 1557.16 | 3.400 | 3.400 | |||||||
598 | 2003-12-09T16:03 | 192.0 | 1 | 505 | 11.00 | 1559.06 | 3.480 | 3.480 | 93.0 | ||||||
599 | 2003-12-09T18:20 | 246.0 | 1 | 555 | 14.00 | 1561.50 | |||||||||
600 | 2003-12-10T09:07 | 160.5 | 1 | 863 | 9.50 | 1562.94 | 3.000 | 3.000 | 97.0 | ||||||
601 | 2003-12-10T11:30 | 268.0 | 1 | 974 | 16.00 | 1565.64 | 3.200 | 3.200 | 100.0 | ||||||
602 | 2003-12-10T14:10 | 909 | 1568.24 | core did not break on first pull, go back | 3.200 | 3.200 | |||||||||
602 | 2003-12-10T14:10 | 228.0 | 1 | 430 | 12.50 | 1568.24 | 3.200 | 3.200 | 98.0 | ||||||
603 | 2003-12-10T16:30 | 307.0 | 2 | 825 | 18.00 | 1571.13 | pump disengaged | 3.300 | 3.300 | 98.0 | |||||
604 | 2003-12-10T20:25 | 184.5 | 1 | 1153 | 13.00 | 1572.84 | core catchers could not be disengaged by going back | 3.300 | 3.300 | 99.0 | |||||
605 | 2003-12-11T09:35 | 295.0 | 1 | 634 | 17.00 | 1575.90 | 2.900 | 2.900 | 104.0 | ||||||
606 | 2003-12-11T11:55 | 245.0 | 1 | 595 | 15.00 | 1578.38 | 3.200 | 3.200 | 105.0 | ||||||
607 | 2003-12-11T14:03 | 240.0 | 1 | 722 | 13.00 | 1580.85 | 3.200 | 3.200 | 110.0 | ||||||
608 | 2003-12-11T16:25 | 258.0 | 1 | 890 | 13.00 | 1583.35 | 3.200 | 3.200 | 100.0 | ||||||
609 | 2003-12-11T18:36 | 273.5 | 1 | 516 | 15.00 | 1586.10 | 3.280 | 3.280 | 106.0 | ||||||
610 | 2003-12-11T20:58 | 232.5 | 1 | 650 | 14.50 | 1588.92 | 3.200 | 3.200 | 110.0 | ||||||
611 | 2003-12-12T10:00 | 260.0 | 1 | 681 | 16.00 | 1590.94 | 3.100 | 3.100 | 155.0 | ||||||
612 | 2003-12-12T13:04 | 172.0 | 1 | 518 | 11.00 | 1591.55 | 3.200 | 3.200 | 148.0 | ||||||
613 | 2003-12-12T15:52 | 258.0 | 2 | 729 | 15.50 | 1595.21 | bottom break | 3.200 | 3.200 | 151.0 | |||||
614 | 2003-12-12T18:33 | 165.0 | 1 | 729 | 10.00 | 1596.86 | 3.260 | 3.260 | 154.0 | ||||||
615 | 2003-12-12T21:03 | 312.0 | 1 | 596 | 17.00 | 1599.89 | 3.050 | 3.050 | 157.0 | ||||||
616 | 2003-12-13T09:33 | 276.0 | 1 | 607 | 16.00 | 1602.70 | 2.800 | 2.800 | 165.0 | 0.633 | 919.0 | -27.5 | |||
617 | 2003-12-13T13:35 | 265.0 | 1 | 856 | 15.00 | 1605.41 | 2.800 | 2.800 | 125.0 | ||||||
618 | 2003-12-13T16:11 | 231.0 | 1 | 885 | 14.50 | 1607.80 | 2.700 | 2.700 | 129.0 | ||||||
619 | 2003-12-14T15:15 | 208.0 | 2 | 710 | 11.50 | 1609.59 | changed to drill head H2 withh 17/100 mm clearance an 3.6 mm nominal pitch shoes | pump disengaged, one flap from upper piston found in chips | 3.300 | 3.300 | 132.0 | ||||
620 | 2003-12-14T17:12 | 222.0 | 1 | 505 | 13.50 | 1611.99 | 3.300 | 3.300 | 137.0 | ||||||
621 | 2003-12-14T19:29 | 900 | 1614.49 | no core break, wnet down to 230 kg and rotated 2 times F8 | |||||||||||
621 | 2003-12-14T19:29 | 246.0 | 1 | 712 | 14.00 | 1614.49 | liquid sample from core barrel: 922.5 kg/m**3 at -38°C | 3.300 | 3.300 | 143.0 | |||||
622 | 2003-12-14T21:33 | 208.0 | 1 | 838 | 13.00 | 1616.59 | 3.300 | 3.300 | 147.0 | ||||||
623 | 2003-12-15T08:15 | 254.0 | 1 | 701 | 14.50 | 1619.14 | 3.200 | 3.200 | 153.0 | ||||||
624 | 2003-12-15T10:36 | 257.0 | 1 | 537 | 16.00 | 1621.75 | 3.300 | 3.300 | 158.0 | ||||||
625 | 2003-12-15T12:46 | 253.0 | 1 | 545 | 13.00 | 1624.26 | 3.300 | 3.300 | 160.0 | 0.575 | 916.0 | -24.5 | |||
626 | 2003-12-15T15:07 | 233.0 | 1 | 878 | 13.50 | 1626.50 | 3.400 | 3.400 | 126.0 | ||||||
627 | 2003-12-15T17:00 | 232.0 | 1 | 520 | 13.00 | 1628.79 | 3.400 | 3.400 | 128.0 | ||||||
628 | 2003-12-15T19:10 | 236.0 | 1 | 582 | 13.00 | 1631.16 | 3.200 | 3.200 | 131.0 | ||||||
629 | 2003-12-15T21:09 | 220.0 | 1 | 633 | 13.00 | 1633.46 | 3.300 | 3.300 | 136.0 | ||||||
630 | 2003-12-15T23:03 | 230.0 | 1 | 726 | 13.00 | 1635.61 | 2.300 | 2.300 | 140.0 | ||||||
631 | 2003-12-16T08:08 | 888 | 1637.71 | pulled till torque limit settin of winch | |||||||||||
631 | 2003-12-16T08:08 | 210.0 | 1 | 608 | 13.00 | 1637.71 | 2.100 | 2.100 | 144.0 | ||||||
632 | 2003-12-16T10:25 | 293.0 | 1 | 517 | 16.50 | 1640.84 | changed to drill head H2 0.16, 0.17, 0.17mm clearance, shoes nominal 3.6 mm | pump disengaged | 2.950 | 2.950 | 149.0 | ||||
633 | 2003-12-16T12:40 | 322.0 | 3 | 643 | 18.00 | 1643.92 | 3.000 | 3.000 | 154.0 | ||||||
634 | 2003-12-16T14:38 | 267.0 | 1 | 737 | 15.00 | 1646.54 | 3.100 | 3.100 | 159.0 | ||||||
635 | 2003-12-16T17:00 | 900 | 1649.62 | ||||||||||||
635 | 2003-12-16T17:00 | 308.0 | 1 | 961 | 19.00 | 1649.62 | pump disengaged | 2.900 | 2.900 | 167.0 | 0.431 | 917.0 | -25.9 | ||
636 | 2003-12-16T19:48 | 282.0 | 1 | 610 | 16.00 | 1652.40 | pump disengaged | 2.900 | 2.900 | 138.0 | 0.365 | 914.0 | -22.5 | ||
637 | 2003-12-16T21:58 | 900 | 1655.08 | ||||||||||||
637 | 2003-12-16T21:58 | 271.0 | 1 | 823 | 16.00 | 1655.08 | 3.100 | 3.100 | 115.0 | ||||||
FR32 | 2003-12-17T07:12 | 0.25 | 1655.08 | went fast down to the bottom of the hole; hole absolutely clean | |||||||||||
638 | 2003-12-17T09:12 | 251.0 | 1 | 554 | 15.50 | 1657.48 | core catchers sharpened on drill head H2 | 3.000 | 3.000 | 121.0 | |||||
639 | 2003-12-17T11:55 | 283.0 | 1 | 604 | 16.00 | 1660.57 | ice in screw hole under one shoe | 2.900 | 2.900 | 125.0 | |||||
640 | 2003-12-17T14:07 | 201.0 | 1 | 906 | 12.00 | 1662.57 | 3.000 | 3.000 | 130.0 | ||||||
641 | 2003-12-17T15:58 | 224.0 | 1 | 689 | 13.00 | 1664.68 | 3.100 | 3.100 | 134.0 | ||||||
642 | 2003-12-17T17:45 | 243.0 | 1 | 844 | 14.00 | 1667.12 | 3.100 | 3.100 | 139.0 | ||||||
643 | 2003-12-17T19:40 | 211.0 | 1 | 663 | 12.00 | 1669.27 | 3.000 | 3.000 | 143.0 | ||||||
644 | 2003-12-17T21:32 | 258.0 | 1 | 557 | 14.00 | 1671.90 | 3.050 | 3.100 | 150.0 | ||||||
645 | 2003-12-17T23:19 | 254.0 | 1 | 525 | 14.50 | 1674.51 | 3.000 | 3.000 | 153.0 | ||||||
646 | 2003-12-18T08:15 | 223.0 | 1 | 546 | 13.00 | 1676.58 | head H2: cutters better aligned than +/-5/1000 mm, adjusted to 17/100 mm | 3.100 | 3.100 | 156.0 | |||||
647 | 2003-12-18T10:45 | 212.0 | 1 | 566 | 13.00 | 1678.68 | core barrel changed | 3.000 | 3.000 | 161.0 | |||||
648 | 2003-12-18T12:54 | 500 | 1679.16 | no penetration at 270 kg load | 2.700 | 2.700 | 170.0 | ||||||||
648 | 2003-12-18T12:54 | 56.0 | 2 | 649 | 4.00 | 1679.25 | no penetration | 2.700 | 2.700 | 170.0 | |||||
649 | 2003-12-18T15:03 | 59.0 | 2 | 632 | 4.00 | 1679.88 | no penetration | 2.600 | 2.600 | 172.0 | 0.442 | 915.0 | -22.4 | ||
650 | 2003-12-18T17:24 | 83.0 | 1 | 862 | 5.00 | 1680.74 | rested drill with cutter load 0 to get rid of chips under the cutter shoes. | 2.300 | 3.100 | ||||||
651 | 2003-12-18T20:06 | 202.0 | 1 | 535 | 11.00 | 1682.56 | grinded lower face of shoes to get rid of edges at screwholes | put in spacer in lower end of the pump | 2.900 | 2.900 | 142.0 | ||||
652 | 2003-12-18T22:07 | 190.0 | 1 | 913 | 11.00 | 1684.74 | 2.900 | 2.900 | 145.0 | ||||||
653 | 2003-12-19T08:33 | 554 | 1686.12 | ||||||||||||
653 | 2003-12-19T08:33 | 302.0 | 2 | 829 | 18.00 | 1687.47 | 2.900 | 3.100 | 149.0 | ||||||
654 | 2003-12-19T11:10 | 279.0 | 1 | 984 | 15.00 | 1690.22 | 2.900 | 2.900 | 121.0 | 0.454 | 914.0 | -22.5 | |||
655 | 2003-12-19T13:44 | 256.0 | 1 | 727 | 14.00 | 1692.78 | 2.800 | 2.800 | 126.0 | ||||||
656 | 2003-12-19T15:48 | 273.0 | 1 | 512 | 15.00 | 1695.63 | 2.900 | 2.900 | 130.0 | ||||||
657 | 2003-12-19T18:14 | 593 | 1696.80 | no rotation | |||||||||||
657 | 2003-12-19T18:14 | 282.0 | 2 | 620 | 16.00 | 1698.29 | 2.900 | 2.900 | 134.0 | ||||||
658 | 2003-12-19T21:03 | 241.5 | 2 | 647 | 13.00 | 1700.82 | 2.900 | 2.900 | 139.0 | ||||||
659 | 2003-12-19T23:08 | 828 | 1702.59 | high idle current | |||||||||||
659 | 2003-12-19T23:08 | 227.0 | 2 | 524 | 14.00 | 1703.13 | 2.900 | 2.900 | 144.0 | ||||||
660 | 2003-12-20T08:18 | 274.0 | 1 | 617 | 17.00 | 1705.96 | 2.800 | 2.800 | 149.0 | ||||||
661 | 2003-12-20T10:40 | 255.0 | 1 | 530 | 16.00 | 1708.52 | 2.900 | 2.900 | 116.0 | 0.506 | 917.0 | -25.5 | |||
662 | 2003-12-20T12:50 | 252.0 | 1 | 854 | 14.50 | 1711.03 | 3.000 | 3.000 | 120.0 | ||||||
663 | 2003-12-20T14:49 | 264.0 | 1 | 848 | 16.50 | 1713.76 | 2.800 | 2.800 | 124.0 | ||||||
664 | 2003-12-21T13:15 | 251.0 | 1 | 875 | 13.50 | 1716.19 | 2.900 | 2.900 | 129.0 | ||||||
665 | 2003-12-21T15:20 | 283.0 | 1 | 905 | 16.00 | 1719.05 | 3.000 | 3.000 | 133.0 | ||||||
666 | 2003-12-21T17:26 | 900 | 1721.55 | pulled and decended to 175 | |||||||||||
666 | 2003-12-21T17:26 | 905 | 1721.55 | pulled and decended to 180 | |||||||||||
666 | 2003-12-21T17:26 | 253.0 | 1 | 649 | 14.00 | 1721.55 | 3.100 | 3.100 | 137.0 | ||||||
667 | 2003-12-21T19:33 | 268.5 | 1 | 828 | 14.50 | 1724.16 | 2.900 | 2.900 | 142.0 | ||||||
668 | 2003-12-21T21:22 | 268.5 | 1 | 485 | 15.00 | 1726.93 | 2.900 | 2.900 | 148.0 | ||||||
669 | 2003-12-21T23:46 | 169.0 | 2 | 530 | 10.00 | 1728.52 | sharpened one cutter | fixed one pin of pump flap | 2.750 | 2.750 | 120.0 | 0.419 | 912.5 | -20.5 | |
670 | 2003-12-22T02:08 | 900 | 1731.71 | ||||||||||||
670 | 2003-12-22T02:08 | 300.0 | 1 | 460 | 16.50 | 1731.71 | 2.650 | 2.650 | 125.0 | ||||||
671 | 2003-12-22T04:10 | 308.0 | 1 | 675 | 17.00 | 1734.80 | 2.650 | 2.650 | 129.0 | ||||||
672 | 2003-12-22T06:15 | 296.0 | 1 | 652 | 17.00 | 1737.71 | 2.800 | 2.800 | 134.0 | ||||||
673 | 2003-12-22T08:15 | 284.0 | 1 | 715 | 17.00 | 1740.56 | 2.700 | 2.700 | 139.0 | ||||||
674 | 2003-12-22T10:25 | 271.0 | 1 | 830 | 15.00 | 1743.19 | 2.700 | 2.700 | 144.0 | ||||||
675 | 2003-12-22T12:10 | 901 | 1746.23 | ||||||||||||
675 | 2003-12-22T12:10 | 308.0 | 1 | 856 | 17.50 | 1746.23 | 3.000 | 3.000 | 118.0 | 0.524 | 916.0 | -24.5 | |||
676 | 2003-12-22T14:22 | 906 | 1747.45 | ||||||||||||
676 | 2003-12-22T14:22 | 139.0 | 2 | 580 | 9.00 | 1747.37 | piece of plastic on top of core; lower ball bearing of electronics broken | 2.500 | 2.500 | 115.0 | |||||
677 | 2003-12-22T19:07 | 187.0 | 1 | 761 | 10.50 | 1749.45 | 2.300 | 2.300 | |||||||
678 | 2003-12-22T21:29 | 249.5 | 1 | 910 | 15.00 | 1751.98 | changed to other core barrel with drill head H1, shoes nominal 4mm, clearance 16.5, 17, 17.5/100mm, antitorque measured 30.0, 30.3, 31.0 mm | 2.100 | 2.100 | 122.0 | |||||
679 | 2003-12-22T23:33 | 1752.06 | one screw to hold cutters damaged | 128.0 | |||||||||||
FR33 | 2003-12-23T01:45 | 1752.06 | fished a piece of ball from the broken ball bearing with the magnetic tool | ||||||||||||
680 | 2003-12-23T04:24 | 776 | 1752.16 | persistent anti torque rotation | |||||||||||
680 | 2003-12-23T04:24 | 295.0 | 3 | 804 | 19.00 | 1754.64 | 2.300 | 2.300 | 130.0 | ||||||
681 | 2003-12-23T07:04 | 259.0 | 1 | 780 | 15.00 | 1757.60 | few antitorque rotations | 2.400 | 2.400 | 135.0 | |||||
682 | 2003-12-23T09:08 | 228.0 | 1 | 598 | 13.00 | 1760.07 | few antitorque rotations | 2.700 | 2.700 | 140.0 | |||||
683 | 2003-12-23T11:15 | 240.0 | 1 | 614 | 13.00 | 1762.27 | few antitorque rotations | 2.500 | 2.500 | 0.524 | 918.0 | -26.0 | |||
684 | 2003-12-23T13:51 | 900 | 1764.64 | few antitorque rotations | |||||||||||
684 | 2003-12-23T13:51 | 241.0 | 1 | 840 | 14.00 | 1764.64 | 2.600 | 2.600 | 110.0 | ||||||
685 | 2003-12-23T16:38 | 190.0 | 1 | 577 | 11.00 | 1766.48 | few antitorque rotations | 2.600 | 2.600 | 115.0 | |||||
686 | 2003-12-23T19:07 | 310.0 | 1 | 910 | 18.00 | 1769.51 | tighed antitorque 32.1 to 33.75mm | 2.700 | 2.700 | 119.0 | |||||
687 | 2003-12-23T21:32 | 228.0 | 1 | 764 | 15.00 | 1771.80 | tuned drill head H2, 16,17,17/100 mm clearance | 2.450 | 2.450 | 124.0 | |||||
688 | 2003-12-23T23:52 | 290.0 | 1 | 586 | 16.00 | 1775.00 | removed one shim under each cutter | 2.750 | 2.750 | 128.0 | |||||
689 | 2003-12-24T02:00 | 215.0 | 1 | 784 | 13.50 | 1777.23 | 2.850 | 2.850 | 132.0 | ||||||
690 | 2003-12-24T04:01 | 208.0 | 1 | 580 | 11.50 | 1779.33 | 2.900 | 2.900 | 137.0 | ||||||
691 | 2003-12-24T05:42 | 906 | 1782.31 | ||||||||||||
691 | 2003-12-24T05:42 | 305.0 | 1 | 566 | 17.00 | 1782.31 | 2.850 | 2.850 | 140.0 | ||||||
692 | 2003-12-24T07:50 | 257.0 | 1 | 892 | 15.00 | 1784.76 | 2.900 | 2.900 | 145.0 | ||||||
693 | 2003-12-24T09:42 | 307.0 | 1 | 625 | 17.00 | 1787.82 | 2.900 | 2.900 | 149.0 | ||||||
694 | 2003-12-24T11:45 | 287.0 | 1 | 589 | 16.50 | 1790.36 | 2.800 | 2.800 | 128.0 | 0.579 | 914.0 | -22.5 | |||
695 | 2003-12-24T13:50 | 257.0 | 1 | 766 | 15.00 | 1793.29 | 2.900 | 2.900 | 114.0 | ||||||
696 | 2003-12-24T16:13 | 276.0 | 1 | 772 | 16.50 | 1795.86 | switched to drill head H1 with Rufli cutter with 0.5 high edge, aligned better than +/-1/100mm, clearance 20/100mm | 3.100 | 3.100 | 120.0 | |||||
697 | 2003-12-25T11:13 | 256.0 | 1 | 827 | 14.00 | 1798.44 | 3.100 | 3.100 | 125.0 | ||||||
698 | 2003-12-25T13:20 | 296.0 | 2 | 865 | 16.00 | 1801.35 | 3.400 | 3.400 | 129.0 | ||||||
699 | 2003-12-25T15:34 | 644 | 1803.51 | 3.200 | 3.200 | 134.0 | |||||||||
699 | 2003-12-25T15:34 | 245.0 | 2 | 647 | 15.00 | 1803.82 | 3.200 | 3.200 | 134.0 | ||||||
700 | 2003-12-25T18:10 | 629 | 1804.95 | 3.500 | 3.500 | 138.0 | |||||||||
700 | 2003-12-25T18:10 | 214.0 | 2 | 633 | 12.00 | 1806.21 | 3.500 | 3.500 | 138.0 | ||||||
701 | 2003-12-25T20:26 | 591 | 1807.25 | 3.500 | 3.500 | 143.0 | 0.351 | 917.0 | -22.4 | ||||||
701 | 2003-12-25T20:26 | 252.0 | 2 | 864 | 14.00 | 1808.52 | 3.500 | 3.500 | 143.0 | 0.351 | 917.0 | -22.4 | |||
702 | 2003-12-25T22:30 | 613 | 1810.27 | no break | 3.100 | 3.100 | 149.0 | ||||||||
702 | 2003-12-25T22:30 | 289.0 | 2 | 890 | 18.00 | 1811.43 | 3.100 | 3.100 | 149.0 | ||||||
703 | 2003-12-26T01:16 | 574 | 1813.02 | 3.200 | 3.200 | 129.0 | |||||||||
703 | 2003-12-26T01:16 | 265.0 | 2 | 865 | 15.00 | 1814.19 | 3.200 | 3.200 | 129.0 | ||||||
704 | 2003-12-26T03:55 | 900 | 1816.44 | no break | 3.100 | 3.100 | 132.0 | ||||||||
704 | 2003-12-26T03:55 | 219.0 | 1 | 507 | 14.00 | 1816.44 | 3.100 | 3.100 | 132.0 | ||||||
705 | 2003-12-26T05:53 | 236.0 | 1 | 692 | 14.00 | 1818.78 | 3.150 | 3.150 | 136.0 | ||||||
706 | 2003-12-26T07:56 | 227.0 | 1 | 637 | 14.00 | 1821.16 | 2.600 | 2.800 | 141.0 | ||||||
707 | 2003-12-26T09:55 | 900 | 1822.05 | no break | 3.000 | 3.000 | 144.0 | 0.474 | 919.5 | -28.0 | |||||
707 | 2003-12-26T09:55 | 2 | 531 | 7.00 | 1822.05 | 3.000 | 3.000 | 144.0 | 0.474 | 919.5 | -28.0 | ||||
707 | 2003-12-26T09:55 | 110.0 | 2 | 567 | 7.00 | 1822.05 | 3.000 | 3.000 | 144.0 | 0.474 | 919.5 | -28.0 | |||
708 | 2003-12-26T12:05 | 165.5 | 1 | 555 | 9.00 | 1823.90 | 2.900 | 2.900 | 126.0 | ||||||
709 | 2003-12-26T15:12 | 900 | 1826.20 | no break | 3.000 | 3.000 | 116.0 | ||||||||
709 | 2003-12-26T15:12 | 234.0 | 1 | 760 | 13.00 | 1826.20 | 3.000 | 3.000 | 116.0 | ||||||
710 | 2003-12-26T17:17 | 255.5 | 1 | 583 | 15.00 | 1828.88 | 2.400 | 2.400 | 120.0 | ||||||
711 | 2003-12-26T19:33 | 219.0 | 1 | 867 | 13.00 | 1830.94 | 2.300 | 2.300 | 125.0 | ||||||
712 | 2003-12-26T21:59 | 236.0 | 1 | 889 | 14.00 | 1833.34 | 2.200 | 2.200 | 128.0 | ||||||
713 | 2003-12-26T23:45 | 180.0 | 1 | 906 | 11.00 | 1835.06 | persistent antitorque | 3.200 | 3.200 | 133.0 | |||||
714 | 2003-12-27T01:45 | 179.0 | 1 | 794 | 10.00 | 1837.00 | persistent antitorque | 3.050 | 3.050 | 137.0 | |||||
715 | 2003-12-27T03:11 | 770 | 1838.73 | persistent antitorque | 3.250 | 3.250 | 140.0 | ||||||||
715 | 2003-12-27T03:11 | 296.0 | 2 | 696 | 17.00 | 1839.82 | persistent antitorque | 3.250 | 3.250 | 140.0 | |||||
716 | 2003-12-27T05:37 | 619 | 1841.00 | persistent antitorque,no break | 3.100 | 3.100 | 145.0 | ||||||||
716 | 2003-12-27T05:37 | 253.0 | 2 | 781 | 15.00 | 1842.36 | persistent antitorque | 3.100 | 3.100 | 145.0 | |||||
717 | 2003-12-27T07:47 | 249.0 | 1 | 681 | 14.00 | 1844.89 | 3.200 | 3.200 | 151.0 | ||||||
718 | 2003-12-27T09:55 | 672 | 1846.32 | antitorque, no break | 3.100 | 3.100 | 154.0 | 0.442 | 919.0 | -28.0 | |||||
718 | 2003-12-27T09:55 | 241.0 | 2 | 671 | 13.50 | 1847.32 | Changed drill head, alignment 0.9, shoes 2*4 mm,1*6 mm | 3.100 | 3.100 | 154.0 | 0.442 | 919.0 | -28.0 | ||
719 | 2003-12-27T12:15 | 207.0 | 1 | 752 | 12.00 | 1849.38 | 3.800 | 3.800 | 126.0 | ||||||
720 | 2003-12-27T14:08 | 193.0 | 1 | 634 | 12.00 | 1851.43 | 3.700 | 3.700 | 130.0 | ||||||
721 | 2003-12-27T16:29 | 139.0 | 1 | 910 | 9.50 | 1853.00 | Changed to Hans Tausen | 1.600 | 1.600 | 135.0 | |||||
FR34 | 2003-12-28T09:45 | 1854.47 | Filterrun | ||||||||||||
722 | 2003-12-28T13:18 | 131.0 | 1 | 903 | 8.00 | 1854.21 | Hans Tausen | 3.800 | 3.800 | 139.0 | |||||
723 | 2003-12-28T15:12 | 125.0 | 1 | 665 | 7.00 | 1855.42 | Hans Tausen | 3.900 | 3.900 | 140.0 | |||||
724 | 2003-12-28T17:00 | 136.0 | 2 | 807 | 8.00 | 1856.75 | Hans Tausen | 3.600 | 3.600 | 143.0 | 0.573 | 915.0 | -23.0 | ||
725 | 2003-12-28T19:05 | 900 | 1858.03 | Hans Tausen, no break | 4.000 | 4.000 | 116.0 | ||||||||
725 | 2003-12-28T19:05 | 900 | 1858.03 | Hans Tausen, no break | 4.000 | 4.000 | 116.0 | ||||||||
725 | 2003-12-28T19:05 | 124.0 | 1 | 654 | 8.00 | 1858.03 | Hans Tausen | 4.000 | 4.000 | 116.0 | |||||
726 | 2003-12-28T21:30 | 900 | 1858.64 | change to normal size, drill head 1 | 3.000 | 3.000 | 109.0 | ||||||||
726 | 2003-12-28T21:30 | 765 | 1858.64 | change to normal size, drill head 1 | 3.000 | 3.000 | 109.0 | ||||||||
726 | 2003-12-28T21:30 | 146.5 | 2 | 696 | 8.00 | 1859.24 | change to normal size, drill head 1 | 3.000 | 3.000 | 109.0 | |||||
727 | 2003-12-28T23:20 | 882 | 1860.33 | 3.900 | 3.900 | 114.0 | |||||||||
727 | 2003-12-28T23:20 | 172.0 | 2 | 850 | 9.50 | 1860.91 | 3.900 | 3.900 | 114.0 | ||||||
728 | 2003-12-29T02:08 | 113.0 | 1 | 689 | 10.00 | 1862.58 | changed to Hans Tausen, persistent antitorque | 3.400 | 3.400 | 114.0 | |||||
729 | 2003-12-29T04:29 | 912 | 1863.81 | no core break | 3.500 | 3.500 | |||||||||
729 | 2003-12-29T04:29 | 116.0 | 1 | 729 | 7.00 | 1863.81 | 3.500 | 3.500 | |||||||
730 | 2003-12-29T06:40 | 907 | 1864.90 | 2.700 | 2.800 | 118.0 | |||||||||
730 | 2003-12-29T06:40 | 907 | 1864.90 | 2.700 | 2.800 | 118.0 | |||||||||
730 | 2003-12-29T06:40 | 908 | 1864.90 | 2.700 | 2.800 | 118.0 | |||||||||
730 | 2003-12-29T06:40 | 112.0 | 1 | 6.00 | 1864.90 | 2.700 | 2.800 | 118.0 | |||||||
731 | 2003-12-29T09:25 | 902 | 1865.48 | no break | 2.700 | 2.700 | 119.0 | ||||||||
731 | 2003-12-29T09:25 | 71.0 | 1 | 669 | 6.00 | 1865.48 | 2.700 | 2.700 | 119.0 | ||||||
732 | 2003-12-29T22:04 | 53.0 | 1 | 528 | 4.00 | 1865.16 | changed to normal drill, damage on the cutter | 2.650 | 2.750 | 122.0 | |||||
733 | 2003-12-29T23:48 | 969 | 1867.69 | 2.950 | 2.950 | 127.0 | |||||||||
733 | 2003-12-29T23:48 | 202.0 | 1 | 656 | 14.50 | 1867.69 | 2.950 | 2.950 | 127.0 | ||||||
734 | 2003-12-30T01:25 | 191.0 | 1 | 847 | 14.00 | 1869.77 | 2.800 | 2.800 | 133.0 | ||||||
735 | 2003-12-30T02:57 | 235.0 | 1 | 916 | 13.00 | 1872.05 | 2.750 | 2.750 | 137.0 | ||||||
736 | 2003-12-30T04:29 | 218.0 | 1 | 579 | 13.00 | 1874.34 | 2.180 | 2.180 | 142.0 | ||||||
737 | 2003-12-30T06:03 | 272.0 | 1 | 567 | 1877.08 | 2.850 | 2.850 | 147.0 | |||||||
738 | 2003-12-30T07:40 | 1877.08 | Drilled pulled up due to short cut | 152.0 | 0.435 | 917.0 | -26.1 | ||||||||
739 | 2003-12-30T11:10 | 900 | 1879.34 | 2.800 | 2.800 | 119.0 | |||||||||
739 | 2003-12-30T11:10 | 262.0 | 1 | 863 | 15.00 | 1879.34 | 2.800 | 2.800 | 119.0 | ||||||
740 | 2003-12-30T12:53 | 245.0 | 1 | 782 | 15.00 | 1881.71 | 2.800 | 2.800 | |||||||
741 | 2003-12-30T14:53 | 276.0 | 1 | 905 | 15.00 | 1884.44 | 2.900 | 2.900 | 129.0 | ||||||
742 | 2003-12-30T16:43 | 226.0 | 1 | 603 | 13.00 | 1886.71 | 2.700 | 2.700 | 134.0 | ||||||
743 | 2003-12-30T18:25 | 278.0 | 1 | 869 | 16.00 | 1889.61 | 2.800 | 2.800 | 138.0 | ||||||
744 | 2003-12-30T20:09 | 230.5 | 1 | 824 | 13.00 | 1891.91 | 2.800 | 2.800 | 143.0 | ||||||
745 | 2003-12-30T21:45 | 182.0 | 1 | 717 | 10.00 | 1893.86 | 2.500 | 2.700 | 149.0 | ||||||
746 | 2003-12-30T23:36 | 269.0 | 2 | 681 | 18.00 | 1896.48 | 2.650 | 2.650 | 155.0 | ||||||
747 | 2003-12-31T03:43 | 248.0 | 1 | 759 | 20.00 | 1898.95 | 2.750 | 2.750 | 160.0 | ||||||
748 | 2003-12-31T05:37 | 250.0 | 1 | 772 | 14.00 | 1901.64 | changed spring on one cutter | 2.800 | 2.800 | 166.0 | 0.406 | 917.0 | -25.1 | ||
749 | 2003-12-31T07:50 | 232.0 | 1 | 901 | 14.00 | 1903.96 | 2.800 | 2.800 | 136.0 | ||||||
750 | 2003-12-31T09:45 | 91.0 | 1 | 890 | 8.50 | 1905.22 | removed burr from one cutter | 2.700 | 2.700 | 139.0 | |||||
751 | 2003-12-31T11:38 | 903 | 1905.56 | no core break, no cutting at 308 due to a spring in the hole? | 2.600 | 2.750 | 142.0 | ||||||||
751 | 2003-12-31T11:38 | 331.0 | 2 | 899 | 16.00 | 1907.82 | no core break, no cutting at 308 due to a spring in the hole? | 2.600 | 2.750 | 142.0 | |||||
752 | 2003-12-31T13:46 | 260.0 | 1 | 850 | 14.50 | 1910.64 | 2.600 | 2.600 | 148.0 | ||||||
753 | 2003-12-31T15:32 | 242.0 | 1 | 579 | 13.00 | 1913.17 | 2.700 | 2.700 | 154.0 | ||||||
754 | 2003-12-31T17:21 | 258.0 | 1 | 832 | 1915.72 | 2.500 | 2.500 | 158.0 | 0.444 | 918.0 | -25.2 | ||||
755 | 2004-01-01T10:35 | 89.0 | 1 | 712 | 6.50 | 1916.82 | change to Hans Tausen | 1.700 | 1.700 | 128.0 | |||||
756 | 2004-01-01T12:55 | 112.5 | 1 | 641 | 6.00 | 1918.11 | HT | 1.800 | 1.800 | 130.0 | |||||
757 | 2004-01-01T15:03 | 121.5 | 2 | 637 | 5.50 | 1919.20 | HT | 1.900 | 1.900 | 134.0 | |||||
758 | 2004-01-01T17:01 | 641 | 1919.49 | HT | 1.500 | 1.500 | 135.0 | ||||||||
758 | 2004-01-01T17:01 | 85.0 | 2 | 900 | 5.00 | 1919.49 | HT | 1.500 | 1.500 | 135.0 | |||||
759 | 2004-01-01T19:10 | 135.0 | 1 | 574 | 6.00 | 1921.28 | HT | 1.700 | 1.700 | 137.0 | |||||
760 | 2004-01-01T21:29 | 1041 | 1922.36 | HT, no break | 2.200 | 2.200 | 143.0 | ||||||||
760 | 2004-01-01T21:29 | 140.5 | 2 | 946 | 10.00 | 1922.36 | HT | 2.200 | 2.200 | 143.0 | |||||
761 | 2004-01-02T00:09 | 903 | 1922.97 | HT, no break | 1.800 | 1.800 | 140.0 | ||||||||
761 | 2004-01-02T00:09 | 44.0 | 1 | 651 | 4.00 | 1922.97 | HT, one cutter damaged by the spring in the hole | 1.800 | 1.800 | 140.0 | |||||
762 | 2004-01-02T02:20 | 78.0 | 1 | 667 | 5.00 | 1923.81 | HT, cutter damaged | 1.650 | 1.650 | 151.0 | |||||
763 | 2004-01-02T04:30 | 94.0 | 1 | 812 | 5.50 | 1924.77 | HT | 2.000 | 2.000 | 154.0 | 0.506 | 915.0 | -23.5 | ||
764 | 2004-01-02T06:55 | 978 | 1925.61 | HT, no break | 1.800 | 1.800 | 119.0 | ||||||||
764 | 2004-01-02T06:55 | 1030 | 1925.61 | HT, no break | 1.800 | 1.800 | 119.0 | ||||||||
764 | 2004-01-02T06:55 | 112.0 | 1 | 623 | 6.00 | 1925.61 | HT | 1.800 | 1.800 | 119.0 | |||||
FR35 | 2004-01-02T09:15 | 1925.61 | 0.000 | 0.000 | 0.0 | ||||||||||
FR36 | 2004-01-02T11:50 | 1925.61 | 0.000 | 0.000 | 0.0 | ||||||||||
FR37 | 2004-01-02T14:40 | 1925.61 | 0.000 | 0.000 | 0.0 | ||||||||||
765 | 2004-01-02T18:12 | 624 | 1924.56 | HT,changed to drill head H2, new cutters | 2.200 | 2.200 | 123.0 | ||||||||
765 | 2004-01-02T18:12 | 82.0 | 2 | 831 | 6.00 | 1924.56 | HT,changed to drill head H2, new cutters | 2.200 | 2.200 | 123.0 | |||||
FR38 | 2004-01-02T22:04 | 1924.56 | HT with special hash to bring parts in the centre | 0.000 | 0.000 | 0.0 | |||||||||
766 | 2004-01-03T00:22 | 906 | 1927.70 | HT,no break | 2.600 | 2.600 | 127.0 | ||||||||
766 | 2004-01-03T00:22 | 105.0 | 1 | 606 | 6.00 | 1927.70 | HT | 2.600 | 2.600 | 127.0 | |||||
767 | 2004-01-03T03:30 | 101.0 | 1 | 612 | 7.00 | 1928.52 | changed to long drill, no clear cutting, 14cm chips on top | 1.200 | 1.200 | 129.0 | |||||
768 | 2004-01-03T06:45 | 905 | 1928.91 | changed back to HT | 3.200 | 3.200 | 132.0 | ||||||||
768 | 2004-01-03T06:45 | 678 | 1929.54 | changed back to HT | 3.200 | 3.200 | 132.0 | ||||||||
768 | 2004-01-03T06:45 | 129.0 | 3 | 789 | 8.00 | 1929.90 | changed back to HT | 3.200 | 3.200 | 132.0 | |||||
769 | 2004-01-03T09:19 | 542 | 1930.90 | HT | 3.000 | 3.000 | 132.0 | ||||||||
769 | 2004-01-03T09:19 | 619 | 1931.21 | HT | 3.000 | 3.000 | 132.0 | ||||||||
769 | 2004-01-03T09:19 | 118.0 | 3 | 705 | 7.00 | 1931.53 | HT | 3.000 | 3.000 | 132.0 | |||||
770 | 2004-01-03T11:34 | 515 | 1931.56 | HT | 3.400 | 3.400 | 139.0 | ||||||||
770 | 2004-01-03T11:34 | 82.0 | 2 | 906 | 5.00 | 1932.16 | HT | 3.400 | 3.400 | 139.0 | |||||
771 | 2004-01-03T13:48 | 24.0 | 1 | 545 | 3.00 | 1932.32 | HT | 3.200 | 3.200 | 140.0 | |||||
772 | 2004-01-03T15:49 | 605 | 1933.21 | HT | 3.000 | 3.000 | 141.0 | ||||||||
772 | 2004-01-03T15:49 | 145.5 | 2 | 906 | 6.00 | 1933.68 | HT | 3.000 | 3.000 | 141.0 | |||||
773 | 2004-01-03T22:17 | 834 | 1934.57 | Change to long drill, drill head H2 | 1.000 | 1.600 | 148.0 | ||||||||
773 | 2004-01-03T22:17 | 131.0 | 2 | 620 | 8.00 | 1934.61 | Change to long drill, drill head H2 | 1.000 | 1.600 | 148.0 | |||||
774 | 2004-01-04T13:43 | 7.0 | 1 | 748 | 6.00 | 1934.55 | 151.0 | 0.418 | 911.0 | -18.9 | |||||
775 | 2004-01-04T15:20 | 270.0 | 1 | 609 | 16.00 | 1937.20 | 2.100 | 2.200 | 152.0 | ||||||
776 | 2004-01-04T17:50 | 258.0 | 1 | 732 | 15.00 | 1940.08 | 2.300 | 2.200 | 126.0 | ||||||
777 | 2004-01-04T19:35 | 900 | 1942.16 | no break | 2.200 | 2.200 | 130.0 | ||||||||
777 | 2004-01-04T19:35 | 1063 | 1942.16 | no break | 2.200 | 2.200 | 130.0 | ||||||||
777 | 2004-01-04T19:35 | 197.0 | 1 | 1060 | 11.00 | 1942.16 | 2.200 | 2.200 | 130.0 | ||||||
778 | 2004-01-04T21:38 | 265.0 | 1 | 860 | 16.00 | 1944.86 | 2.100 | 2.100 | 134.0 | ||||||
779 | 2004-01-04T23:25 | 300.0 | 1 | 882 | 17.00 | 1947.84 | 2.100 | 2.100 | 129.0 | ||||||
780 | 2004-01-05T01:35 | 263.0 | 1 | 703 | 15.00 | 1950.42 | 2.600 | 2.600 | 145.0 | ||||||
781 | 2004-01-05T03:30 | 272.0 | 1 | 569 | 16.00 | 1953.27 | 2.550 | 2.550 | 150.0 | 0.441 | 915.0 | -23.0 | |||
782 | 2004-01-05T05:28 | 272.0 | 1 | 745 | 15.00 | 1956.07 | 2.700 | 2.700 | 121.0 | ||||||
783 | 2004-01-05T07:33 | 241.0 | 1 | 722 | 14.50 | 1958.33 | 2.800 | 2.900 | 126.0 | ||||||
784 | 2004-01-05T09:27 | 265.0 | 1 | 723 | 14.50 | 1961.00 | 2.700 | 2.800 | 132.0 | ||||||
785 | 2004-01-05T11:05 | 264.0 | 1 | 656 | 14.00 | 1963.65 | 2.800 | 2.900 | 138.0 | ||||||
786 | 2004-01-05T12:55 | 207.0 | 1 | 824 | 12.00 | 1965.76 | 2.600 | 2.700 | 142.0 | ||||||
787 | 2004-01-05T14:59 | 265.0 | 1 | 907 | 16.00 | 1968.44 | changed to drill head H3 (Rufli) | 2.600 | 2.600 | 146.0 | |||||
788 | 2004-01-05T16:45 | 236.0 | 1 | 677 | 11.50 | 1970.75 | 3.900 | 3.900 | 151.0 | ||||||
789 | 2004-01-05T18:46 | 235.0 | 1 | 834 | 14.00 | 1972.94 | 3.000 | 3.000 | 156.0 | 0.510 | 914.0 | -21.5 | |||
790 | 2004-01-05T20:40 | 277.0 | 1 | 897 | 15.00 | 1975.63 | 2.800 | 2.800 | 147.0 | ||||||
791 | 2004-01-05T22:35 | 244.0 | 1 | 903 | 14.50 | 1978.20 | 2.900 | 2.900 | 128.0 | ||||||
792 | 2004-01-06T00:43 | 256.0 | 1 | 908 | 16.00 | 1980.73 | 3.100 | 3.100 | 132.0 | ||||||
793 | 2004-01-06T03:05 | 280.0 | 1 | 903 | 17.00 | 1983.65 | 3.200 | 3.200 | 136.0 | ||||||
794 | 2004-01-06T05:18 | 283.0 | 1 | 910 | 16.50 | 1986.46 | 2.890 | 2.890 | 140.0 | ||||||
795 | 2004-01-06T07:18 | 271.0 | 1 | 798 | 15.00 | 1989.29 | 3.100 | 3.100 | 145.0 | ||||||
796 | 2004-01-06T09:16 | 262.0 | 1 | 795 | 15.00 | 1991.85 | 3.300 | 3.300 | 150.0 | ||||||
797 | 2004-01-06T11:07 | 903 | 1994.46 | no break | 3.100 | 3.100 | 154.0 | ||||||||
797 | 2004-01-06T11:07 | 260.0 | 1 | 675 | 15.00 | 1994.46 | 3.100 | 3.100 | 154.0 | ||||||
798 | 2004-01-06T13:20 | 1994.46 | Run aborted,broken incremental counter | 3.100 | 3.100 | 154.0 | 0.398 | 915.0 | -22.4 | ||||||
799 | 2004-01-06T21:25 | 270.0 | 1 | 899 | 15.00 | 1996.63 | 2.800 | 2.800 | 131.0 | ||||||
800 | 2004-01-06T23:18 | 253.0 | 1 | 903 | 15.00 | 1999.25 | 3.100 | 3.100 | 135.0 | ||||||
801 | 2004-01-07T01:17 | 170.0 | 1 | 553 | 10.00 | 2001.38 | 3.300 | 3.300 | 142.0 | ||||||
802 | 2004-01-07T03:32 | 7.0 | 1 | 777 | 2001.50 | persistent cutting problems, plastic found around the drillhead | 144.0 | ||||||||
803 | 2004-01-07T06:02 | 61.0 | 1 | 787 | 4.50 | 2002.30 | persistent cutting problems, plastic found around the drillhead | 2.400 | 2.400 | 145.0 | |||||
804 | 2004-01-07T08:17 | 270.0 | 1 | 582 | 15.00 | 2004.75 | 3.250 | 3.250 | 148.0 | ||||||
805 | 2004-01-07T10:09 | 209.0 | 1 | 609 | 12.00 | 2007.01 | 3.200 | 3.200 | 154.0 | ||||||
806 | 2004-01-07T12:31 | 231.0 | 1 | 683 | 13.00 | 2009.23 | 3.500 | 3.500 | 159.0 | 0.450 | 911.0 | -18.7 | |||
807 | 2004-01-07T14:20 | 268.0 | 1 | 676 | 15.00 | 2011.84 | 3.100 | 3.100 | 127.0 | ||||||
808 | 2004-01-07T16:15 | 285.5 | 1 | 666 | 16.00 | 2014.62 | 3.200 | 3.200 | 133.0 | ||||||
809 | 2004-01-07T18:13 | 900 | 2017.22 | no break | 3.200 | 3.200 | 137.0 | ||||||||
809 | 2004-01-07T18:13 | 241.0 | 1 | 424 | 13.00 | 2017.22 | 3.200 | 3.200 | 137.0 | ||||||
810 | 2004-01-07T20:12 | 174.0 | 1 | 627 | 10.00 | 2019.09 | 3.300 | 3.600 | 142.0 | ||||||
811 | 2004-01-07T22:10 | 900 | 2021.68 | 3.200 | 3.200 | 146.0 | |||||||||
811 | 2004-01-07T22:10 | 274.0 | 1 | 530 | 14.00 | 2021.68 | 3.200 | 3.200 | 146.0 | 0.533 | 915.0 | -23.0 | |||
812 | 2004-01-08T00:01 | 220.0 | 1 | 768 | 14.00 | 2024.16 | 3.300 | 3.300 | |||||||
813 | 2004-01-08T02:13 | 303.0 | 1 | 826 | 17.00 | 2027.04 | 2.600 | 2.600 | 116.0 | ||||||
814 | 2004-01-08T04:10 | 305.0 | 2 | 683 | 16.00 | 2030.16 | 2.600 | 2.600 | 122.0 | ||||||
815 | 2004-01-08T06:17 | 250.0 | 1 | 687 | 15.00 | 2032.66 | 2.100 | 2.100 | 126.0 | ||||||
816 | 2004-01-08T08:28 | 243.0 | 1 | 734 | 13.50 | 2035.04 | 2.300 | 2.300 | 133.0 | ||||||
817 | 2004-01-08T10:26 | 273.5 | 1 | 663 | 14.50 | 2037.74 | 2.100 | 2.100 | 136.0 | ||||||
818 | 2004-01-08T12:20 | 278.0 | 1 | 593 | 15.00 | 2040.44 | 2.100 | 2.100 | 140.0 | ||||||
819 | 2004-01-08T14:02 | 911 | 2043.33 | no break | 2.100 | 2.100 | 145.0 | ||||||||
819 | 2004-01-08T14:02 | 282.0 | 1 | 472 | 16.00 | 2043.33 | Tower motor broken. | 2.100 | 2.100 | 145.0 | |||||
820 | 2004-01-08T20:00 | 303.0 | 1 | 846 | 18.00 | 2045.93 | 2.500 | 2.500 | 105.0 | 0.533 | 915.0 | -23.0 | |||
821 | 2004-01-08T22:10 | 67.0 | 1 | 911 | 5.50 | 2047.23 | 2.400 | 2.400 | 111.0 | ||||||
822 | 2004-01-09T00:10 | 272.0 | 1 | 797 | 15.00 | 2049.82 | persistent cutting problems | 2.200 | 2.200 | 113.0 | |||||
823 | 2004-01-09T03:00 | 298.0 | 1 | 762 | 16.00 | 2052.88 | 2.350 | 2.350 | 123.0 | ||||||
824 | 2004-01-09T05:35 | 232.0 | 1 | 676 | 12.00 | 2055.26 | 2.250 | 2.250 | 127.0 | ||||||
825 | 2004-01-09T08:01 | 1 | 901 | 2057.07 | no break | 2.500 | 2.500 | 132.0 | |||||||
825 | 2004-01-09T08:01 | 1043 | 2057.07 | 2.500 | 2.500 | 132.0 | |||||||||
825 | 2004-01-09T08:01 | 207.0 | 1 | 900 | 12.00 | 2057.07 | 2.500 | 2.500 | 132.0 | ||||||
826 | 2004-01-09T10:50 | 209.0 | 1 | 637 | 12.00 | 2059.05 | 2.700 | 2.800 | 137.0 | ||||||
827 | 2004-01-09T12:36 | 232.0 | 1 | 693 | 14.00 | 2061.59 | 2.600 | 2.600 | 141.0 | 0.421 | 917.0 | -25.5 | |||
828 | 2004-01-09T14:30 | 249.0 | 1 | 806 | 14.00 | 2063.88 | all cutters and catchers sharpened | 2.800 | 2.800 | 120.0 | |||||
829 | 2004-01-09T16:30 | 238.5 | 1 | 634 | 14.00 | 2066.44 | 2.900 | 2.900 | 120.0 | ||||||
830 | 2004-01-09T18:45 | 254.0 | 1 | 746 | 15.00 | 2068.81 | 2.900 | 2.900 | 125.0 | ||||||
831 | 2004-01-09T20:50 | 253.0 | 1 | 688 | 14.00 | 2071.54 | 2.900 | 2.900 | 130.0 | ||||||
832 | 2004-01-09T22:35 | 272.0 | 1 | 765 | 18.50 | 2073.85 | 2.700 | 2.700 | 133.0 | ||||||
833 | 2004-01-10T00:30 | 256.0 | 2 | 647 | 14.00 | 2076.86 | 2.600 | 2.600 | 137.0 | ||||||
834 | 2004-01-10T02:20 | 257.0 | 1 | 626 | 14.50 | 2079.65 | 2.700 | 2.700 | 142.0 | 0.462 | 916.0 | -24.4 | |||
835 | 2004-01-10T04:14 | 280.0 | 1 | 555 | 16.00 | 2082.38 | 2.600 | 2.600 | 148.0 | ||||||
836 | 2004-01-10T06:07 | 271.0 | 1 | 685 | 14.50 | 2085.07 | 2.600 | 2.600 | 118.0 | ||||||
837 | 2004-01-10T07:51 | 261.0 | 1 | 643 | 15.50 | 2087.62 | 2.700 | 2.700 | 122.0 | ||||||
838 | 2004-01-10T09:56 | 288.0 | 1 | 634 | 16.00 | 2090.36 | 2.800 | 2.800 | 126.0 | ||||||
839 | 2004-01-10T11:52 | 900 | 2093.09 | no break | 2.800 | 2.800 | 132.0 | ||||||||
839 | 2004-01-10T11:52 | 264.0 | 1 | 680 | 16.00 | 2093.09 | 2.800 | 2.800 | 132.0 | ||||||
840 | 2004-01-10T13:55 | 935 | 2095.13 | no break | 2.800 | 2.800 | 137.0 | ||||||||
840 | 2004-01-10T13:55 | 262.0 | 1 | 565 | 15.00 | 2095.13 | 2.800 | 2.800 | 137.0 | ||||||
841 | 2004-01-10T15:45 | 277.0 | 1 | 899 | 15.00 | 2098.38 | 2.700 | 2.700 | 142.0 | ||||||
842 | 2004-01-10T17:40 | 265.0 | 1 | 649 | 15.00 | 2101.05 | 2.600 | 2.600 | 143.0 | 0.436 | 917.0 | -25.0 | |||
FR38 | 2004-01-11T02:30 | 2101.61 | 1-2kg slush | ||||||||||||
843 | 2004-01-11T13:05 | 234.0 | 1 | 598 | 16.00 | 2103.20 | change shaft | 2.800 | 2.800 | ||||||
844 | 2004-01-11T15:00 | 170.0 | 1 | 691 | 9.00 | 2105.10 | 2.700 | 2.700 | 124.0 | ||||||
845 | 2004-01-11T16:45 | 2 | 623 | 2106.57 | due to high motor current early break | 2.800 | 2.800 | 127.0 | |||||||
845 | 2004-01-11T16:45 | 229.0 | 2 | 954 | 14.00 | 2106.78 | 2.800 | 2.800 | 127.0 | ||||||
846 | 2004-01-11T18:55 | 313.0 | 1 | 642 | 17.00 | 2110.10 | 2.500 | 2.500 | 134.0 | ||||||
847 | 2004-01-11T21:22 | 280.0 | 2 | 842 | 16.00 | 2113.41 | 2.700 | 2.700 | 136.0 | ||||||
848 | 2004-01-11T23:28 | 265.0 | 1 | 864 | 15.50 | 2115.87 | 2.600 | 2.600 | 142.0 | ||||||
849 | 2004-01-12T01:50 | 278.0 | 1 | 1049 | 16.00 | 2118.74 | 2.600 | 2.600 | 147.0 | 0.270 | 917.0 | -25.0 | |||
850 | 2004-01-12T04:09 | 900 | 2121.46 | no break | 2.500 | 2.500 | 142.0 | ||||||||
850 | 2004-01-12T04:09 | 262.0 | 1 | 637 | 15.00 | 2121.46 | 2.500 | 2.500 | 142.0 | ||||||
851 | 2004-01-12T07:06 | 905 | 2123.80 | no break | 3.000 | 3.000 | 130.0 | ||||||||
851 | 2004-01-12T07:06 | 251.0 | 1 | 620 | 16.00 | 2123.80 | 3.000 | 3.000 | 130.0 | ||||||
852 | 2004-01-12T09:20 | 253.0 | 1 | 652 | 14.00 | 2126.54 | 2.850 | 2.850 | 135.0 | ||||||
853 | 2004-01-12T11:22 | 212.0 | 1 | 617 | 13.00 | 2128.63 | 3.400 | 3.400 | 139.0 | ||||||
854 | 2004-01-12T13:45 | 217.0 | 1 | 690 | 12.00 | 2130.72 | 3.300 | 3.600 | 145.0 | ||||||
855 | 2004-01-12T15:45 | 213.0 | 1 | 694 | 14.00 | 2133.15 | 2.600 | 2.800 | 151.0 | 0.418 | 917.0 | -24.0 | |||
856 | 2004-01-12T18:05 | 950 | 2135.36 | no break | 2.400 | 2.600 | 151.0 | ||||||||
856 | 2004-01-12T18:05 | 1044 | 2135.36 | no break | 2.400 | 2.600 | 151.0 | ||||||||
856 | 2004-01-12T18:05 | 1081 | 2135.36 | no break | 2.400 | 2.600 | 151.0 | ||||||||
856 | 2004-01-12T18:05 | 253.0 | 1 | 1208 | 14.50 | 2135.36 | bottom break,persistent antitorque,both legs of one spring gone, magnetic replaced | 2.400 | 2.600 | 151.0 | |||||
857 | 2004-01-12T20:27 | 265.0 | 1 | 855 | 16.00 | 2137.88 | 2.900 | 3.000 | 127.0 | ||||||
858 | 2004-01-12T22:35 | 2 | 625 | 2139.18 | break and down again | 2.000 | 2.100 | 132.0 | |||||||
858 | 2004-01-12T22:35 | 210.0 | 2 | 807 | 13.00 | 2140.08 | 2.000 | 2.100 | 132.0 | ||||||
859 | 2004-01-13T01:10 | 231.5 | 1 | 695 | 13.00 | 2142.57 | 2.700 | 2.700 | 138.0 | ||||||
860 | 2004-01-13T03:12 | 900 | 2144.61 | no break | 2.500 | 2.500 | 142.0 | ||||||||
860 | 2004-01-13T03:12 | 900 | 2144.61 | no break | 2.500 | 2.500 | 142.0 | ||||||||
860 | 2004-01-13T03:12 | 1080 | 2144.61 | no break | 2.500 | 2.500 | 142.0 | ||||||||
860 | 2004-01-13T03:12 | 205.0 | 1 | 1060 | 12.50 | 2144.61 | no break | 2.500 | 2.500 | 142.0 | |||||
861 | 2004-01-13T06:23 | 2 | 796 | 2145.33 | break because of cutting problems | 1.700 | 2.400 | 145.0 | |||||||
861 | 2004-01-13T06:23 | 79.0 | 2 | 564 | 5.00 | 2145.33 | 1.700 | 2.400 | 145.0 | ||||||
862 | 2004-01-13T08:28 | 182.0 | 1 | 968 | 11.00 | 2147.31 | 1.800 | 2.000 | 150.0 | 0.460 | 916.0 | -24.0 | |||
FR39 | 2004-01-13T10:45 | 2147.27 | changed to drill head H2 | 133.0 | |||||||||||
863 | 2004-01-13T13:32 | 205.0 | 1 | 782 | 13.00 | 2148.94 | 2.600 | 2.800 | 124.0 | ||||||
864 | 2004-01-13T15:50 | 277.0 | 1 | 1005 | 16.00 | 2151.90 | 2.800 | 2.800 | 126.0 | ||||||
865 | 2004-01-13T17:55 | 260.0 | 1 | 603 | 15.50 | 2154.58 | 2.800 | 2.800 | 129.0 | ||||||
866 | 2004-01-13T19:55 | 266.0 | 1 | 823 | 16.00 | 2157.10 | 2.800 | 2.800 | 136.0 | ||||||
867 | 2004-01-13T21:45 | 266.5 | 1 | 956 | 16.00 | 2159.92 | 2.700 | 2.700 | 139.0 | ||||||
868 | 2004-01-13T23:49 | 229.5 | 1 | 577 | 13.00 | 2162.41 | 2.500 | 2.500 | 146.0 | ||||||
869 | 2004-01-14T02:22 | 274.0 | 1 | 1061 | 16.00 | 2164.86 | 2.500 | 2.500 | 150.0 | 0.390 | 917.5 | -26.0 | |||
870 | 2004-01-14T04:33 | 255.0 | 1 | 620 | 14.50 | 2167.60 | 2.600 | 2.600 | 126.0 | ||||||
871 | 2004-01-14T06:44 | 173.0 | 1 | 951 | 12.00 | 2169.24 | 2.700 | 2.700 | 131.0 | ||||||
872 | 2004-01-14T08:36 | 238.0 | 1 | 656 | 15.00 | 2171.52 | 2.900 | 2.900 | 132.0 | ||||||
873 | 2004-01-14T10:55 | 228.0 | 1 | 751 | 15.00 | 2174.44 | 3.000 | 3.000 | 139.0 | ||||||
874 | 2004-01-14T12:55 | 213.0 | 2 | 639 | 10.00 | 2175.96 | 2.400 | 2.500 | 146.0 | ||||||
875 | 2004-01-14T15:00 | 274.0 | 1 | 728 | 14.00 | 2178.84 | 2.400 | 2.400 | 150.0 | 0.428 | 916.0 | -25.0 | |||
876 | 2004-01-14T17:10 | 3 | 607 | 15.00 | 2181.31 | break due to cutting problems | 2.300 | 2.300 | 122.0 | ||||||
876 | 2004-01-14T17:10 | 262.0 | 3 | 943 | 15.00 | 2181.31 | 2.300 | 2.300 | 122.0 | ||||||
877 | 2004-01-14T19:40 | 246.0 | 1 | 631 | 14.00 | 2183.70 | 2.500 | 2.500 | 126.0 | ||||||
878 | 2004-01-14T21:25 | 268.0 | 1 | 659 | 15.00 | 2186.61 | 2.000 | 2.100 | 130.0 | ||||||
879 | 2004-01-14T23:32 | 266.0 | 1 | 686 | 14.50 | 2189.36 | 2.100 | 2.100 | 136.0 | ||||||
880 | 2004-01-15T01:44 | 272.0 | 1 | 611 | 15.50 | 2192.11 | changed drill head H1 | 2.100 | 2.100 | 141.0 | 0.434 | 918.6 | -27.0 | ||
881 | 2004-01-15T04:04 | 279.0 | 1 | 642 | 15.50 | 2194.81 | 3.700 | 3.700 | 145.0 | ||||||
882 | 2004-01-15T06:29 | 272.0 | 1 | 712 | 15.00 | 2197.57 | 3.000 | 3.000 | 117.0 | ||||||
883 | 2004-01-15T08:35 | 248.0 | 1 | 665 | 14.00 | 2200.04 | 2.700 | 2.700 | 119.0 | ||||||
884 | 2004-01-15T10:40 | 276.0 | 4 | 619 | 16.00 | 2202.72 | 2.650 | 2.650 | 126.0 | ||||||
885 | 2004-01-15T12:50 | 228.0 | 1 | 637 | 13.00 | 2205.19 | 2.700 | 2.700 | 131.0 | ||||||
886 | 2004-01-15T14:59 | 277.5 | 1 | 682 | 15.00 | 2207.79 | 2.300 | 2.600 | 136.0 | ||||||
887 | 2004-01-15T17:00 | 261.0 | 1 | 881 | 15.00 | 2210.48 | 2.600 | 2.600 | 141.0 | ||||||
888 | 2004-01-15T18:50 | 286.0 | 1 | 778 | 16.00 | 2213.26 | 2.100 | 2.100 | 142.0 | 0.499 | 912.0 | -20.0 | |||
889 | 2004-01-15T21:01 | 273.0 | 1 | 924 | 16.00 | 2215.97 | 1.900 | 1.900 | 115.0 | ||||||
890 | 2004-01-15T23:02 | 276.0 | 1 | 704 | 15.00 | 2218.74 | 2.400 | 2.400 | 121.0 | ||||||
891 | 2004-01-16T01:08 | 278.0 | 1 | 674 | 15.00 | 2221.53 | 2.900 | 2.900 | 125.0 | ||||||
892 | 2004-01-16T03:18 | 227.0 | 1 | 671 | 13.00 | 2223.69 | 3.400 | 3.400 | 129.0 | ||||||
893 | 2004-01-16T05:21 | 255.0 | 1 | 821 | 14.00 | 2226.48 | 3.400 | 3.400 | 135.0 | ||||||
894 | 2004-01-16T07:26 | 272.0 | 1 | 699 | 17.00 | 2229.14 | 3.200 | 3.400 | 140.0 | ||||||
895 | 2004-01-16T09:30 | 261.0 | 1 | 920 | 14.00 | 2231.91 | 3.100 | 3.100 | 145.0 | ||||||
896 | 2004-01-16T11:20 | 258.0 | 1 | 782 | 15.00 | 2234.48 | 3.100 | 3.100 | 150.0 | ||||||
897 | 2004-01-16T13:20 | 275.0 | 1 | 728 | 16.00 | 2237.21 | 2.900 | 2.900 | 156.0 | 0.375 | 917.0 | -25.0 | |||
898 | 2004-01-16T15:23 | 248.0 | 1 | 627 | 12.00 | 2239.80 | 2.900 | 2.900 | 160.0 | ||||||
899 | 2004-01-16T17:14 | 236.0 | 1 | 759 | 13.00 | 2242.01 | 2.900 | 2.900 | 130.0 | ||||||
900 | 2004-01-16T19:36 | 265.0 | 1 | 748 | 15.00 | 2244.61 | 3.000 | 3.000 | 140.0 | ||||||
901 | 2004-01-16T21:35 | 247.0 | 1 | 613 | 14.00 | 2247.26 | 2.900 | 2.900 | 146.0 | ||||||
902 | 2004-01-16T23:33 | 259.0 | 1 | 969 | 14.00 | 2249.90 | 3.000 | 3.000 | 151.0 | 0.428 | 917.0 | -26.0 | |||
903 | 2004-01-17T02:18 | 201.0 | 1 | 1042 | 12.00 | 2251.64 | 3.400 | 3.400 | 158.0 | ||||||
904 | 2004-01-17T04:35 | 123.0 | 1 | 778 | 7.00 | 2253.16 | 3.100 | 3.100 | 128.0 | ||||||
905 | 2004-01-17T06:42 | 150.0 | 1 | 682 | 9.00 | 2254.54 | New Drill Head | 3.100 | 3.100 | 133.0 | |||||
906 | 2004-01-17T08:40 | 0 | 2254.54 | Short Cut in electronics, spring released | |||||||||||
907 | 2004-01-17T11:26 | 132.0 | 1 | 1039 | 8.00 | 2255.83 | 3.500 | 3.500 | 135.0 | ||||||
908 | 2004-01-17T13:31 | 163.5 | 1 | 664 | 8.00 | 2257.40 | cutting problems, new inclinometer settings | 2.300 | 2.400 | 139.0 | |||||
909 | 2004-01-17T15:39 | 173.0 | 1 | 693 | 10.00 | 2259.07 | cutting problems due to no voltage in the drill | 2.400 | 2.400 | 145.0 | |||||
910 | 2004-01-18T13:06 | 290.0 | 1 | 687 | 17.00 | 2261.89 | 2.500 | 2.500 | 148.0 | ||||||
911 | 2004-01-18T15:15 | 246.0 | 1 | 710 | 13.00 | 2264.52 | 2.700 | 2.700 | 154.0 | 0.508 | 917.0 | -25.0 | |||
912 | 2004-01-18T17:08 | 230.0 | 1 | 1055 | 13.50 | 2266.91 | 2.300 | 2.300 | 143.0 | ||||||
913 | 2004-01-18T20:00 | 142.0 | 2 | 1085 | 8.00 | 2267.73 | 1.000 | 1.900 | 124.0 | ||||||
914 | 2004-01-18T22:13 | 196.0 | 1 | 721 | 11.00 | 2270.26 | 2.400 | 2.900 | 126.0 | ||||||
915 | 2004-01-19T00:26 | 212.0 | 1 | 715 | 12.00 | 2272.29 | changed shaft | 2.750 | 2.750 | 131.0 | |||||
916 | 2004-01-19T03:03 | 247.0 | 1 | 1124 | 14.00 | 2274.86 | 2.400 | 2.700 | 135.0 | ||||||
917 | 2004-01-19T05:23 | 277.0 | 1 | 1065 | 15.00 | 2277.63 | 2.700 | 2.700 | 140.0 | ||||||
918 | 2004-01-19T07:52 | 270.0 | 1 | 958 | 16.00 | 2280.63 | 2.600 | 2.600 | 146.0 | 0.480 | 915.0 | -23.5 | |||
919 | 2004-01-19T10:00 | 199.0 | 1 | 646 | 13.00 | 2282.49 | 2.650 | 2.650 | 125.0 | ||||||
920 | 2004-01-19T11:55 | 274.0 | 1 | 1109 | 16.00 | 2285.06 | 2.700 | 2.700 | 119.0 | ||||||
921 | 2004-01-19T14:08 | 259.0 | 1 | 1036 | 15.00 | 2287.79 | 2.800 | 2.800 | 124.0 | ||||||
922 | 2004-01-19T16:13 | 289.0 | 1 | 599 | 16.00 | 2290.52 | 2.650 | 2.800 | 128.0 | ||||||
923 | 2004-01-19T18:20 | 243.0 | 1 | 994 | 14.00 | 2292.91 | 2.800 | 2.800 | 134.0 | ||||||
924 | 2004-01-19T20:22 | 279.0 | 1 | 882 | 16.00 | 2295.71 | 2.800 | 2.800 | 139.0 | ||||||
925 | 2004-01-19T22:59 | 278.0 | 1 | 712 | 14.00 | 2295.83 | 3.400 | 3.400 | |||||||
926 | 2004-01-20T01:46 | 278.0 | 1 | 956 | 16.00 | 2301.36 | 2.700 | 2.700 | 149.0 | 0.465 | 918.0 | -26.5 | |||
927 | 2004-01-20T03:59 | 283.0 | 1 | 843 | 15.50 | 2304.28 | 2.600 | 2.600 | 119.0 | ||||||
928 | 2004-01-20T06:15 | 217.0 | 1 | 1011 | 14.00 | 2306.41 | 2.200 | 2.200 | 123.0 | ||||||
929 | 2004-01-20T08:30 | 172.0 | 1 | 868 | 10.00 | 2308.05 | 2.700 | 2.700 | 129.0 | ||||||
930 | 2004-01-20T11:10 | 266.0 | 1 | 685 | 14.50 | 2311.01 | 2.900 | 3.000 | 132.0 | ||||||
931 | 2004-01-20T14:12 | 213.0 | 1 | 1037 | 12.00 | 2313.07 | 2.600 | 2.900 | 137.0 | ||||||
932 | 2004-01-20T16:50 | 256.0 | 1 | 1131 | 15.00 | 2315.18 | 2.300 | 2.400 | 144.0 | ||||||
933 | 2004-01-20T18:50 | 99.0 | 2 | 836 | 7.00 | 2316.47 | 1.000 | 2.600 | 148.0 | ||||||
934 | 2004-01-20T21:07 | 267.0 | 1 | 865 | 14.50 | 2319.19 | 2.300 | 2.500 | 120.0 | 0.421 | 917.0 | -25.7 | |||
935 | 2004-01-20T23:27 | 269.0 | 1 | 1017 | 15.00 | 2321.84 | 2.300 | 2.300 | 125.0 | ||||||
936 | 2004-01-21T01:45 | 41.0 | 1 | 1029 | 2322.31 | screw from valve was blocked, changed shaft | 2.500 | 2.500 | 128.0 | ||||||
937 | 2004-01-21T03:44 | 206.0 | 1 | 823 | 14.00 | 2324.36 | change to H1 | 2.300 | 2.300 | 134.0 | |||||
938 | 2004-01-21T06:03 | 173.0 | 1 | 788 | 11.00 | 2325.97 | 3.500 | 3.500 | 138.0 | ||||||
939 | 2004-01-21T08:08 | 233.0 | 1 | 880 | 14.00 | 2328.28 | 3.000 | 3.000 | 142.0 | ||||||
940 | 2004-01-21T10:25 | 254.0 | 1 | 875 | 14.00 | 2330.87 | 3.000 | 3.000 | 148.0 | 0.396 | 918.6 | -27.0 | |||
941 | 2004-01-21T12:20 | 260.0 | 1 | 667 | 15.00 | 2333.36 | 3.200 | 3.200 | 121.0 | ||||||
942 | 2004-01-21T14:23 | 271.0 | 1 | 679 | 14.50 | 2336.06 | 3.000 | 3.200 | 126.0 | ||||||
943 | 2004-01-21T16:30 | 259.0 | 1 | 770 | 15.00 | 2338.55 | 3.200 | 3.200 | 129.0 | ||||||
944 | 2004-01-21T18:28 | 249.0 | 1 | 709 | 14.00 | 2340.90 | 3.200 | 3.200 | 134.5 | ||||||
945 | 2004-01-21T20:34 | 1200 | 2343.43 | no break | 2.900 | 3.400 | 139.0 | ||||||||
945 | 2004-01-21T20:34 | 253.0 | 1 | 740 | 15.00 | 2343.43 | changed core catcher springs | 2.900 | 3.400 | 139.0 | |||||
946 | 2004-01-21T23:03 | 218.0 | 1 | 728 | 12.00 | 2345.83 | 3.200 | 3.200 | 145.0 | 0.486 | 917.0 | -25.5 | |||
947 | 2004-01-22T01:13 | 249.0 | 1 | 712 | 14.00 | 2348.43 | 3.400 | 3.400 | |||||||
948 | 2004-01-22T03:30 | 209.0 | 1 | 1335 | 11.00 | 2350.46 | 3.400 | 3.400 | 119.0 | ||||||
949 | 2004-01-22T06:14 | 136.0 | 1 | 1092 | 5.00 | 2352.11 | persistent communication problems | 2.400 | 2.600 | 123.0 | |||||
950 | 2004-01-22T08:15 | 2 | 954 | 2353.58 | break due to high current | persistent communication problems | 3.200 | 3.200 | 129.0 | ||||||
950 | 2004-01-22T08:15 | 179.0 | 2 | 1204 | 15.00 | 2353.96 | persistent communication problems | 3.200 | 3.200 | 129.0 | |||||
951 | 2004-01-22T11:38 | 200.0 | 1 | 1200 | 11.00 | 2355.62 | cleaned sliping/ changed to two new core catchers | persistent communication problems | 2.300 | 2.500 | 133.0 | ||||
952 | 2004-01-22T14:10 | 236.0 | 1 | 1137 | 14.00 | 2358.08 | persistent communication problems | 2.500 | 2.500 | 138.0 | |||||
953 | 2004-01-22T16:24 | 221.0 | 1 | 1035 | 13.00 | 2360.23 | changed to 3 core catchers | persistent communication problems | 2.400 | 2.700 | 144.0 | 0.530 | 916.0 | -25.5 | |
954 | 2004-01-22T19:36 | 166.0 | 1 | 834 | 9.00 | 2361.62 | persistent communication problems | 2.900 | 2.900 | 116.0 | |||||
955 | 2004-01-22T21:37 | 197.0 | 1 | 1061 | 11.00 | 2363.98 | persistent communication problems | 2.800 | 2.800 | 115.0 | |||||
956 | 2004-01-23T00:37 | 226.0 | 1 | 728 | 13.00 | 2365.95 | persistent communication problems | 2.750 | 2.750 | ||||||
957 | 2004-01-23T03:00 | 221.0 | 1 | 687 | 12.50 | 2368.49 | changed to drillhead H2 | persistent communication problems | 2.600 | 2.600 | 123.0 | ||||
958 | 2004-01-23T05:19 | 1 | 740 | 2369.66 | pull up due to closing window | persistent communication problems | 3.500 | 3.600 | 128.0 | ||||||
958 | 2004-01-23T05:19 | 135.0 | 1 | 983 | 7.00 | 2369.66 | tried to reduce pitch | persistent communication problems | 3.500 | 3.600 | 128.0 | ||||
959 | 2004-01-23T07:41 | 187.0 | 1 | 896 | 14.00 | 2371.68 | add shin under the cutter | persistent communication problems | 3.200 | 3.100 | 133.0 | ||||
960 | 2004-01-23T09:50 | 1 | 789 | 2372.57 | core break due to high current | persistent communication problems | 2.100 | 2.100 | 138.0 | ||||||
960 | 2004-01-23T09:50 | 163.0 | 1 | 766 | 10.00 | 2373.50 | changed to H1 | persistent communication problems | 2.100 | 2.100 | 138.0 | ||||
961 | 2004-01-23T12:20 | 135.0 | 1 | 686 | 11.00 | 2374.66 | persistent communication problems | 2.400 | 2.400 | 141.0 | |||||
962 | 2004-01-23T14:55 | 1 | 2374.66 | no rotation, pump stocked | persistent communication problems | 147.0 | 0.476 | 917.0 | -25.3 | ||||||
963 | 2004-01-23T16:45 | 220.0 | 1 | 955 | 14.00 | 2376.87 | persistent communication problems | 2.300 | 2.100 | 141.0 | |||||
964 | 2004-01-23T18:54 | 2 | 1200 | 2377.81 | no break, pull up due to high current | persistent communication problems | 1.800 | 1.800 | 120.0 | ||||||
964 | 2004-01-23T18:54 | 2 | 715 | 2377.81 | pull up due to high current | persistent communication problems | 1.800 | 1.800 | 120.0 | ||||||
964 | 2004-01-23T18:54 | 102.0 | 2 | 719 | 6.00 | 2377.70 | changed to H2 | persistent communication problems | 1.800 | 1.800 | 120.0 | ||||
965 | 2004-01-23T21:30 | 173.0 | 1 | 690 | 9.00 | 2379.66 | persistent communication problems | 2.100 | 2.100 | 124.0 | |||||
966 | 2004-01-23T23:39 | 111.0 | 1 | 686 | 9.00 | 2379.90 | stopped due to high current | persistent communication problems | 2.050 | 2.050 | 129.0 | ||||
967 | 2004-01-24T02:08 | 152.0 | 1 | 1201 | 8.00 | 2382.14 | persistent communication problems | 2.900 | 2.900 | 131.0 | |||||
968 | 2004-01-24T04:25 | 167.0 | 1 | 692 | 9.00 | 2384.16 | persistent communication problems | 2.800 | 2.800 | 136.0 | |||||
969 | 2004-01-24T06:29 | 181.0 | 1 | 1000 | 11.00 | 2385.73 | persistent communication problems | 2.600 | 2.700 | 140.0 | |||||
970 | 2004-01-24T08:35 | 195.0 | 1 | 698 | 11.00 | 2387.91 | persistent communication problems | 2.700 | 2.700 | 144.0 | 0.413 | 920.0 | -29.0 | ||
971 | 2004-01-24T10:40 | 188.0 | 1 | 947 | 11.00 | 2389.81 | persistent communication problems | 2.600 | 2.700 | 119.0 | |||||
972 | 2004-01-24T12:45 | 193.0 | 1 | 1197 | 10.00 | 2391.63 | persistent communication problems | 3.100 | 3.100 | 123.0 | |||||
973 | 2004-01-24T14:55 | 170.0 | 1 | 793 | 10.00 | 2393.31 | stopped due to high current | persistent communication problems | 3.200 | 3.200 | 128.0 | ||||
974 | 2004-01-24T17:00 | 163.0 | 1 | 998 | 10.00 | 2394.95 | stopped due to high current | persistent communication problems | 3.200 | 3.400 | 131.0 | ||||
FR40 | 2004-01-25T01:40 | 2394.95 | clean hole | 134.0 | |||||||||||
FR41 | 2004-01-25T03:00 | 2394.95 | logging,new brass tube,new contact in the antitorque section | ||||||||||||
975 | 2004-01-25T14:14 | 103.0 | 1 | 845 | 7.00 | 2395.44 | 4.200 | 4.200 | 136.0 | ||||||
976 | 2004-01-25T16:30 | 99.0 | 1 | 1190 | 6.50 | 2397.06 | 2.000 | 2.000 | 141.0 | ||||||
977 | 2004-01-25T18:56 | 216.0 | 1 | 1140 | 11.00 | 2398.92 | 3.000 | 3.000 | 147.0 | 0.484 | 916.0 | -24.6 | |||
978 | 2004-01-25T21:05 | 86.0 | 1 | 806 | 6.00 | 2400.18 | persistent communication problems | 2.200 | 2.200 | 114.0 | |||||
979 | 2004-01-25T23:30 | 128.0 | 1 | 753 | 7.50 | 2401.08 | persistent communication problems | 3.000 | 3.000 | 117.0 | |||||
980 | 2004-01-26T01:32 | 154.0 | 1 | 777 | 9.00 | 2402.88 | problems with the control of the motor | persistent communication problems | 3.100 | 3.100 | 122.0 | ||||
981 | 2004-01-26T03:59 | 47.0 | 1 | 799 | 3.50 | 2403.62 | problems with the control of the motor | persistent communication problems | 2.600 | 2.600 | 127.0 | ||||
982 | 2004-01-26T06:48 | 81.0 | 1 | 1008 | 5.00 | 2404.27 | problems with the control of the motor | 2.700 | 2.800 | 130.0 | |||||
983 | 2004-01-26T09:20 | 46.0 | 1 | 738 | 4.00 | 2404.80 | problems with the control of the motor | persistent communication problems | 2.000 | 2.000 | 135.0 | ||||
984 | 2004-01-26T11:18 | 117.0 | 1 | 769 | 7.00 | 2405.87 | changed core barrel, problems with the control of the barrel | persistent communication problems, changed to old electronics | 2.900 | 2.900 | 140.0 | ||||
985 | 2004-01-26T14:25 | 153.0 | 1 | 720 | 10.00 | 2407.17 | occasional communication problems | 1.900 | 1.900 | 143.0 | 0.242 | 918.6 | -27.0 | ||
986 | 2004-01-26T16:25 | 176.0 | 1 | 832 | 11.00 | 2408.99 | occasional communication problems | 1.900 | 1.900 | 111.0 | |||||
987 | 2004-01-26T18:40 | 2 | 1206 | 2410.39 | pulled due to high pump current | occasional communication problems | 1.800 | 1.900 | 115.0 | ||||||
987 | 2004-01-26T18:40 | 166.0 | 2 | 1036 | 10.00 | 2410.39 | occasional communication problems | 1.800 | 1.900 | 115.0 | |||||
988 | 2004-01-26T21:15 | 35.0 | 1 | 909 | 2.00 | 2411.77 | cutting problem | 2.400 | 2.400 | 121.0 | |||||
989 | 2004-01-26T23:44 | 137.0 | 1 | 717 | 8.00 | 2412.50 | changed drill head | 2.400 | 2.400 | 123.0 | |||||
990 | 2004-01-27T02:03 | 270.0 | 1 | 647 | 14.00 | 2415.31 | 2.800 | 2.800 | 128.0 | ||||||
991 | 2004-01-27T04:22 | 140.0 | 1 | 1049 | 8.00 | 2416.73 | 2.400 | 2.600 | 132.0 | ||||||
992 | 2004-01-27T06:30 | 169.0 | 1 | 1006 | 10.00 | 2418.38 | 2.700 | 2.800 | 140.0 | ||||||
993 | 2004-01-27T08:33 | 290.0 | 1 | 715 | 18.00 | 2421.26 | 2.600 | 2.600 | 141.0 | ||||||
994 | 2004-01-27T10:46 | 2 | 752 | 2422.46 | break due to instable cutting, instable idle current | 2.800 | 2.800 | 147.0 | |||||||
994 | 2004-01-27T10:46 | 120.0 | 2 | 762 | 2422.46 | instable cutting, instable idle current | 2.800 | 2.800 | 147.0 | 0.495 | 920.0 | -27.0 | |||
995 | 2004-01-27T12:53 | 260.0 | 1 | 675 | 16.00 | 2424.93 | 2.100 | 2.400 | 147.0 | ||||||
996 | 2004-01-27T15:05 | 243.0 | 1 | 748 | 13.00 | 2427.27 | 2.600 | 3.000 | 119.0 | ||||||
997 | 2004-01-27T17:06 | 93.0 | 1 | 731 | 2428.44 | 2.800 | 2.800 | 123.0 | |||||||
998 | 2004-01-27T19:20 | 156.0 | 1 | 863 | 13.00 | 2429.95 | 2.600 | 2.600 | 128.0 | ||||||
999 | 2004-01-27T21:15 | 202.0 | 1 | 1137 | 12.00 | 2432.13 | 1.800 | 2.600 | 131.0 | ||||||
1000 | 2004-01-27T23:26 | 166.0 | 1 | 1105 | 10.00 | 2433.74 | 2.650 | 2.650 | 134.0 | ||||||
1001 | 2004-01-28T01:42 | 138.0 | 1 | 1078 | 8.00 | 2435.18 | 2.550 | 2.550 | 140.0 | ||||||
1002 | 2004-01-28T03:48 | 167.0 | 1 | 735 | 9.00 | 2436.76 | 2.600 | 2.600 | 146.0 | ||||||
1003 | 2004-01-28T05:59 | 1200 | 2437.97 | no break | 2.000 | 2.000 | 150.0 | ||||||||
1003 | 2004-01-28T05:59 | 118.0 | 1 | 634 | 7.00 | 2437.97 | 2.000 | 2.000 | 150.0 | 0.453 | 921.0 | -30.0 | |||
1004 | 2004-01-28T08:05 | 2 | 652 | 10.00 | 2439.20 | break due to high cutting current | 2.000 | 2.000 | 120.0 | ||||||
1004 | 2004-01-28T08:05 | 136.0 | 2 | 652 | 10.00 | 2439.20 | high idle current, changed drill head | 2.000 | 2.000 | 120.0 | |||||
1005 | 2004-01-28T10:27 | 1204 | 2440.45 | break due to high pumping current, no break | 3.400 | 3.400 | 125.0 | ||||||||
1005 | 2004-01-28T10:27 | 872 | 7.00 | 2440.45 | break due to high pumping current | 3.400 | 3.400 | 125.0 | |||||||
1005 | 2004-01-28T10:27 | 136.0 | 3 | 752 | 7.00 | 2440.45 | 3.400 | 3.400 | 125.0 | ||||||
1006 | 2004-01-28T12:55 | 168.0 | 1 | 1054 | 10.00 | 2442.24 | 3.100 | 3.400 | 129.0 | ||||||
1007 | 2004-01-28T15:25 | 213.0 | 1 | 834 | 12.00 | 2444.31 | 2.200 | 2.800 | 133.0 | ||||||
1008 | 2004-01-28T17:47 | 276.0 | 1 | 650 | 16.00 | 2447.05 | 2.400 | 2.500 | 137.0 | ||||||
1009 | 2004-01-28T20:12 | 278.0 | 1 | 658 | 15.00 | 2449.67 | 2.400 | 2.400 | 144.0 | ||||||
1010 | 2004-01-28T22:32 | 107.0 | 1 | 1120 | 4.00 | 2451.33 | 2.800 | 2.800 | 150.0 | 0.373 | 920.0 | -28.3 | |||
1011 | 2004-01-29T01:09 | 141.0 | 1 | 986 | 7.50 | 2452.70 | changed to H2 | 2.700 | 2.700 | 124.0 | |||||
1012 | 2004-01-29T03:24 | 250.0 | 1 | 673 | 14.50 | 2455.10 | 2.400 | 2.400 | 127.0 | ||||||
1013 | 2004-01-29T05:35 | 256.0 | 1 | 823 | 14.00 | 2457.67 | 2.400 | 2.400 | 133.0 | ||||||
1014 | 2004-01-29T07:50 | 263.0 | 1 | 1021 | 17.00 | 2460.37 | 2.300 | 2.300 | 136.0 | ||||||
1015 | 2004-01-29T10:30 | 139.0 | 1 | 1105 | 8.00 | 2461.70 | 2.200 | 2.200 | 142.0 | 0.470 | 921.0 | -30.0 | |||
1016 | 2004-01-29T12:52 | 268.0 | 1 | 1207 | 15.50 | 2464.40 | 2.400 | 2.500 | 112.0 | ||||||
1017 | 2004-01-29T15:15 | 267.0 | 1 | 1154 | 15.00 | 2466.88 | 2.700 | 2.700 | 119.0 | ||||||
1018 | 2004-01-29T17:25 | 274.0 | 1 | 642 | 15.00 | 2469.66 | 2.300 | 2.400 | 122.0 | ||||||
1019 | 2004-01-29T19:51 | 148.0 | 1 | 764 | 8.50 | 2471.26 | 2.200 | 2.300 | 129.0 | ||||||
1020 | 2004-01-29T22:12 | 1200 | 2473.23 | no break | 3.500 | 3.500 | 133.0 | ||||||||
1020 | 2004-01-29T22:12 | 198.0 | 1 | 745 | 12.00 | 2473.23 | piece of core catcher missing | 3.500 | 3.500 | 133.0 | |||||
1021 | 2004-01-30T01:14 | 248.0 | 1 | 1147 | 14.50 | 2475.77 | 2.800 | 2.800 | 136.0 | ||||||
1022 | 2004-01-30T04:02 | 60.0 | 1 | 684 | 4.00 | 2476.49 | one cutter damaged | 2.200 | 2.200 | 140.0 | 0.497 | 922.0 | -31.0 | ||
FR42 | 2004-01-30T06:09 | 2476.49 | spring found and up again, switched to H2 | ||||||||||||
1023 | 2004-01-30T09:55 | 278.0 | 1 | 851 | 16.00 | 2478.76 | 3.400 | 3.400 | 114.0 | ||||||
1024 | 2004-01-30T12:15 | 64.0 | 1 | 1208 | 4.00 | 2479.99 | antitorque, break diue to high current | 3.400 | 3.400 | 114.0 | |||||
1025 | 2004-01-30T14:47 | 111.0 | 1 | 763 | 6.00 | 2481.03 | chips under the shoes | 3.200 | 3.400 | 119.0 | |||||
1026 | 2004-01-30T17:03 | 121.0 | 1 | 956 | 8.00 | 2482.20 | 2.600 | 2.600 | 123.0 | ||||||
1027 | 2004-01-30T19:30 | 235.0 | 1 | 760 | 2484.28 | 2.200 | 2.400 | 129.0 | |||||||
1028 | 2004-01-30T22:07 | 256.0 | 1 | 687 | 15.00 | 2486.80 | 2.300 | 2.400 | 133.0 | ||||||
1029 | 2004-01-31T00:38 | 1200 | 2488.28 | no break | 2.600 | 2.600 | 129.0 | ||||||||
1029 | 2004-01-31T00:38 | 122.0 | 1 | 924 | 7.00 | 2488.28 | cutting problems | 2.600 | 2.600 | 139.0 | |||||
1030 | 2004-01-31T03:00 | 112.0 | 1 | 1204 | 6.00 | 2489.17 | high idle current | 2.400 | 2.400 | 143.0 | 0.367 | 922.0 | -30.8 | ||
1031 | 2004-01-31T05:19 | 134.0 | 1 | 730 | 8.00 | 2490.86 | 2.500 | 2.500 | 122.0 | ||||||
1032 | 2004-01-31T07:29 | 150.0 | 1 | 963 | 11.00 | 2492.10 | changed to H2 | 2.100 | 2.100 | 126.0 | |||||
1033 | 2004-01-31T09:40 | 248.0 | 1 | 1208 | 15.00 | 2494.50 | 3.100 | 3.100 | 132.0 | ||||||
1034 | 2004-01-31T11:58 | 240.0 | 1 | 661 | 13.00 | 2497.09 | 3.100 | 3.100 | 135.0 | 0.336 | 920.0 | -29.0 | |||
1035 | 2004-01-31T14:15 | 113.0 | 1 | 1029 | 7.00 | 2498.14 | 2.800 | 3.100 | 112.0 | ||||||
1036 | 2004-01-31T16:35 | 255.0 | 1 | 1141 | 14.00 | 2500.48 | 3.150 | 3.100 | 118.0 | ||||||
FR43 | 2004-02-01T04:30 | 1.00 | 2500.48 | changed to shaft with Danish pump | |||||||||||
1037 | 2004-02-01T13:10 | 205.0 | 1 | 1191 | 15.00 | 2502.40 | 3.000 | 3.000 | 121.0 | ||||||
1038 | 2004-02-01T15:35 | 200.0 | 1 | 742 | 12.00 | 2504.63 | 3.100 | 3.100 | 130.0 | ||||||
1039 | 2004-02-01T17:35 | 119.0 | 1 | 1157 | 7.00 | 2505.72 | 3.100 | 3.100 | 133.0 | ||||||
1040 | 2004-02-01T20:05 | 134.0 | 1 | 1141 | 7.00 | 2507.30 | 2.000 | 2.000 | 139.0 | ||||||
1041 | 2004-02-01T22:32 | 760 | 2507.77 | antitorque and short rotation | 2.200 | 2.200 | 144.0 | ||||||||
1041 | 2004-02-01T22:32 | 40.0 | 2 | 1058 | 2507.94 | 2.200 | 2.200 | 144.0 | |||||||
1042 | 2004-02-02T01:01 | 69.0 | 1 | 1180 | 6.00 | 2508.52 | changed to H1 | 1.650 | 1.650 | 147.0 | 0.547 | 921.0 | -28.5 | ||
1043 | 2004-02-02T03:03 | 102.0 | 1 | 768 | 6.00 | 2509.52 | due to high current | 2.700 | 2.700 | 126.0 | |||||
1044 | 2004-02-02T05:02 | 112.0 | 1 | 1204 | 6.00 | 2510.48 | due to high current | 2.800 | 2.800 | 117.0 | |||||
1045 | 2004-02-02T07:30 | 1 | 1204 | 2512.26 | no break | 3.100 | 3.100 | 120.0 | |||||||
1045 | 2004-02-02T07:30 | 166.0 | 1 | 650 | 9.00 | 2512.26 | One spring broken | 3.100 | 3.100 | 120.0 | |||||
1046 | 2004-02-02T09:45 | 181.0 | 1 | 1112 | 13.00 | 2514.07 | 2.900 | 2.900 | 125.0 | ||||||
1047 | 2004-02-02T12:28 | 205.0 | 1 | 1204 | 12.00 | 2516.12 | 3.100 | 3.100 | 129.0 | ||||||
1048 | 2004-02-02T14:45 | 169.0 | 1 | 1072 | 10.00 | 2517.91 | 3.100 | 3.100 | 133.0 | ||||||
1049 | 2004-02-02T17:10 | 178.0 | 1 | 1142 | 9.00 | 2519.64 | 2.800 | 2.900 | 140.0 | ||||||
1050 | 2004-02-02T19:41 | 259.0 | 1 | 1023 | 14.50 | 2522.06 | 3.000 | 3.000 | 146.0 | 0.395 | 918.0 | -27.0 | |||
1051 | 2004-02-02T22:15 | 221.0 | 1 | 822 | 12.00 | 2524.42 | 3.100 | 3.100 | 119.0 | ||||||
1052 | 2004-02-03T00:41 | 187.0 | 1 | 975 | 10.00 | 2526.11 | 3.000 | 3.000 | 123.0 | ||||||
1053 | 2004-02-03T03:02 | 1 | 1210 | 2528.87 | no break | 3.100 | 3.200 | 130.0 | |||||||
1053 | 2004-02-03T03:02 | 254.0 | 1 | 1207 | 15.00 | 2528.87 | 3.100 | 3.200 | 130.0 | ||||||
1054 | 2004-02-03T06:05 | 133.0 | 1 | 1189 | 7.00 | 2530.37 | 3.300 | 3.300 | 134.0 | ||||||
1055 | 2004-02-03T08:15 | 1 | 1206 | 2530.37 | no break | 1.200 | 1.200 | 138.0 | |||||||
1055 | 2004-02-03T08:15 | 15.0 | 1 | 1252 | 3.00 | 2530.37 | cutting problems | 1.200 | 1.200 | 138.0 | |||||
1056 | 2004-02-03T11:23 | 115.0 | 1 | 1243 | 2531.33 | 2.300 | 2.500 | 141.0 | 0.430 | 922.0 | -30.5 | ||||
1057 | 2004-02-03T13:16 | 27.0 | 1 | 1003 | 2531.90 | cutting problems | 3.700 | 3.700 | |||||||
1058 | 2004-02-03T15:52 | 1 | 1250 | 2532.20 | no break | 2.550 | 2.550 | ||||||||
1058 | 2004-02-03T15:52 | 38.0 | 1 | 1304 | 6.00 | 2532.20 | cutting problems | 2.550 | 2.550 | ||||||
1059 | 2004-02-03T18:38 | 47.0 | 1 | 1095 | 3.00 | 2532.63 | cutting problems | 1.300 | 1.300 | 122.0 | |||||
1060 | 2004-02-03T21:00 | 56.0 | 1 | 1023 | 3.00 | 2533.50 | 1.200 | 1.200 | 127.0 | ||||||
1061 | 2004-02-03T23:26 | 155.0 | 1 | 1282 | 8.50 | 2534.79 | 1.550 | 1.550 | 133.0 | ||||||
1062 | 2004-02-04T01:55 | 175.0 | 1 | 824 | 10.00 | 2536.53 | 3.100 | 3.100 | 136.0 | ||||||
1063 | 2004-02-04T04:22 | 88.0 | 1 | 1201 | 5.00 | 2537.35 | 3.200 | 3.200 | 140.0 | ||||||
1064 | 2004-02-04T06:44 | 2537.35 | no cutting after various trials | 0.520 | 921.4 | -30.0 | |||||||||
1065 | 2004-02-04T09:28 | 13.0 | 1 | 1128 | 3.50 | 2537.26 | high cutting current, no rotation | 3.800 | 3.800 | 106.0 | |||||
1066 | 2004-02-04T11:56 | 71.0 | 1 | 893 | 3.50 | 2538.58 | changed to Hans Taussen | 2.700 | 3.700 | 110.0 | |||||
1067 | 2004-02-04T14:42 | 129.0 | 1 | 913 | 6.00 | 2539.36 | 2.700 | 2.500 | 112.0 | ||||||
1068 | 2004-02-04T17:00 | 86.0 | 1 | 934 | 6.00 | 2540.56 | 2.700 | 2.700 | 115.0 | ||||||
1069 | 2004-02-04T19:35 | 2540.56 | stoped due to cutting problems, no core in the barrel for unknown reasons, supposed break was at 500 kg | 117.0 | |||||||||||
1070 | 2004-02-04T21:54 | 110.0 | 1 | 868 | 4.00 | 2541.56 | 2.700 | 2.700 | 118.0 | ||||||
1071 | 2004-02-05T00:38 | 122.0 | 1 | 938 | 5.50 | 2542.82 | 3.100 | 3.100 | 120.0 | ||||||
1072 | 2004-02-05T02:53 | 48.0 | 1 | 1358 | 3.00 | 2543.45 | changed springs and unmounted screw of lower coupling | 3.000 | 3.000 | 122.0 | |||||
1073 | 2004-02-05T05:20 | 67.0 | 1 | 1332 | 4.00 | 2544.26 | persistent cutting problems | 3.000 | 3.000 | 124.0 | |||||
1074 | 2004-02-05T08:00 | 53.0 | 1 | 1294 | 4.00 | 2545.04 | 2.700 | 2.800 | 128.0 | ||||||
1075 | 2004-02-05T10:27 | 85.0 | 1 | 1024 | 5.00 | 2545.51 | changed electronics, back to HT | 2.900 | 2.700 | 131.0 | |||||
FR44 | 2004-02-05T13:46 | 2545.51 | spoooled cable out to repare winch, doesnt work | ||||||||||||
1076 | 2004-02-05T17:48 | 1 | 1304 | 2546.06 | no break, short rotation | 2.800 | 2.800 | 133.0 | |||||||
1076 | 2004-02-05T17:48 | 1 | 1324 | 2546.06 | no break, short rotation | 2.800 | 2.800 | 133.0 | |||||||
1076 | 2004-02-05T17:48 | 1 | 1462 | 2546.06 | no break, short rotation | 2.800 | 2.800 | 133.0 | |||||||
1076 | 2004-02-05T17:48 | 1 | 1620 | 2546.06 | no break, short rotation | 2.800 | 2.800 | 133.0 | |||||||
1076 | 2004-02-05T17:48 | 62.0 | 1 | 1606 | 4.50 | 2546.06 | rotation under load | 2.800 | 2.800 | 133.0 | |||||
1077 | 2004-02-05T21:30 | 92.0 | 1 | 1120 | 6.00 | 2547.24 | 2.800 | 2.800 | 137.0 | ||||||
1078 | 2004-02-06T00:37 | 32.0 | 1 | 1209 | 2547.72 | 2.700 | 2.700 | 138.0 | |||||||
1079 | 2004-02-06T02:55 | 87.0 | 1 | 1103 | 7.00 | 2548.63 | 2.700 | 2.700 | 139.0 | ||||||
1080 | 2004-02-06T05:07 | 60.0 | 1 | 1172 | 5.00 | 2549.18 | 2.800 | 2.800 | 141.0 | ||||||
1081 | 2004-02-06T07:21 | 90.0 | 1 | 1257 | 5.00 | 2550.08 | 2.400 | 2.400 | 143.0 | ||||||
1082 | 2004-02-06T09:48 | 100.0 | 1 | 1358 | 6.00 | 2557.03 | 2.700 | 2.700 | 146.0 | 0.421 | 922.0 | -30.6 | |||
1083 | 2004-02-06T11:58 | 66.0 | 1 | 1037 | 4.00 | 2551.62 | 2.900 | 2.900 | 116.0 | ||||||
1084 | 2004-02-06T14:36 | 43.0 | 1 | 1510 | 3.00 | 2551.91 | 2.300 | 2.300 | 121.0 | ||||||
BR1 | 2004-02-06T17:25 | 2551.76 | bailed down to bottom of the hole, tower flipped over when a band broke | 0.040 | 954.0 | -27.0 | |||||||||
FR45 | 2004-02-06T23:08 | 2551.76 | almost no slush | ||||||||||||
FR46 | 2004-02-07T00:37 | 2551.76 | |||||||||||||
1085 | 2004-02-07T12:14 | 36.0 | 1 | 1095 | 3.00 | 2552.55 | 2.200 | 2.200 | 119.0 | ||||||
FR47 | 2004-02-07T15:12 | 4.00 | 2552.55 | 4kg chips | |||||||||||
1086 | 2004-02-07T21:35 | 21.0 | 1 | 1154 | 2552.55 | 2.200 | 2.200 | 125.0 | |||||||
FR48 | 2004-02-08T03:00 | 2552.55 | 124.0 | ||||||||||||
2004-02-08T10:00 | 2552.55 | 0.523 | 920.0 | -29.3 | |||||||||||
2004-02-08T11:00 | 2552.55 | 0.571 | 920.0 | -29.3 | |||||||||||
END | 2004-02-08T12:00 | 2552.55 | plumbing with antitorque zeroed on lid | 70.0 | |||||||||||
START | 2005-11-14T17:10 | 2552.55 | measuring the liquid level, indicated depth with logger approx. 80 m | 80.0 | |||||||||||
2005-11-15T08:53 | 2554.37 | logging the hole | 80.0 | ||||||||||||
2005-11-20T15:00 | 2550.00 | logging the hole | 80.0 | ||||||||||||
RR1 | 2005-11-21T12:00 | 4.00 | 2378.37 | reaming with drill head with new cutters | old electronics mounted | 81.0 | |||||||||
RR2 | 2005-11-22T09:20 | 1700.00 | long drill with conical reamer attached to the end of the core barrel; no further penetration at approx. 1700 m, persistent antitorque rotation | 81.0 | |||||||||||
RR3 | 2005-11-22T15:00 | 3.50 | 339.15 | reaming hole from top with conical tool | |||||||||||
RR4 | 2005-11-22T17:20 | 11.00 | 791.00 | aborted run due to no more rotation possible | |||||||||||
RR5 | 2005-11-22T22:32 | 13.00 | 1277.60 | aborted run for cleaning and sharpening of the tool; repeated AT failures, tightened AT by 1/2 turn giving between 35-36.5 mm | |||||||||||
RR6 | 2005-11-23T10:50 | 11.00 | 1365.00 | aborted due to AT failures | changed inclinometer | ||||||||||
RR7 | 2005-11-23T16:40 | 21.00 | 1799.00 | aborted to clean | |||||||||||
RR8 | 2005-11-24T13:30 | 14.00 | 1948.15 | aborted due to rising current | 86.0 | ||||||||||
RR9 | 2005-11-25T02:30 | 18.00 | 2000.10 | aborted due to rising idle current | 88.0 | ||||||||||
RR10 | 2005-11-25T07:55 | 9.00 | 2101.11 | ||||||||||||
RR11 | 2005-11-25T14:05 | 18.00 | 2151.20 | high idle current | |||||||||||
RR12 | 2005-11-25T19:17 | 16.00 | 2204.56 | ||||||||||||
RR13 | 2005-11-26T03:20 | 17.00 | 2270.22 | 97.0 | |||||||||||
RR14 | 2005-11-26T08:47 | 15.50 | 2346.07 | 98.0 | |||||||||||
RR15 | 2005-11-26T14:55 | 9.00 | 2374.00 | stopped for Saturday night | 94.0 | ||||||||||
RR16 | 2005-11-27T14:56 | 15.00 | 2425.00 | 99.0 | |||||||||||
RR17 | 2005-11-28T01:00 | 6.50 | 2450.19 | 98.0 | |||||||||||
RR18 | 2005-11-28T09:50 | 19.00 | 2484.98 | 99.0 | |||||||||||
RR19 | 2005-11-28T19:15 | 16.00 | 2500.00 | pump blocked with chips and severly damaged: upper wave guide broken, one valve ring and 3 valves replaced | |||||||||||
FR48 | 2005-11-29T02:55 | 0.00 | 2401.00 | 92.0 | |||||||||||
RR20 | 2005-11-29T11:45 | 2425.08 | 98.0 | ||||||||||||
RR21 | 2005-11-29T15:15 | 8.00 | 2500.59 | 99.0 | |||||||||||
RR22 | 2005-11-29T17:48 | 19.00 | 2510.00 | chip chamber completely filled, pump damaged, several parts exchanged | 99.0 | ||||||||||
RR23 | 2005-11-29T21:36 | 16.00 | 2514.57 | ||||||||||||
RR24 | 2005-11-30T01:35 | 17.00 | 2520.00 | 98.0 | |||||||||||
RR25 | 2005-11-30T05:30 | 14.00 | 2525.00 | 98.0 | |||||||||||
RR26 | 2005-11-30T09:36 | 14.50 | 2530.00 | ||||||||||||
RR27 | 2005-11-30T13:20 | 14.50 | 2535.00 | changed to drillhead 3 x 0.18 mm# | 98.0 | ||||||||||
RR28 | 2005-11-30T16:45 | 14.00 | 2535.04 | stopped because of AT failure | 140.0 | ||||||||||
RR29 | 2005-11-30T20:14 | 19.00 | 2540.00 | 143.0 | |||||||||||
RR30 | 2005-11-30T23:26 | 17.00 | 2544.00 | 144.0 | |||||||||||
RR31 | 2005-12-01T04:20 | 17.00 | 2547.30 | stopped due to unstable current | chip chamber and pump completely filled, two valve rings are out of place | 150.0 | |||||||||
RR32 | 2005-12-01T09:08 | 19.00 | 2549.00 | 153.0 | |||||||||||
RR33 | 2005-12-01T12:25 | 14.00 | 2550.90 | load dropping, while going down | 153.0 | ||||||||||
RR34 | 2005-12-01T15:24 | 14.00 | 2552.90 | seems to rest on something (bottom ?) | 158.0 | ||||||||||
FR49 | 2005-12-01T18:45 | 2436.88 | can not penetrate further than 2457 m, pull back and can not penetrate beyond 2436.88 m | 160.0 | |||||||||||
RR35 | 2005-12-01T21:45 | 0.00 | 2507.04 | reamed again and pulled up after 100 m | 161.0 | ||||||||||
RR36 | 2005-12-02T01:05 | 7.00 | 2552.22 | 165.0 | |||||||||||
FR50 | 2005-12-02T03:55 | 8.00 | 2534.36 | 167.0 | |||||||||||
RR37 | 2005-12-02T06:20 | 15.00 | 2552.20 | ||||||||||||
FR51 | 2005-12-02T09:32 | 9.00 | 2539.66 | 172.0 | |||||||||||
RR38 | 2005-12-02T12:30 | 14.00 | 2552.30 | 174.0 | |||||||||||
FR52 | 2005-12-02T15:10 | 9.00 | 2543.00 | dumped pure densifier | 175.0 | 1.040 | 1300.0 | -29.0 | |||||||
RR39 | 2005-12-02T22:00 | 13.00 | 2520.00 | mounted the drill head; cutters came up damaged | 148.0 | 0.471 | 924.0 | -30.0 | |||||||
RR40 | 2005-12-03T02:00 | 11.00 | 2552.71 | 85.0 | |||||||||||
FR52 | 2005-12-03T05:15 | 12.00 | 2552.50 | 85.0 | |||||||||||
RR41 | 2005-12-03T08:25 | 10.50 | 2552.43 | no clear cutting | two metal parts and 1 screw are missing | 90.0 | |||||||||
1087 | 2005-12-03T11:45 | 6.5 | 1 | 5.00 | 2552.50 | heavily damaged core | 90.0 | ||||||||
FR53 | 2005-12-03T14:50 | 4.50 | 2552.50 | ||||||||||||
FR54 | 2005-12-03T17:20 | 2.00 | 2552.60 | 91.0 | |||||||||||
FR55 | 2005-12-04T14:20 | 1.00 | 2552.60 | 91.0 | |||||||||||
1088 | 2005-12-04T17:30 | 2552.05 | drillhead with centering tools | 96.0 | |||||||||||
1089 | 2005-12-04T19:55 | 6.5 | 1 | 980 | 1.50 | 2553.02 | AT failure; knives heavily damaged; plenty of metal chips | 95.0 | |||||||
1090 | 2005-12-04T23:10 | 803 | 2552.80 | loosened AT before run from 36/35.2/37.2 mm to 33.4/33.6/35.5 mm; AT failure | 98.0 | ||||||||||
1091 | 2005-12-05T01:30 | 3.0 | 1 | 810 | 2.00 | 2552.98 | tuned AT to 34.7/34.1/36.0 mm | 99.0 | |||||||
1092 | 2005-12-05T03:40 | 3.5 | 2 | 889 | 2552.78 | ||||||||||
1093 | 2005-12-05T06:10 | 2552.80 | no penetration | 99.0 | |||||||||||
1094 | 2005-12-05T09:33 | 7.0 | 4 | 996 | 2553.59 | changed AT to 34.9/36.8/35.3 mm | 104.0 | ||||||||
1095 | 2005-12-05T13:00 | 9.0 | 1 | 772 | 2552.79 | changed to new drillhead with 0.16/0.17 mm clearance | 106.0 | ||||||||
1096 | 2005-12-05T15:30 | 8.5 | 1 | 1024 | 2552.54 | tightened AT to 36.2/38.3/37.0 mm | 110.0 | ||||||||
1097 | 2005-12-05T19:04 | 870 | 2552.54 | changed to head with different cutters 0.225/0.22/0.225 mm; changed to used but resharpened AT blades 34.8/34.1/34.1 mm | 98.0 | 0.357 | 926.0 | -29.0 | |||||||
1097 | 2005-12-05T19:04 | 760 | 2552.54 | 98.0 | |||||||||||
1098 | 2005-12-05T22:15 | 34.0 | 1 | 1262 | 2553.22 | 98.0 | |||||||||
1099 | 2005-12-06T00:30 | 700 | 2553.22 | 100.0 | |||||||||||
1099 | 2005-12-06T00:30 | 8.5 | 1 | 696 | 2553.29 | ||||||||||
1100 | 2005-12-06T03:00 | 3.0 | 1 | 804 | 4.00 | 2553.73 | 102.0 | ||||||||
1101 | 2005-12-06T05:25 | 10.5 | 3 | 875 | 3.00 | 2550.80 | 102.0 | ||||||||
1102 | 2005-12-06T08:55 | 13.5 | 1 | 1061 | 1.00 | 2553.67 | switched to French HT with Danish top coupling and PE-spiral core barrel | 102.0 | |||||||
1103 | 2005-12-06T14:18 | 21.5 | 1 | 1297 | 2552.48 | found huge brass piece of unknown origin on top of core; head with new AWI cutters 0.175/0.18/0.19 mm; switched back to long drill | 102.0 | ||||||||
1104 | 2005-12-06T18:25 | 7.0 | 1 | 902 | 2553.30 | 110.0 | |||||||||
1105 | 2005-12-06T21:00 | 9.0 | 1 | 984 | 2.00 | 2553.55 | 110.0 | ||||||||
1106 | 2005-12-06T23:27 | 4.0 | 1 | 1024 | 2553.90 | loosened AT to 33.0/33.0/33.7 mm | 119.0 | ||||||||
1107 | 2005-12-07T02:15 | 8.0 | 3 | 1444 | 6.00 | 2553.68 | 123.0 | ||||||||
1108 | 2005-12-07T04:35 | 20.0 | 1 | 893 | 2554.38 | 127.0 | |||||||||
1109 | 2005-12-07T07:00 | 13.5 | 1 | 871 | 2554.38 | 135.0 | |||||||||
1110 | 2005-12-07T09:25 | 17.0 | 1 | 620 | 2554.18 | put 1 shim under each cutter | 136.0 | ||||||||
1111 | 2005-12-07T12:35 | 15.5 | 2 | 1162 | 3.00 | 2554.36 | measured cutters to 0.12/0.125/0.105 mm | 113.0 | 0.341 | 933.0 | -30.0 | ||||
1112 | 2005-12-07T15:20 | 10.0 | 1 | 583 | 2554.42 | stop because no penetration with dropping load | 93.0 | 0.386 | 933.0 | -30.1 | |||||
1113 | 2005-12-07T17:36 | 10.5 | 1 | 726 | 2554.80 | 95.0 | |||||||||
1114 | 2005-12-07T20:50 | 11.5 | 1 | 1109 | 2554.73 | loosened AT to 33.5/33.0/33.2 mm | 97.0 | ||||||||
1115 | 2005-12-08T00:20 | 6.0 | 1 | 1314 | 2554.92 | changed to head with 1 cutter and 2 pitch cutters with 0° free angle and 1 mm/2 mm | |||||||||
1116 | 2005-12-08T03:10 | 16.5 | 1 | 633 | 10.00 | 2555.43 | changed to old drill head | 109.0 | |||||||
1117 | 2005-12-08T05:20 | 18.0 | 1 | 686 | 2555.43 | 114.0 | |||||||||
1118 | 2005-12-08T07:25 | 34.0 | 1 | 610 | 2556.11 | ||||||||||
1119 | 2005-12-08T09:40 | 11.0 | 1 | 848 | 2556.05 | 119.0 | |||||||||
1120 | 2005-12-08T12:00 | 9.0 | 1 | 1106 | 3.00 | 2556.15 | 93.0 | 0.472 | 926.0 | -31.5 | |||||
1121 | 2005-12-08T14:30 | 18.0 | 1 | 593 | 2555.78 | measured head to 0.12/0.12/0.13 mm; tuned to 0.145/0.155/0.16 mm | 96.0 | ||||||||
1122 | 2005-12-08T16:38 | 52.0 | 1 | 633 | 3.00 | 2556.69 | 1.500 | 1.500 | 98.0 | ||||||
1123 | 2005-12-08T21:10 | 11.0 | 1 | 1121 | 1.00 | 2556.60 | changed to HT drill with same head | 2.800 | 2.800 | 99.0 | |||||
1124 | 2005-12-08T23:25 | 128.0 | 1 | 1167 | 5.50 | 2557.89 | changed to head H2 with new AWI cutters; tuned to 0.17/0.18/0.18 mm | 102.0 | |||||||
1125 | 2005-12-09T01:25 | 35.0 | 1 | 954 | 3.00 | 2558.95 | 106.0 | ||||||||
1126 | 2005-12-09T03:40 | 80.5 | 1 | 918 | 2.50 | 2558.99 | 108.0 | ||||||||
1127 | 2005-12-09T05:55 | 29.0 | 1 | 865 | 2559.27 | 110.0 | |||||||||
1128 | 2005-12-09T08:10 | 63.5 | 1 | 1316 | 3.00 | 2560.25 | 4.000 | 4.000 | 111.0 | ||||||
1129 | 2005-12-09T10:46 | 105.0 | 1 | 502 | 5.00 | 2561.40 | 3.800 | 3.800 | 113.4 | ||||||
1130 | 2005-12-09T13:15 | 75.0 | 1 | 1166 | 4.50 | 2561.78 | 3.600 | 3.600 | 94.0 | 0.376 | 923.0 | -29.0 | |||
1131 | 2005-12-09T15:18 | 102.0 | 1 | 626 | 5.50 | 2562.87 | 3.650 | 3.650 | |||||||
1132 | 2005-12-09T17:18 | 39.0 | 1 | 1078 | 2.50 | 2563.47 | 3.300 | 3.300 | 93.0 | ||||||
1133 | 2005-12-09T19:30 | 50.0 | 1 | 1505 | 2.50 | 2563.70 | 94.0 | ||||||||
1134 | 2005-12-09T21:35 | 57.0 | 1 | 1291 | 4.00 | 2564.35 | changed to head H1 tuned to 0.14/0.15/0.16 mm | 97.0 | |||||||
1135 | 2005-12-10T00:20 | 55.0 | 2 | 1230 | 2.00 | 2564.86 | changed to head H2 tuned to 0.175/0.18/0.19 mm | 100.0 | |||||||
1136 | 2005-12-10T02:25 | 70.0 | 1 | 1102 | 5.00 | 2565.75 | changed to head H1 tuned to 0.14/0.15/0.16 mm; screws sealed with candle wax | 102.0 | |||||||
1137 | 2005-12-10T04:20 | 29.0 | 1 | 1818 | 2.50 | 2566.50 | 105.0 | ||||||||
1138 | 2005-12-10T06:40 | 28.5 | 1 | 1222 | 2566.24 | persistent antitorque rotation | 2.500 | 2.500 | 108.0 | ||||||
1139 | 2005-12-10T08:50 | 67.0 | 1 | 1031 | 5.00 | 2566.99 | 2.500 | 2.500 | 107.0 | ||||||
1140 | 2005-12-10T11:15 | 76.5 | 1 | 1256 | 3.00 | 2567.70 | mounted 3rd core catcher; sealed shoe screws with wax | 1.000 | 1.000 | 109.0 | |||||
1141 | 2005-12-10T13:40 | 42.0 | 1 | 1196 | 2.50 | 2568.03 | 90.0 | 0.339 | 920.0 | -23.3 | |||||
1142 | 2005-12-10T16:10 | 57.0 | 2 | 1233 | 3.00 | 2569.16 | 90.0 | ||||||||
FR56 | 2005-12-11T09:02 | 2.00 | 2569.50 | 92.0 | |||||||||||
1143 | 2005-12-11T13:48 | 13.0 | 1 | 834 | 2568.09 | changed to long drill; freshly tuned drill head 0.145/0.15/0.165 mm; shoes sealed with glued PE | 98.0 | ||||||||
1144 | 2005-12-11T16:30 | 12.0 | 1 | 1353 | 2569.31 | changed to short drill | 96.0 | ||||||||
1145 | 2005-12-11T18:50 | 106.0 | 1 | 1229 | 5.50 | 2569.62 | 3.200 | 3.200 | 98.0 | ||||||
1146 | 2005-12-11T20:50 | 120.0 | 1 | 714 | 5.00 | 2569.98 | 3.350 | 3.350 | 100.0 | ||||||
1147 | 2005-12-11T22:58 | 89.0 | 1 | 1049 | 5.00 | 2571.83 | 3.300 | 3.300 | 100.0 | ||||||
1148 | 2005-12-12T00:55 | 98.0 | 1 | 1462 | 5.00 | 2573.22 | 3.450 | 3.450 | 88.0 | 0.366 | 923.0 | -27.5 | |||
1149 | 2005-12-12T02:55 | 103.0 | 1 | 1038 | 5.00 | 2574.31 | 3.300 | 3.300 | 91.0 | ||||||
1150 | 2005-12-12T04:50 | 105.0 | 1 | 1150 | 5.00 | 2575.33 | 3.300 | 3.300 | 93.0 | ||||||
1151 | 2005-12-12T07:05 | 104.0 | 2 | 1120 | 5.00 | 2576.30 | 3.100 | 3.100 | 96.0 | ||||||
1152 | 2005-12-12T09:10 | 81.0 | 1 | 995 | 5.00 | 2576.94 | 3.360 | 3.360 | 93.0 | ||||||
1153 | 2005-12-12T11:33 | 97.0 | 1 | 714 | 6.00 | 2577.66 | 3.200 | 3.200 | 94.0 | ||||||
1154 | 2005-12-12T14:12 | 75.5 | 1 | 1275 | 5.00 | 2578.00 | 3.400 | 3.400 | 93.0 | ||||||
1155 | 2005-12-12T16:35 | 108.0 | 1 | 1111 | 5.00 | 2579.72 | 3.370 | 3.370 | 95.0 | ||||||
1156 | 2005-12-12T18:45 | 110.0 | 1 | 1216 | 5.00 | 2580.52 | 3.400 | 3.400 | 93.0 | ||||||
1157 | 2005-12-12T20:45 | 85.0 | 1 | 687 | 5.00 | 2581.38 | 3.400 | 3.400 | 100.0 | ||||||
1158 | 2005-12-12T22:40 | 112.0 | 1 | 1408 | 6.00 | 2582.67 | 3.600 | 3.600 | 102.0 | ||||||
1159 | 2005-12-13T00:45 | 87.0 | 1 | 974 | 5.00 | 2583.97 | 3.380 | 3.380 | 106.0 | ||||||
1160 | 2005-12-13T02:45 | 91.7 | 1 | 1360 | 5.00 | 2584.93 | 3.350 | 3.350 | 108.0 | ||||||
1161 | 2005-12-13T04:45 | 88.0 | 1 | 1266 | 5.00 | 2585.85 | 3.350 | 3.350 | 111.0 | ||||||
1162 | 2005-12-13T06:50 | 66.0 | 1 | 1298 | 4.00 | 2586.45 | 3.200 | 3.200 | 113.0 | ||||||
1163 | 2005-12-13T09:50 | 6.0 | 1 | 711 | 2585.71 | changed core catcher springs; changed to long drill; sharpened all core catchers | 113.0 | ||||||||
1164 | 2005-12-13T12:15 | 24.0 | 1 | 994 | 2586.38 | changed to short drill | 3.500 | 3.500 | 117.0 | ||||||
1165 | 2005-12-13T14:22 | 58.0 | 1 | 676 | 6.00 | 2587.02 | 2.500 | 2.500 | 92.0 | 0.370 | 922.0 | -27.6 | |||
1166 | 2005-12-13T16:22 | 97.0 | 1 | 667 | 4.50 | 2587.71 | 2.660 | 2.660 | 94.0 | ||||||
1167 | 2005-12-13T18:20 | 103.0 | 2 | 1154 | 2588.68 | 3.000 | 3.000 | 96.0 | |||||||
1168 | 2005-12-13T20:55 | 7.0 | 1 | 1056 | 5.00 | 2588.47 | changed to long drill with new plastic centering parts on core barrel | 101.0 | |||||||
1169 | 2005-12-13T23:30 | 17.0 | 2 | 1095 | 2589.16 | changed to HT drill with 18000 holes; 1 cutter slightly damaged - sharpened | 104.0 | ||||||||
1170 | 2005-12-14T01:35 | 11.0 | 1 | 643 | 5.00 | 2589.38 | 107.0 | ||||||||
1171 | 2005-12-14T03:40 | 67.0 | 1 | 986 | 4.00 | 2589.32 | changed to drill head H1 0.145/0.15/0.15 mm | 3.390 | 3.390 | 110.0 | |||||
1172 | 2005-12-14T05:35 | 98.0 | 1 | 1148 | 5.00 | 2590.91 | 3.350 | 3.350 | 107.0 | ||||||
1173 | 2005-12-14T07:40 | 45.0 | 1 | 1273 | 2591.55 | 3.400 | 3.400 | 113.0 | |||||||
1174 | 2005-12-14T10:05 | 101.0 | 1 | 1137 | 6.00 | 2592.16 | 3.200 | 3.200 | 113.0 | ||||||
1175 | 2005-12-14T12:42 | 64.0 | 1 | 1060 | 3.00 | 2592.71 | 3.500 | 3.500 | 89.0 | 0.407 | 918.0 | -23.9 | |||
1176 | 2005-12-14T15:13 | 81.0 | 1 | 1513 | 4.50 | 2593.28 | 3.400 | 3.400 | 90.0 | ||||||
1177 | 2005-12-14T17:40 | 101.0 | 1 | 1023 | 5.50 | 2594.99 | 3.400 | 3.400 | 91.0 | ||||||
1178 | 2005-12-14T19:40 | 58.0 | 1 | 1110 | 2.00 | 2595.29 | 3.300 | 3.300 | 93.0 | ||||||
1179 | 2005-12-14T21:50 | 73.0 | 1 | 1234 | 3.50 | 2595.89 | 3.400 | 3.400 | 96.0 | ||||||
1180 | 2005-12-15T00:01 | 68.0 | 1 | 1207 | 2.50 | 2596.49 | 3.380 | 3.380 | 100.0 | ||||||
1181 | 2005-12-15T01:55 | 49.0 | 1 | 1466 | 2597.80 | 3.530 | 3.530 | 102.0 | |||||||
1182 | 2005-12-15T04:05 | 61.0 | 1 | 867 | 5.00 | 2598.52 | 3.420 | 3.420 | 102.0 | ||||||
1183 | 2005-12-15T06:05 | 23.0 | 1 | 1123 | 1.00 | 2599.07 | 3.260 | 3.260 | 106.0 | ||||||
1184 | 2005-12-15T09:07 | 112.0 | 1 | 1306 | 4.00 | 2598.63 | 3.300 | 3.300 | 106.0 | ||||||
1185 | 2005-12-15T11:05 | 58.0 | 1 | 1302 | 2.50 | 2600.05 | 3.300 | 3.300 | 108.0 | ||||||
1186 | 2005-12-15T13:15 | 68.5 | 1 | 882 | 3.00 | 2600.52 | 3.350 | 3.350 | 88.0 | 0.370 | 921.0 | -26.9 | |||
1187 | 2005-12-15T15:20 | 61.0 | 1 | 1240 | 2.00 | 2600.87 | 3.300 | 3.300 | 90.0 | ||||||
1188 | 2005-12-15T17:45 | 86.5 | 1 | 1143 | 3.00 | 2602.21 | 3.500 | 3.500 | 90.0 | ||||||
1189 | 2005-12-15T20:05 | 18.0 | 1 | 1810 | 2602.17 | changed to Danish shaft and pump with French outer barrel | 92.0 | ||||||||
1190 | 2005-12-15T23:25 | 34.0 | 3 | 734 | 2602.83 | 3.300 | 3.300 | 94.0 | |||||||
1191 | 2005-12-16T01:30 | 34.0 | 1 | 833 | 2603.10 | 3.300 | 3.300 | 96.0 | |||||||
1192 | 2005-12-16T05:05 | 46.0 | 1 | 853 | 5.00 | 2603.48 | changed to French shaft and pump | 3.350 | 3.350 | 99.0 | |||||
1193 | 2005-12-16T07:30 | 102.0 | 1 | 1303 | 6.00 | 2604.75 | 3.200 | 3.200 | 102.0 | ||||||
1194 | 2005-12-16T09:30 | 20.0 | 1 | 984 | 1.00 | 2604.87 | 101.0 | ||||||||
1195 | 2005-12-16T11:40 | 52.0 | 1 | 1501 | 2.50 | 2605.12 | 3.000 | 3.000 | 84.0 | 0.411 | 917.0 | -23.3 | |||
1196 | 2005-12-16T14:10 | 82.0 | 1 | 1233 | 4.50 | 2605.79 | changed to PE spiral core barrel with French HT drill | 3.000 | 3.000 | 85.0 | |||||
1197 | 2005-12-16T16:20 | 75.0 | 1 | 1235 | 4.00 | 2606.51 | 3.200 | 3.200 | 86.0 | ||||||
1198 | 2005-12-16T18:45 | 19.0 | 1 | 1190 | 1.00 | 2606.82 | 86.0 | ||||||||
1199 | 2005-12-16T21:00 | 82.0 | 1 | 1150 | 3.50 | 2607.43 | 3.400 | 3.400 | 87.0 | ||||||
1200 | 2005-12-16T23:40 | 101.0 | 1 | 1308 | 5.00 | 2608.71 | 3.400 | 3.400 | 89.0 | ||||||
1201 | 2005-12-17T01:55 | 103.0 | 1 | 1305 | 5.00 | 2610.23 | 3.350 | 3.350 | 93.0 | ||||||
1202 | 2005-12-17T04:05 | 81.0 | 1 | 1208 | 4.00 | 2610.97 | 3.550 | 3.550 | 95.0 | ||||||
1203 | 2005-12-17T06:25 | 24.0 | 1 | 1201 | 2611.55 | 98.0 | |||||||||
1204 | 2005-12-17T08:40 | 89.0 | 1 | 847 | 4.00 | 2611.86 | 3.700 | 3.700 | 92.0 | ||||||
1205 | 2005-12-17T11:00 | 114.0 | 1 | 1051 | 5.00 | 2612.44 | changed to drill head H2 0.165/0.15/0.145 mm | 3.060 | 3.060 | 84.0 | 0.344 | 919.0 | -24.7 | ||
1206 | 2005-12-17T13:10 | 91.0 | 1 | 1222 | 4.00 | 2613.23 | 3.200 | 3.200 | 83.0 | ||||||
1207 | 2005-12-17T15:25 | 67.5 | 1 | 717 | 4.00 | 2613.90 | 3.300 | 3.300 | 84.0 | ||||||
1208 | 2005-12-17T17:40 | 79.0 | 1 | 1127 | 5.00 | 2614.90 | 0.500 | 3.200 | 86.0 | ||||||
FR57 | 2005-12-18T04:30 | 3.00 | 2614.90 | 92.0 | |||||||||||
1209 | 2005-12-18T13:20 | 90.0 | 1 | 1606 | 5.00 | 2616.04 | 3.100 | 3.100 | 89.0 | ||||||
1210 | 2005-12-18T15:30 | 79.0 | 1 | 1302 | 4.50 | 2616.12 | 3.000 | 3.000 | 89.0 | ||||||
1211 | 2005-12-18T17:25 | 40.0 | 1 | 1312 | 2.00 | 2617.31 | 91.0 | ||||||||
1212 | 2005-12-18T19:45 | 78.0 | 1 | 1122 | 4.00 | 2618.19 | 3.000 | 3.000 | 91.0 | ||||||
1213 | 2005-12-18T21:47 | 71.0 | 1 | 1274 | 3.00 | 2618.80 | lost one lid of pump; found lid and 1 screw | 3.300 | 3.300 | 93.0 | |||||
1214 | 2005-12-19T00:15 | 15.0 | 1 | 1218 | 2619.15 | 95.0 | |||||||||
1215 | 2005-12-19T03:00 | 115.0 | 1 | 1457 | 7.00 | 2620.47 | 3.120 | 3.120 | 97.0 | ||||||
1216 | 2005-12-19T05:00 | 77.0 | 1 | 1015 | 4.00 | 2621.76 | 3.500 | 3.500 | 101.0 | ||||||
1217 | 2005-12-19T07:10 | 31.0 | 1 | 630 | 2.00 | 2621.55 | 104.0 | ||||||||
1218 | 2005-12-19T09:20 | 82.0 | 1 | 1408 | 6.00 | 2622.33 | 103.0 | ||||||||
1219 | 2005-12-19T11:35 | 54.0 | 1 | 1128 | 3.00 | 2623.60 | 3.360 | 3.360 | 85.0 | 0.360 | 921.0 | -27.5 | |||
1220 | 2005-12-19T13:45 | 38.0 | 1 | 696 | 1.50 | 2622.86 | 3.000 | 3.000 | 86.0 | ||||||
1221 | 2005-12-19T17:00 | 91.0 | 1 | 1312 | 4.50 | 2623.85 | two grooves of the inner barrel heavily iced; changed to aluminium spiral core barrel with the same head | 3.200 | 3.200 | 91.0 | |||||
1222 | 2005-12-19T19:00 | 49.0 | 1 | 1044 | 3.00 | 2624.57 | 3.000 | 3.000 | 90.0 | ||||||
1223 | 2005-12-19T21:40 | 40.0 | 1 | 1266 | 2624.75 | 3.280 | 3.280 | 91.0 | |||||||
1224 | 2005-12-20T00:25 | 21.0 | 1 | 858 | 2625.22 | 3.300 | 3.300 | 95.0 | |||||||
1225 | 2005-12-20T03:20 | 31.0 | 1 | 1607 | 4.00 | 2625.60 | changed to barrel with PE spirals | 3.450 | 3.450 | 98.0 | |||||
1226 | 2005-12-20T05:50 | 74.0 | 1 | 1080 | 4.00 | 2626.99 | 3.400 | 3.400 | 100.0 | ||||||
1227 | 2005-12-20T08:25 | 31.0 | 1 | 691 | 2.00 | 2627.49 | 102.0 | ||||||||
1228 | 2005-12-20T10:30 | 112.0 | 1 | 1252 | 5.00 | 2627.49 | changed to H2, tuned 0.16/0.165/0.16 mm | 3.200 | 3.200 | 102.0 | |||||
1229 | 2005-12-20T12:40 | 103.0 | 1 | 1282 | 5.50 | 2628.76 | 3.200 | 3.200 | 103.0 | ||||||
1230 | 2005-12-20T15:00 | 32.0 | 1 | 1505 | 2.00 | 2628.61 | 3.200 | 3.200 | 86.0 | 0.360 | 919.0 | -24.5 | |||
1231 | 2005-12-20T17:15 | 83.0 | 1 | 1406 | 4.50 | 2629.58 | 3.300 | 3.300 | 88.0 | ||||||
1232 | 2005-12-20T19:55 | 85.0 | 1 | 972 | 4.00 | 2630.38 | 3.500 | 3.500 | 89.0 | ||||||
1233 | 2005-12-20T22:10 | 106.0 | 1 | 1156 | 5.00 | 2631.66 | 3.250 | 3.250 | 91.0 | ||||||
1234 | 2005-12-21T00:15 | 91.0 | 1 | 1414 | 5.00 | 2632.63 | 3.300 | 3.300 | 93.0 | ||||||
1235 | 2005-12-21T02:35 | 96.0 | 1 | 929 | 5.00 | 2633.58 | 3.300 | 3.300 | 95.0 | ||||||
1236 | 2005-12-21T04:40 | 49.0 | 1 | 1024 | 2.00 | 2633.97 | 3.390 | 3.390 | 98.0 | ||||||
1237 | 2005-12-21T07:05 | 88.0 | 1 | 1211 | 4.00 | 2635.08 | 3.600 | 3.600 | 100.0 | ||||||
1238 | 2005-12-21T09:05 | 82.0 | 3 | 1155 | 4.50 | 2636.48 | 3.600 | 3.600 | 99.0 | ||||||
1239 | 2005-12-21T11:35 | 40.0 | 2 | 1302 | 2.00 | 2636.08 | 3.200 | 3.200 | 83.0 | 0.372 | 918.0 | -23.5 | |||
1240 | 2005-12-21T14:00 | 65.0 | 1 | 1809 | 3.00 | 2636.51 | 86.0 | ||||||||
1241 | 2005-12-21T17:28 | 34.0 | 1 | 1223 | 1.00 | 2637.00 | 3.200 | 3.200 | 87.0 | ||||||
1242 | 2005-12-21T19:40 | 31.0 | 1 | 1058 | 1.50 | 2637.79 | 3.200 | 3.200 | 88.0 | ||||||
1243 | 2005-12-21T21:50 | 88.0 | 2 | 1310 | 2638.18 | 3.200 | 3.200 | 88.0 | |||||||
1244 | 2005-12-21T23:59 | 47.0 | 2 | 1190 | 6.00 | 2638.71 | 3.000 | 3.000 | 91.0 | ||||||
1245 | 2005-12-22T02:25 | 23.0 | 1 | 1032 | 1.00 | 2639.86 | 3.650 | 3.650 | 93.0 | ||||||
1246 | 2005-12-22T04:25 | 81.0 | 1 | 1700 | 3.00 | 2640.56 | 3.600 | 3.600 | 94.0 | ||||||
1247 | 2005-12-22T07:00 | 68.0 | 1 | 1207 | 4.00 | 2641.33 | 3.800 | 3.800 | 97.0 | ||||||
1248 | 2005-12-22T09:15 | 66.5 | 1 | 1010 | 3.00 | 2641.20 | 3.300 | 3.300 | 96.0 | ||||||
1249 | 2005-12-22T11:05 | 57.0 | 1 | 1510 | 2.50 | 2641.62 | 3.300 | 3.300 | 99.0 | ||||||
1250 | 2005-12-22T13:55 | 13.5 | 1 | 988 | 2641.84 | 85.0 | 0.310 | 919.0 | -24.0 | ||||||
1251 | 2005-12-22T16:54 | 85.5 | 1 | 1019 | 4.00 | 2642.41 | changed to Rufli head with 1 cutter, 2 x 0° free angle with 1 mm clearance steps; nominal pitch 3 mm | 3.200 | 3.200 | 87.0 | |||||
1252 | 2005-12-22T19:10 | 96.5 | 1 | 741 | 4.50 | 2643.43 | 3.200 | 3.200 | 87.0 | ||||||
1253 | 2005-12-22T21:13 | 56.0 | 3 | 719 | 3.00 | 2644.07 | 2.700 | 2.700 | 89.0 | ||||||
1254 | 2005-12-23T00:05 | 50.0 | 2 | 694 | 2644.74 | measured clearance 0/0.85/1.9 mm; adjusted to 0/0.7/1.4 mm | 92.0 | ||||||||
1255 | 2005-12-23T02:05 | 117.0 | 1 | 724 | 7.00 | 2644.96 | 2.400 | 2.400 | 94.0 | ||||||
1256 | 2005-12-23T04:20 | 94.0 | 1 | 1407 | 5.00 | 2647.16 | 2.400 | 2.400 | 96.0 | ||||||
1257 | 2005-12-23T06:30 | 81.0 | 1 | 777 | 4.00 | 2647.77 | 2.500 | 2.500 | 98.0 | ||||||
1258 | 2005-12-23T09:10 | 62.0 | 1 | 1275 | 3.00 | 2648.31 | 2.300 | 2.300 | 95.0 | ||||||
1259 | 2005-12-23T11:40 | 96.0 | 1 | 984 | 4.00 | 2649.19 | 2.400 | 2.400 | 85.0 | 0.365 | 919.0 | -25.0 | |||
1260 | 2005-12-23T13:58 | 95.0 | 1 | 676 | 4.00 | 2650.14 | 2.400 | 2.400 | 86.0 | ||||||
1261 | 2005-12-23T16:10 | 56.0 | 2 | 904 | 2.00 | 2650.51 | 2.700 | 2.700 | 87.0 | ||||||
1262 | 2005-12-23T18:15 | 86.0 | 1 | 692 | 1.00 | 2651.73 | 2.400 | 2.400 | 88.0 | ||||||
1263 | 2005-12-23T20:37 | 52.0 | 1 | 698 | 3.00 | 2652.27 | 2.500 | 2.500 | 89.0 | ||||||
1264 | 2005-12-23T22:55 | 95.0 | 1 | 1120 | 4.00 | 2653.17 | 2.550 | 2.550 | 90.0 | ||||||
1265 | 2005-12-24T01:10 | 83.0 | 1 | 1205 | 3.00 | 2654.25 | 2.550 | 2.550 | 94.0 | ||||||
1266 | 2005-12-24T03:00 | 88.0 | 1 | 730 | 4.00 | 2655.58 | 2.620 | 2.620 | 95.0 | ||||||
1267 | 2005-12-24T05:00 | 59.0 | 1 | 1204 | 2.00 | 2655.92 | 2.550 | 2.550 | 96.0 | ||||||
1268 | 2005-12-24T07:05 | 81.0 | 1 | 1125 | 2.50 | 2656.35 | 2.750 | 2.750 | 98.0 | ||||||
1269 | 2005-12-24T09:10 | 110.0 | 1 | 1166 | 4.00 | 2657.31 | 2.350 | 2.350 | 95.0 | ||||||
1270 | 2005-12-24T11:30 | 66.0 | 2 | 2080 | 3.50 | 2657.83 | 2.600 | 2.700 | 99.0 | ||||||
1271 | 2005-12-24T16:00 | 85.0 | 2 | 1413 | 4.00 | 2658.60 | changed to drill head H1 with closed core catcher windows; pitch adjusted to 0/0.65/1.3 mm | 2.200 | 2.200 | 84.0 | 0.369 | 918.0 | -23.5 | ||
FR58 | 2005-12-25T14:12 | 2.00 | 2659.00 | ||||||||||||
1272 | 2005-12-25T16:35 | 86.0 | 1 | 1248 | 5.00 | 2659.29 | 2.500 | 2.500 | 87.0 | ||||||
1273 | 2005-12-25T18:00 | 102.0 | 1 | 1025 | 5.00 | 2660.96 | 2.420 | 2.420 | 86.0 | ||||||
1274 | 2005-12-25T20:45 | 95.0 | 1 | 1026 | 5.00 | 2661.40 | 2.500 | 2.500 | 89.0 | ||||||
1275 | 2005-12-25T22:54 | 72.0 | 2 | 987 | 3.50 | 2662.22 | 2.400 | 2.400 | 90.0 | ||||||
1276 | 2005-12-26T01:15 | 96.0 | 1 | 1088 | 5.00 | 2663.23 | 2.550 | 2.550 | 74.0 | 0.292 | 916.5 | -22.2 | |||
1277 | 2005-12-26T03:20 | 91.0 | 1 | 948 | 4.50 | 2664.60 | 2.400 | 2.400 | 78.0 | ||||||
1278 | 2005-12-26T05:25 | 100.0 | 1 | 642 | 5.00 | 2665.30 | 2.400 | 2.400 | 82.0 | ||||||
1279 | 2005-12-26T07:35 | 73.5 | 1 | 1510 | 3.50 | 2665.94 | 2.150 | 2.150 | 86.0 | ||||||
1280 | 2005-12-26T10:00 | 84.0 | 1 | 1074 | 3.50 | 2666.59 | 2.200 | 2.200 | 87.0 | ||||||
1281 | 2005-12-26T12:15 | 74.0 | 1 | 1523 | 4.00 | 2667.31 | 2.800 | 2.800 | 87.0 | ||||||
1282 | 2005-12-26T15:10 | 60.0 | 1 | 1201 | 3.00 | 2667.94 | 2.500 | 2.500 | 88.0 | ||||||
1283 | 2005-12-26T17:45 | 42.0 | 1 | 1083 | 2.50 | 2668.31 | 2.800 | 2.800 | 89.0 | ||||||
1284 | 2005-12-26T20:15 | 56.0 | 2 | 1837 | 2.50 | 2668.75 | 2.500 | 2.500 | 89.0 | ||||||
1285 | 2005-12-26T23:05 | 58.0 | 1 | 2400 | 2669.76 | 2.400 | 2.400 | 91.0 | |||||||
1286 | 2005-12-27T03:05 | 20.0 | 1 | 1208 | 4.50 | 2669.94 | 2.400 | 2.400 | 84.0 | 0.275 | 918.0 | -24.2 | |||
1287 | 2005-12-27T05:00 | 45.0 | 1 | 991 | 2.00 | 2670.63 | 2.400 | 2.400 | 87.0 | ||||||
1288 | 2005-12-27T14:05 | 41.0 | 1 | 1504 | 2.00 | 2670.58 | 2.300 | 2.300 | 84.0 | ||||||
1289 | 2005-12-27T16:30 | 48.0 | 1 | 1232 | 1.00 | 2671.32 | 2.500 | 2.500 | 85.0 | ||||||
1290 | 2005-12-27T18:40 | 49.0 | 1 | 718 | 2.00 | 2671.68 | 2.100 | 2.100 | 87.0 | ||||||
1291 | 2005-12-27T21:45 | 53.0 | 1 | 1366 | 1.00 | 2672.20 | 1.550 | 1.550 | 89.0 | ||||||
1292 | 2005-12-27T23:50 | 26.0 | 1 | 1457 | 1.00 | 2672.76 | 1.600 | 1.600 | 90.0 | ||||||
1293 | 2005-12-28T02:05 | 41.0 | 1 | 1196 | 1.00 | 2673.64 | 1.580 | 1.580 | 85.0 | 0.175 | 918.0 | -23.5 | |||
1294 | 2005-12-28T04:05 | 35.0 | 1 | 1118 | 1.00 | 2673.76 | 1.850 | 1.850 | 87.0 | ||||||
1295 | 2005-12-28T06:15 | 33.0 | 1 | 1116 | 1.00 | 2674.59 | 1.800 | 1.800 | 90.0 | ||||||
1296 | 2005-12-28T08:15 | 38.0 | 1 | 1275 | 2.00 | 2674.33 | 89.0 | ||||||||
1297 | 2005-12-28T10:45 | 39.0 | 1 | 1140 | 1.00 | 2674.41 | 89.0 | ||||||||
1298 | 2005-12-28T13:30 | 24.0 | 1 | 985 | 2.00 | 2674.55 | changed to aluminium spiral core barrel with Danish pump (hard springs), same drill head | 1.125 | 1.125 | 90.0 | |||||
1299 | 2005-12-28T16:38 | 11.0 | 1 | 1759 | 2.00 | 2674.72 | changed to french shaft with lower valve; tuned head to nominal pitch 2.0; sharped cutter | 90.0 | |||||||
1300 | 2005-12-28T19:45 | 14.0 | 1 | 1519 | 2675.01 | 89.0 | |||||||||
1301 | 2005-12-28T22:00 | 26.0 | 1 | 739 | 2675.20 | 1.400 | 1.400 | 81.0 | 0.316 | 917.0 | -22.5 | ||||
1302 | 2005-12-29T00:05 | 35.0 | 1 | 908 | 4.00 | 2675.57 | 2.050 | 2.050 | |||||||
1303 | 2005-12-29T02:10 | 38.0 | 1 | 1551 | 2.00 | 2676.47 | 84.0 | ||||||||
1304 | 2005-12-29T04:30 | 32.0 | 1 | 1495 | 2.00 | 2676.45 | 1.920 | 1.920 | 86.0 | ||||||
1305 | 2005-12-29T06:35 | 34.0 | 1 | 1407 | 2.00 | 2676.91 | changed to plastic-spiral core barrel | 88.0 | |||||||
1306 | 2005-12-29T08:45 | 55.0 | 1 | 1517 | 1.00 | 2677.39 | 2.900 | 2.900 | 86.0 | ||||||
1307 | 2005-12-29T11:15 | 29.5 | 1 | 1408 | 2677.14 | 2.800 | 2.800 | 88.0 | |||||||
1308 | 2005-12-29T13:40 | 34.0 | 1 | 740 | 2677.65 | 87.0 | |||||||||
1309 | 2005-12-29T16:30 | 38.0 | 1 | 1217 | 2677.97 | 88.0 | |||||||||
1310 | 2005-12-29T18:35 | 22.0 | 1 | 1260 | 2678.19 | sharpened cutter and core catchers; tuned to 0/0.58/1.2 mm, nominal pitch 1.8 mm; one screw of plastic spiral lost | 92.0 | ||||||||
1311 | 2005-12-29T21:40 | 43.0 | 1 | 944 | 2.50 | 2678.59 | 1.950 | 1.950 | 92.0 | ||||||
1312 | 2005-12-29T23:35 | 40.0 | 1 | 1526 | 2.50 | 2679.21 | 1.950 | 1.950 | 86.0 | 0.333 | 918.0 | -24.0 | |||
1313 | 2005-12-30T02:00 | 33.0 | 1 | 1410 | 1.50 | 2679.57 | 1.950 | 1.950 | 88.0 | ||||||
1314 | 2005-12-30T04:10 | 46.5 | 1 | 1131 | 2.50 | 2680.45 | 2.000 | 2.000 | 87.0 | ||||||
1315 | 2005-12-30T06:25 | 38.0 | 2 | 1529 | 2.00 | 2680.79 | 89.0 | ||||||||
1316 | 2005-12-30T08:50 | 42.0 | 1 | 1265 | 2.00 | 2680.91 | changed damaged cutter | 2.200 | 2.200 | 88.0 | |||||
1317 | 2005-12-30T11:25 | 35.0 | 1 | 1238 | 2.00 | 2681.08 | 2.200 | 2.200 | 89.0 | ||||||
1318 | 2005-12-30T13:50 | 38.0 | 1 | 740 | 2.00 | 2681.52 | 1.600 | 1.600 | 88.0 | ||||||
1319 | 2005-12-30T16:48 | 31.0 | 1 | 1297 | 1.50 | 2681.64 | changed to cutter with chip breaking grooves; tuned 0/0.65/1.3 mm; nominal 2.0 mm | 90.0 | |||||||
1320 | 2005-12-30T18:55 | 36.0 | 1 | 1282 | 1.50 | 2682.16 | 1.500 | 1.500 | 90.0 | ||||||
1321 | 2005-12-30T21:45 | 41.0 | 1 | 1341 | 1.50 | 2682.22 | 1.430 | 1.430 | 94.0 | ||||||
1322 | 2005-12-30T23:30 | 38.0 | 1 | 1404 | 2.00 | 2682.92 | 1.590 | 1.590 | 82.0 | 0.353 | 918.0 | -24.0 | |||
1323 | 2005-12-31T01:45 | 35.0 | 1 | 1207 | 2.00 | 2683.33 | 1.580 | 1.580 | 84.0 | ||||||
1324 | 2005-12-31T04:00 | 38.0 | 1 | 1213 | 2.00 | 2683.72 | 1.580 | 1.580 | 87.0 | ||||||
1325 | 2005-12-31T06:20 | 39.0 | 1 | 1198 | 2.50 | 2684.20 | 1.550 | 1.550 | 89.0 | ||||||
1326 | 2005-12-31T08:15 | 32.0 | 1 | 667 | 1.50 | 2684.26 | 1.800 | 1.800 | 87.0 | ||||||
1327 | 2005-12-31T10:30 | 41.0 | 1 | 1063 | 2.50 | 2684.67 | 1.500 | 1.500 | 89.0 | ||||||
1328 | 2005-12-31T12:40 | 36.0 | 1 | 1245 | 2.00 | 2684.88 | 2.400 | 2.400 | 89.0 | ||||||
1329 | 2005-12-31T14:40 | 31.0 | 1 | 1327 | 2685.04 | 1.550 | 1.550 | 89.0 | |||||||
1330 | 2005-12-31T16:45 | 32.0 | 1 | 1411 | 2685.41 | 1.600 | 1.600 | 90.0 | |||||||
1331 | 2006-01-01T17:10 | 24.0 | 1 | 1179 | 1.50 | 2685.36 | 1.740 | 1.740 | 92.0 | ||||||
1332 | 2006-01-01T19:50 | 28.0 | 1 | 1614 | 2.50 | 2686.21 | 95.0 | ||||||||
1333 | 2006-01-01T21:55 | 27.0 | 1 | 1355 | 0.00 | 2686.49 | 1.860 | 1.860 | 88.0 | 0.202 | 918.0 | -23.4 | |||
1334 | 2006-01-02T00:15 | 47.0 | 3 | 1498 | 3.00 | 2687.02 | cutter changed, new form | 2.000 | 2.000 | 90.0 | |||||
1335 | 2006-01-02T02:40 | 52.0 | 1 | 1539 | 2.50 | 2688.09 | 2.250 | 2.500 | 91.0 | ||||||
1336 | 2006-01-02T05:05 | 47.0 | 1 | 1427 | 2.50 | 2688.09 | 2.250 | 2.250 | 93.0 | ||||||
1337 | 2006-01-02T07:10 | 42.0 | 1 | 1132 | 1.50 | 2688.27 | 2.300 | 2.300 | 95.0 | ||||||
1338 | 2006-01-02T09:43 | 12.0 | 1 | 1196 | 1.00 | 2688.73 | 2.600 | 2.600 | 95.0 | ||||||
1339 | 2006-01-02T11:50 | 28.0 | 1 | 1101 | 2688.95 | 97.0 | |||||||||
1340 | 2006-01-02T14:10 | 35.0 | 1 | 1287 | 3.00 | 2689.21 | 1.650 | 1.650 | 98.0 | ||||||
1341 | 2006-01-02T16:15 | 21.0 | 1 | 1520 | 1.00 | 2689.35 | 2.200 | 2.200 | 84.0 | 0.408 | 917.0 | -23.0 | |||
1342 | 2006-01-02T18:30 | 34.0 | 1 | 1227 | 1.50 | 2689.57 | 85.0 | ||||||||
1343 | 2006-01-02T20:30 | 28.0 | 1 | 1370 | 1.00 | 2690.00 | 2.500 | 2.500 | 85.0 | ||||||
1344 | 2006-01-02T22:35 | 21.0 | 2 | 1178 | 2690.12 | 87.0 | |||||||||
1345 | 2006-01-03T00:50 | 3.0 | 1 | 1351 | 2690.45 | switched to core barrel with aluminium spirals and aluminium cutters at windows of outer barrel same drill head | 89.0 | ||||||||
1346 | 2006-01-03T02:55 | 16.0 | 1 | 970 | 2.00 | 2690.51 | changed to french pump, outer barrel ch., 1 shoe damaged changed | 91.0 | |||||||
1347 | 2006-01-03T05:30 | 2.0 | 1 | 835 | 0.50 | 2690.58 | 94.0 | ||||||||
1348 | 2006-01-03T08:10 | 20.0 | 1 | 1149 | 0.50 | 2690.72 | 2.300 | 2.300 | 90.0 | ||||||
1349 | 2006-01-03T10:30 | 16.0 | 1618 | 2690.77 | 2.100 | 2.100 | 91.0 | ||||||||
1350 | 2006-01-03T13:40 | 15.0 | 1 | 1457 | 2690.69 | 1.500 | 1.500 | 93.0 | |||||||
1351 | 2006-01-03T15:50 | 13.0 | 1462 | 2691.20 | 93.0 | ||||||||||
1352 | 2006-01-03T18:15 | 20.0 | 1352 | 1.00 | 2691.48 | drill head covered with frozen glycol | 1.750 | 1.750 | 97.0 | ||||||
1353 | 2006-01-03T21:35 | 32.0 | 1550 | 2.50 | 2691.81 | drill head covered with frozen glycol | 98.0 | ||||||||
1354 | 2006-01-04T00:00 | 124.0 | 7 | 1206 | 2692.98 | 500 g ethanol/water, 50%/50% | 85.0 | 0.350 | 918.0 | -24.0 | |||||
1355 | 2006-01-04T03:00 | 14.0 | 1 | 1571 | 2693.57 | 250 g ethanol/water, 50%/50% | 87.0 | ||||||||
1356 | 2006-01-04T06:40 | 15.0 | 1 | 1220 | 0.00 | 2693.53 | 400 g ethanol/water, 50%/50% | 90.0 | |||||||
1357 | 2006-01-04T10:35 | 25.0 | 1583 | 2693.53 | 89.0 | ||||||||||
1358 | 2006-01-04T13:40 | 64.0 | 1 | 981 | 6.50 | 2693.85 | 87.0 | ||||||||
1359 | 2006-01-04T16:25 | 42.0 | 1 | 1559 | 2.50 | 2694.53 | 89.0 | ||||||||
1360 | 2006-01-04T19:00 | 67.0 | 1 | 1382 | 5.00 | 2695.09 | 100 g ethanol/water, 50%/50% | 1.800 | 1.800 | 91.0 | |||||
1361 | 2006-01-04T21:30 | 106.0 | 1 | 1037 | 7.00 | 2696.08 | 125 ml ethanol/water, 50%/50% | 1.700 | 1.700 | 92.0 | |||||
1362 | 2006-01-04T23:48 | 54.0 | 1 | 1513 | 4.00 | 2696.19 | 100 ml ethanol/water, 50%/50% | 82.0 | 0.366 | 915.0 | -21.0 | ||||
1363 | 2006-01-05T02:15 | 69.0 | 2 | 1625 | 2697.39 | 90 ml ethanol/water, 50%/50% | 1.950 | 1.950 | 85.0 | ||||||
1364 | 2006-01-05T05:20 | 99.0 | 1 | 1161 | 7.00 | 2698.56 | 125 ml ethanol/water, 50%/50% | 1.950 | 1.950 | 88.0 | |||||
1365 | 2006-01-05T07:55 | 79.0 | 1 | 659 | 5.00 | 2699.34 | 125 ml ethanol/water, 50%/50% | 2.550 | 2.550 | 88.0 | |||||
1366 | 2006-01-05T10:25 | 125.0 | 1 | 1082 | 7.00 | 2699.98 | 121 ml ethanol/water, 50%/50% | 88.0 | |||||||
1367 | 2006-01-05T12:55 | 111.0 | 1 | 1407 | 7.50 | 2701.35 | 110 ml ethanol/water, 50%/50% | 1.850 | 1.850 | 88.0 | |||||
1368 | 2006-01-05T15:14 | 105.0 | 1 | 1357 | 7.00 | 2702.67 | 100 ml ethanol/water, 50%/50% | 1.670 | 1.670 | 89.0 | |||||
1369 | 2006-01-05T17:45 | 109.0 | 1 | 1242 | 6.00 | 2703.66 | 90 ml ethanol/water, 50%/50% | 1.700 | 1.700 | 90.0 | |||||
1370 | 2006-01-05T20:05 | 90.0 | 2 | 1773 | 5.00 | 2704.69 | 90 ml ethanol/water, 50%/50% | 91.0 | |||||||
1371 | 2006-01-05T23:10 | 77.0 | 2 | 1611 | 8.00 | 2705.66 | 100 ml ethanol/water, 50%/50% | 1.700 | 1.700 | 90.0 | |||||
1372 | 2006-01-06T02:30 | 80.0 | 1 | 1449 | 6.00 | 2706.44 | 121 ml ethanol/water, 50%/50% | 1.700 | 1.700 | 83.0 | 0.335 | 908.0 | -23.0 | ||
1373 | 2006-01-06T05:05 | 104.0 | 2 | 943 | 8.00 | 2707.41 | 110 ml ethanol/water, 50%/50% | 1.700 | 1.700 | 85.0 | |||||
1374 | 2006-01-06T07:30 | 98.0 | 1 | 1165 | 5.50 | 2708.31 | 110 ml ethanol/water, 50%/50% | 1.600 | 1.600 | 86.0 | |||||
1375 | 2006-01-06T10:10 | 102.0 | 1 | 1523 | 6.00 | 2712.20 | 110 ml ethanol/water, 50%/50% | 1.530 | 1.530 | 86.0 | |||||
1376 | 2006-01-06T13:15 | 79.0 | 1 | 1086 | 7.00 | 2709.98 | 110 ml ethanol/water, 50%/50% | 1.800 | 1.800 | 87.0 | |||||
1377 | 2006-01-06T15:50 | 108.0 | 1 | 1192 | 6.00 | 2711.56 | 110 ml ethanol/water, 50%/50% | 1.620 | 1.620 | 86.0 | |||||
1378 | 2006-01-06T18:15 | 107.0 | 2 | 1617 | 7.00 | 2712.40 | 110 ml ethanol/water, 50%/50% | 1.850 | 1.850 | 89.0 | |||||
1379 | 2006-01-06T21:05 | 83.0 | 2 | 1260 | 6.00 | 2713.46 | 110 ml ethanol/water, 50%/50% | 1.700 | 1.700 | 90.0 | 0.345 | 830.0 | -23.0 | ||
1380 | 2006-01-06T23:20 | 103.0 | 3 | 1312 | 8.00 | 2714.49 | 110 ml ethanol/water, 50%/50% | 91.0 | |||||||
1381 | 2006-01-07T02:00 | 95.0 | 1 | 1626 | 7.00 | 2715.71 | 110 ml ethanol/water, 50%/50% | 90.0 | |||||||
1382 | 2006-01-07T04:25 | 105.0 | 1 | 852 | 7.00 | 2716.73 | 110 ml ethanol/water, 50%/50% | 93.0 | |||||||
1383 | 2006-01-07T06:35 | 85.0 | 1 | 1666 | 5.00 | 2717.53 | 110 ml ethanol/water, 50%/50% | 1.780 | 1.780 | 94.0 | |||||
1384 | 2006-01-07T09:30 | 92.0 | 1 | 1460 | 5.00 | 2718.39 | 110 ml ethanol/water, 50%/50% | 1.680 | 1.680 | 90.0 | |||||
1385 | 2006-01-07T12:21 | 100.0 | 2 | 1023 | 6.50 | 2719.02 | 110 ml ethanol/water, 50%/50% | 1.900 | 1.900 | 92.0 | |||||
1386 | 2006-01-07T15:10 | 106.0 | 2 | 1731 | 6.00 | 2720.27 | 110 ml ethanol/water, 50%/50% | 90.0 | |||||||
FR59 | 2006-01-08T07:50 | 5.00 | 2720.40 | 89.0 | |||||||||||
1387 | 2006-01-08T13:05 | 86.0 | 2 | 1353 | 6.00 | 2720.75 | 110 ml ethanol/water, 50%/50% | 1.970 | 1.970 | 77.0 | |||||
1388 | 2006-01-08T15:25 | 87.0 | 2 | 1720 | 5.00 | 2721.73 | 110 ml ethanol/water, 50%/50% | 2.070 | 2.070 | 78.0 | |||||
1389 | 2006-01-08T17:50 | 104.0 | 1 | 1654 | 5.50 | 2722.91 | 110 ml ethanol/water, 50%/50% | 1.810 | 1.810 | 79.0 | |||||
1390 | 2006-01-08T20:15 | 80.0 | 1 | 1344 | 5.00 | 2723.86 | 110 ml ethanol/water, 50%/50% | 1.970 | 1.970 | 80.0 | |||||
1391 | 2006-01-08T22:29 | 97.0 | 1 | 1813 | 5.00 | 2724.61 | 110 ml ethanol/water, 50%/50% | 81.0 | |||||||
1392 | 2006-01-09T00:55 | 73.0 | 1 | 1515 | 6.00 | 2725.91 | 110 ml ethanol/water, 50%/50% | 83.0 | |||||||
1393 | 2006-01-09T03:35 | 106.0 | 2 | 1423 | 8.50 | 2726.80 | 110 ml ethanol/water, 50%/50% | 1.060 | 1.060 | 84.0 | |||||
1394 | 2006-01-09T06:30 | 108.0 | 1 | 1274 | 6.00 | 2727.63 | 110 ml ethanol/water, 50%/50% | 1.080 | 1.080 | 86.0 | |||||
1395 | 2006-01-09T09:30 | 80.0 | 1 | 1600 | 4.50 | 2728.16 | 110 ml ethanol/water, 50%/50% | 1.900 | 1.900 | 86.0 | |||||
1396 | 2006-01-09T12:00 | 71.0 | 1 | 1395 | 4.50 | 2729.10 | 110 ml ethanol/water, 50%/50% | 1.950 | 1.950 | 86.0 | |||||
1397 | 2006-01-09T15:00 | 89.0 | 4 | 1371 | 6.00 | 2729.88 | 110 ml ethanol/water, 50%/50% | 1.620 | 1.620 | 88.0 | |||||
1398 | 2006-01-09T17:10 | 97.0 | 1 | 1350 | 6.00 | 2731.03 | 110 ml ethanol/water, 50%/50% | 1.910 | 1.910 | 89.0 | |||||
1399 | 2006-01-09T19:20 | 93.0 | 1 | 1516 | 6.00 | 2731.85 | 110 ml ethanol/water, 50%/50% | 1.960 | 1.960 | 90.0 | |||||
1400 | 2006-01-09T21:30 | 98.0 | 2 | 1328 | 7.50 | 2732.89 | 110 ml ethanol/water, 50%/50% | 1.640 | 1.640 | 90.0 | |||||
1401 | 2006-01-10T02:10 | 42.0 | 2 | 1617 | 2733.44 | 110 ml ethanol/water, 50%/50% | 81.0 | ||||||||
1402 | 2006-01-10T05:05 | 18.0 | 1 | 1507 | 3.50 | 2733.89 | 110 ml ethanol/water, 50%/50% | 84.0 | |||||||
1403 | 2006-01-10T07:45 | 96.0 | 1 | 1255 | 5.00 | 2734.39 | 110 ml ethanol/water, 50%/50% | 1.690 | 1.690 | 88.0 | |||||
1404 | 2006-01-10T10:00 | 95.0 | 1 | 1286 | 5.00 | 2735.44 | 110 ml ethanol/water, 50%/50% | 1.850 | 1.850 | 86.0 | |||||
1405 | 2006-01-10T12:20 | 103.0 | 1 | 1814 | 6.00 | 2736.36 | 110 ml ethanol/water, 50%/50% | 1.970 | 1.970 | 86.0 | |||||
1406 | 2006-01-10T15:20 | 69.0 | 1 | 1177 | 6.00 | 2737.37 | 110 ml ethanol/water, 50%/50% | 1.930 | 1.930 | 87.0 | |||||
1407 | 2006-01-10T17:50 | 105.0 | 1 | 1298 | 6.50 | 2738.16 | 110 ml ethanol/water, 50%/50% | 1.850 | 1.850 | 89.0 | |||||
1408 | 2006-01-10T20:00 | 82.0 | 1 | 707 | 6.50 | 2739.21 | 110 ml ethanol/water, 50%/50% | 1.840 | 1.840 | 89.0 | |||||
1409 | 2006-01-10T22:10 | 96.0 | 1 | 803 | 7.00 | 2740.10 | 110 ml ethanol/water, 50%/50% | 1.850 | 1.850 | 89.0 | |||||
1410 | 2006-01-11T00:40 | 72.0 | 3 | 1813 | 4.80 | 2740.58 | 110 ml ethanol/water, 50%/50% | 1.850 | 1.850 | 82.0 | |||||
1411 | 2006-01-11T04:00 | 59.0 | 2 | 1636 | 6.00 | 2741.37 | 110 ml ethanol/water, 50%/50% | 84.0 | |||||||
1412 | 2006-01-11T07:05 | 18.0 | 1 | 1267 | 2.00 | 2741.60 | 130 ml ethanol/water, 50%/50% | 85.0 | |||||||
1413 | 2006-01-11T09:25 | 74.0 | 1 | 1378 | 5.00 | 2742.20 | 110 ml ethanol/water, 50%/50% | 1.900 | 1.900 | 85.0 | |||||
1414 | 2006-01-11T11:50 | 93.0 | 1 | 1280 | 6.50 | 2743.15 | 110 ml ethanol/water, 50%/50% | 1.920 | 1.920 | 86.0 | |||||
1415 | 2006-01-11T14:35 | 72.0 | 2 | 1064 | 5.50 | 2743.86 | 110 ml ethanol/water, 50%/50% | 1.810 | 1.810 | 86.0 | |||||
1416 | 2006-01-11T17:10 | 99.0 | 2 | 1328 | 7.00 | 2744.66 | 110 ml ethanol/water, 50%/50% | 1.990 | 1.990 | 87.0 | |||||
1417 | 2006-01-11T19:50 | 83.0 | 1 | 1807 | 6.00 | 2745.62 | 110 ml ethanol/water, 50%/50% | 2.030 | 2.030 | 89.0 | |||||
1418 | 2006-01-11T22:45 | 41.0 | 1 | 1818 | 3.50 | 2746.06 | 110 ml ethanol/water, 50%/50% | 89.0 | |||||||
1419 | 2006-01-12T01:30 | 90.0 | 1 | 1419 | 6.50 | 2746.97 | 110 ml ethanol/water, 50%/50% | 1.870 | 1.870 | 81.0 | |||||
1420 | 2006-01-12T04:05 | 22.0 | 1 | 1508 | 2.00 | 2747.24 | 110 ml ethanol/water, 50%/50% | 84.0 | |||||||
1421 | 2006-01-12T07:10 | 80.0 | 1 | 1493 | 6.50 | 2748.10 | 130 ml ethanol/water, 50%/50% | 1.860 | 1.860 | 86.0 | |||||
1422 | 2006-01-12T09:35 | 70.0 | 1 | 1272 | 4.50 | 2748.58 | 110 ml ethanol/water, 50%/50% | 2.100 | 2.100 | 85.0 | |||||
1423 | 2006-01-12T11:55 | 44.0 | 1 | 1298 | 3.00 | 2748.80 | 100 ml ethanol/water, 50%/50% | 2.150 | 2.150 | 85.0 | |||||
1424 | 2006-01-12T14:50 | 58.0 | 1 | 1816 | 3.00 | 2749.55 | 100 ml ethanol/water, 50%/50% | 2.000 | 2.000 | 87.0 | |||||
1425 | 2006-01-12T17:30 | 16.0 | 1 | 1527 | 1.50 | 2748.71 | 100 ml ethanol/water, 50%/50% | 88.0 | |||||||
1426 | 2006-01-12T20:15 | 61.0 | 1 | 1753 | 6.00 | 2750.52 | 130 ml ethanol/water, 50%/50% | 1.810 | 1.810 | 89.0 | |||||
1427 | 2006-01-12T22:42 | 51.0 | 1 | 1813 | 0.00 | 2751.04 | 140 ml ethanol/water, 50%/50% | 1.850 | 1.850 | 79.0 | |||||
1428 | 2006-01-13T01:10 | 43.0 | 1 | 1341 | 3.50 | 2751.55 | 150 ml ethanol/water, 50%/50% | 80.0 | |||||||
1429 | 2006-01-13T04:00 | 28.0 | 2 | 1623 | 2.00 | 2752.13 | 110 ml ethanol/water, 50%/50% | 84.0 | |||||||
1430 | 2006-01-13T06:40 | 70.0 | 1 | 1473 | 4.00 | 2752.61 | 200 ml ethanol/water, 50%/50% | 84.0 | |||||||
1431 | 2006-01-13T09:40 | 10.0 | 1 | 1819 | 0.00 | 2753.11 | 200 ml ethanol/water, 50%/50% | 84.0 | |||||||
1432 | 2006-01-13T12:30 | 15.0 | 1 | 1144 | 0.00 | 2752.62 | 200 ml ethanol/water, 50%/50% | 84.0 | |||||||
1433 | 2006-01-13T15:28 | 24.0 | 1 | 1816 | 1.50 | 2751.36 | changed other head with pitch 2.4 and splitter cutter design | 85.0 | |||||||
1434 | 2006-01-13T18:15 | 15.0 | 1 | 1217 | 0.00 | 2751.76 | 85.0 | ||||||||
1435 | 2006-01-13T21:01 | 0.0 | 0 | 479 | 0.00 | 2751.26 | lost core barrel | ||||||||
1436 | 2006-01-14T23:00 | 0.0 | 0 | 1226 | 0.00 | 2751.26 | fishing for core barrel | ||||||||
1437 | 2006-01-14T01:15 | 16.0 | 1 | 1533 | 3.50 | 2754.02 | 50 ml ethanol/water, 50%/50% | 79.0 | |||||||
1438 | 2006-01-14T03:40 | 10.0 | 1 | 1521 | 2.00 | 2753.97 | 75 ml ethanol/water, 50%/50% | 81.0 | |||||||
1439 | 2006-01-14T05:55 | 53.0 | 1 | 1768 | 6.00 | 2754.08 | 82.0 | ||||||||
1440 | 2006-01-14T08:40 | 26.5 | 1 | 1309 | 3.50 | 2754.15 | 1.800 | 1.800 | 79.0 | ||||||
1441 | 2006-01-14T11:35 | 42.0 | 1 | 1433 | 2.50 | 2754.12 | 50 ml ethanol/water, 50%/50% | 1.760 | 1.760 | 81.0 | |||||
1442 | 2006-01-14T13:57 | 33.0 | 1 | 1604 | 2.50 | 2754.71 | 50 ml ethanol/water, 50%/50% | 1.900 | 1.900 | 82.0 | |||||
1443 | 2006-01-14T16:42 | 41.0 | 2 | 1760 | 3.00 | 2755.34 | 70 ml ethanol/water, 50%/50% | 1.840 | 1.840 | 84.0 | |||||
FR60 | 2006-01-15T09:15 | 5.00 | 2755.50 | 86.0 | |||||||||||
1444 | 2006-01-15T13:09 | 83.0 | 1 | 1505 | 5.50 | 2756.17 | 100 ml ethanol/water, 50%/50% | 2.050 | 2.050 | 86.0 | |||||
1445 | 2006-01-15T15:27 | 77.0 | 2 | 1635 | 6.00 | 2757.06 | 100 ml ethanol/water, 50%/50% | 2.100 | 2.100 | 87.0 | |||||
1446 | 2006-01-15T20:08 | 19.0 | 1 | 1882 | 2757.18 | 100 ml ethanol/water, 50%/50% | 1.800 | 1.800 | 87.0 | ||||||
1447 | 2006-01-15T22:55 | 45.0 | 1 | 1650 | 6.00 | 2757.78 | 50 ml ethanol/water, 50%/50% | 87.0 | |||||||
1448 | 2006-01-16T01:20 | 63.0 | 1 | 1538 | 6.00 | 2758.76 | 75 ml ethanol/water, 50%/50% | 2.050 | 2.050 | 90.0 | |||||
1449 | 2006-01-16T04:00 | 80.0 | 6 | 1934 | 5.50 | 2759.59 | 75 ml ethanol/water, 50%/50% | 93.0 | |||||||
1450 | 2006-01-16T07:40 | 11.0 | 1 | 1654 | 1.00 | 2759.36 | 75 ml ethanol/water, 50%/50% | 94.0 | |||||||
1451 | 2006-01-16T10:10 | 53.0 | 2 | 1820 | 7.00 | 2759.80 | 1.770 | 1.770 | 91.0 | 0.410 | 830.0 | -23.0 | |||
1452 | 2006-01-16T13:50 | 17.0 | 1 | 1404 | 3.00 | 2759.97 | 80.0 | ||||||||
1453 | 2006-01-16T16:45 | 15.0 | 1 | 1375 | 3.00 | 2759.90 | 75 ml ethanol/water, 50%/50%; changed to pump | 81.0 | |||||||
1454 | 2006-01-16T20:15 | 26.0 | 1 | 874 | 4.50 | 2760.35 | 82.0 | ||||||||
1455 | 2006-01-16T23:40 | 14.0 | 1 | 911 | 5.00 | 2760.90 | 82.0 | ||||||||
1456 | 2006-01-17T03:55 | 52.0 | 2 | 1389 | 5.00 | 2761.77 | 220 ml ethanol/water, 50%/50%; changed to booster | 84.0 | |||||||
1457 | 2006-01-17T07:35 | 6.0 | 1 | 1895 | 2761.35 | 250 ml ethanol/water, 50%/50% | 85.0 | ||||||||
1458 | 2006-01-17T11:54 | 1188 | 2756.23 | 500 ml ethanol/water, 50%/50%; shortage - very short core piece not measurable | 80.0 | ||||||||||
FR61 | 2006-01-17T15:00 | 2180.00 | bailer - aborted due to shortage | ||||||||||||
FR62 | 2006-01-17T18:20 | 2760.09 | bailer - heavily iced at bottom | 80.0 | |||||||||||
1459 | 2006-01-17T21:55 | 2757.86 | no penetration | 85.0 | |||||||||||
1460 | 2006-01-18T02:30 | 2756.89 | 81.0 | 0.151 | 830.0 | -23.0 |